Skip to content

Instantly share code, notes, and snippets.

@RuBiCK
Created April 1, 2020 10:45
Show Gist options
  • Save RuBiCK/4fc768e42469da427c173e3ef77fed6a to your computer and use it in GitHub Desktop.
Save RuBiCK/4fc768e42469da427c173e3ef77fed6a to your computer and use it in GitHub Desktop.
Marlin firmware - Invalid Mesh (229-233 lines)
Changing monitoring state from "Offline" to "Detecting serial port"
Serial port list: [u'/dev/ttyUSB1']
Connecting to: /dev/ttyUSB1
Changing monitoring state from "Detecting serial port" to "Opening serial port"
Connected to: Serial<id=0x716c8d70, open=True>(port='/dev/ttyUSB1', baudrate=250000, bytesize=8, parity='N', stopbits=1, timeout=10.0, xonxoff=False, rtscts=False, dsrdtr=False), starting monitor
Changing monitoring state from "Opening serial port" to "Connecting"
Send: N0 M110 N0*125
Send: N0 M110 N0*125
Recv: Error:checksum mismatch, Last Line: 0
Recv: Resend: 1
Recv: ok
Changing monitoring state from "Connecting" to "Operational"
Send: N0 M110 N0*125
Recv: ok
Send: N1 M115*39
Recv: ok
Send: N2 M21*18
Recv: FIRMWARE_NAME:Marlin bugfix-2.0.x (GitHub) SOURCE_CODE_URL:https://github.com/MarlinFirmware/Marlin PROTOCOL_VERSION:1.0 MACHINE_TYPE:FLSUN QQ-S EXTRUDER_COUNT:1 UUID:cede2a2f-41a2-4748-9b12-c55c62f367ff
Recv: Cap:SERIAL_XON_XOFF:0
Recv: Cap:BINARY_FILE_TRANSFER:0
Recv: Cap:EEPROM:1
Recv: Cap:VOLUMETRIC:1
Recv: Cap:AUTOREPORT_TEMP:1
Recv: Cap:PROGRESS:0
Recv: Cap:PRINT_JOB:1
Recv: Cap:AUTOLEVEL:1
Recv: Cap:Z_PROBE:1
Recv: Cap:LEVELING_DATA:1
Recv: Cap:BUILD_PERCENT:0
Recv: Cap:SOFTWARE_POWER:0
Recv: Cap:TOGGLE_LIGHTS:0
Recv: Cap:CASE_LIGHT_BRIGHTNESS:0
Recv: Cap:EMERGENCY_PARSER:0
Recv: Cap:PROMPT_SUPPORT:0
Recv: Cap:AUTOREPORT_SD_STATUS:0
Recv: Cap:THERMAL_PROTECTION:1
Recv: Cap:MOTION_MODES:0
Recv: Cap:CHAMBER_TEMPERATURE:0
Recv: ok
Send: M420V1
Recv: echo:SD init fail
Recv: ok
Send: M851
[...]
Recv: echo:Invalid mesh.
Recv: echo:Bed Leveling OFF
Recv: ok
Send: M155 S2
Recv: Probe Offset X0.00 Y0.00 Z0.00
Recv: ok
Recv: ok
Send: M115
Recv: FIRMWARE_NAME:Marlin bugfix-2.0.x (GitHub) SOURCE_CODE_URL:https://github.com/MarlinFirmware/Marlin PROTOCOL_VERSION:1.0 MACHINE_TYPE:FLSUN QQ-S EXTRUDER_COUNT:1 UUID:cede2a2f-41a2-4748-9b12-c55c62f367ff
Recv: Cap:SERIAL_XON_XOFF:0
Recv: Cap:BINARY_FILE_TRANSFER:0
Recv: Cap:EEPROM:1
Recv: Cap:VOLUMETRIC:1
Recv: Cap:AUTOREPORT_TEMP:1
Recv: Cap:PROGRESS:0
Recv: Cap:PRINT_JOB:1
Recv: Cap:AUTOLEVEL:1
Recv: Cap:Z_PROBE:1
Recv: Cap:LEVELING_DATA:1
Recv: Cap:BUILD_PERCENT:0
Recv: Cap:SOFTWARE_POWER:0
Recv: Cap:TOGGLE_LIGHTS:0
Recv: Cap:CASE_LIGHT_BRIGHTNESS:0
Recv: Cap:EMERGENCY_PARSER:0
Recv: Cap:PROMPT_SUPPORT:0
Recv: Cap:AUTOREPORT_SD_STATUS:0
Recv: Cap:THERMAL_PROTECTION:1
Recv: Cap:MOTION_MODES:0
Recv: Cap:CHAMBER_TEMPERATURE:0
Recv: ok
Send: M504
Recv: echo:EEPROM OK
Recv: ok
Send: M501
Recv: echo:V74 stored settings retrieved (956 bytes; crc 43676)
Recv: echo: G21 ; Units in mm (mm)
Recv: echo: M149 C ; Units in Celsius
Recv:
Recv: echo:Filament settings: Disabled
Recv: echo: M200 D1.75
Recv: echo: M200 D0
Recv: echo:Steps per unit:
Recv: echo: M92 X100.00 Y100.00 Z100.00 E399.39
Recv: echo:Maximum feedrates (units/s):
Recv: echo: M203 X200.00 Y200.00 Z200.00 E200.00
Recv: echo:Maximum Acceleration (units/s2):
Recv: echo: M201 X1000.00 Y1000.00 Z1000.00 E1000.00
Recv: echo:Acceleration (units/s2): P<print_accel> R<retract_accel> T<travel_accel>
Recv: echo: M204 P1000.00 R1000.00 T1000.00
Recv: echo:Advanced: B<min_segment_time_us> S<min_feedrate> T<min_travel_feedrate> X<max_x_jerk> Y<max_y_jerk> Z<max_z_jerk> E<max_e_jerk>
Recv: echo: M205 B20000.00 S0.00 T0.00 X10.00 Y10.00 Z10.00 E5.00
Recv: echo:Auto Bed Leveling:
Recv: echo: M420 S0
Recv: echo:Endstop adjustment:
Recv: echo: M666 X-1.35 Y0.00 Z-2.19
Recv: echo:Delta settings: L<diagonal_rod> R<radius> H<height> S<segments_per_s> XYZ<tower angle corrections>
Recv: echo: M665 L280.00 R141.77 H377.90 S200.00 X-0.11 Y0.21 Z-0.10
Recv: echo:Material heatup parameters:
Recv: echo: M145 S0 H200 B60 F0
Recv: echo: M145 S1 H235 B80 F0
Recv: echo:PID settings:
Recv: echo: M301 P12.60 I0.84 D46.95
Recv: echo: M304 P325.10 I63.35 D417.10
Recv: echo:Z-Probe Offset (mm):
Recv: echo: M851 X0.00 Y0.00 Z0.00
Recv: echo:Stepper motor currents:
Recv: echo: M907 X1030 Z1030 E1030
Recv: echo:Filament load/unload lengths:
Recv: echo: M603 L700.00 U800.00
Recv: ok
Send: M420V1
Recv: echo:Invalid mesh. ***************************************
Recv: echo:Bed Leveling OFF ***************************************
Recv: ok
Send: M851
Recv: Probe Offset X0.00 Y0.00 Z0.00
Recv: ok
Send: M155 S2
Sign up for free to join this conversation on GitHub. Already have an account? Sign in to comment