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@mmcelhan
Created November 10, 2019 18:50
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surfaceFailureDate,surfaceFailureType,surfaceFailureComponent,surfaceFailureSubComponent,surfaceFailureManufacturer,surfaceFailureModel,surfaceFailureRootCause,surfaceFailureDamages,anonymized_user,anonymized_asset,anonymized_latitude,anonymized_longitude
12/15/2017,Separator,Temp Control System,Pilot Valve,,,,Tripped out. Reset Burner ,user_156,asset_816,48.20742159,-103.6136759
7/4/2018,Wellhead,Tubing,,,,hydrate,Hydrate in wellhead. Methanol going. ,user_107,asset_1980,,
3/17/2018,Compressor,Compressor (Recip),Scrubber Level,,,,Drained scrubbers,user_46,asset_1841,48.0614644,-104.8417043
3/10/2018,Gas Scrubber Separator,ESD,,,,,Issue: well called out shut in alarm. (INT) valve fault Root Cause: not sure I drained both scrubber and they were dry i drained the desi it was dry as well. i checked all the pressure setting everything looked good so i am not sure it it came from Williams end and froze but broke before i got there. Fix: turned well back on and returned to service ,user_136,asset_1437,48.1470144,-103.6180489
10/3/2019,Separator,Choke Valve/Loop,,,,Freezing,"Found pad shut in do to low unit pressure, and entire fuel gas system flooded. jumped pad back on drained all fuel gas lines, scrubbers and desi. Tested all dumps lit burners and SCCs and rtpd well.",user_18,asset_1524,,
6/6/2019,Separator,Choke Valve,Body,,,,The choke stem was seized in the body and needed to be repaired.,user_68,asset_345,43.56424,-91.351691
12/3/2017,Fuel Gas/Start Gas,Regulator,,,,,"Issue: pad down on low unit pressure Root Cause: all the wells are plunger wells so when they all shut in at the same time the 2 burners, 4 glycol pumps, 6 meth pumps, 4 SCC's use up all the unit pressure and then the pad shuts in Fix: once got pad back on I left one well flowing to keep the pad pressured up. Long Term Fix is there is a buy back line there it needs to be put into service ",user_136,asset_492,48.2593814,-102.9010955
10/7/2018,SWD System,Particle Filter,Element,,,,"dirty filters, caused by dirty tanks",user_31,asset_308,43.252261,-115.0567324
1/6/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"Vented well due to being loaded. Plunger arrived, RTP'd well, started cycles, and return to optimizer.",user_141,asset_71,48.1470144,-103.6180489
3/23/2019,Separator,Liquid Dumps,Body,Fisher,,Freezing,+SEPARATOR VESSEL AND FUEL SCRUBBER FULL OF LIQUIDS- WILL NEED DRAINED WHEN RTP'D,user_34,asset_1983,43.56424,-91.351691
10/2/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,Burner out unit froze,user_3,asset_763,47.90439701,-103.4795154
1/28/2018,Gas Scrubber Separator,Dump Line,,,,Freezing,Scrubber on line heater filled up with liquid and shut off burners. Drained and started burners. ,user_156,asset_1600,48.3606323,-103.6349993
9/4/2018,Wellhead,Tubing,,,,hydrate,"plunger was froze in lubricator, meth pump has blown rupture disc, ",user_37,asset_184,43.56424,-91.351691
12/4/2018,Separator,Temp Control System,Thermostat,,,,"OPS: Found bath temp set points @ 90 degrees F and the choke pinched back to a 38/64. The combination of low bath temp and JT effect coming from a pinched choke allowed the Hi/lo to freeze, causing unit PSI loss. OPS RTP'ed well, verified bath temp to 120 degrees and opened choke fully. ",user_54,asset_409,48.1470144,-103.6180489
4/23/2017,SWD System,SWD Pump,Other,Other,Other,Other,Pump down due to plugged filters,user_141,asset_715,48.1470144,-103.6180489
5/27/2019,Chemical System,Pump,Check Valve,Texam,HBC1,Air Locked,Timberline pump not running fast enough to keep check valve functional.,user_54,asset_314,43.56424,-91.351691
5/6/2019,Separator,Liquid Dumps,Float,Norriseal,,Trash,W/M. asked to remove rat nests from inside unit and wash out inside vessel. the nests were really big and alot of sand in vessel. compleated,user_77,asset_672,46.2356189,-100.6010498
1/25/2018,Wellhead,Tubing,,,,,Tubing transmitter was frozen.,user_48,asset_1497,48.22592053,-103.5947778
3/28/2018,Wellhead,Tubing,,,,hydrate,Equalized well ,user_46,asset_2094,48.0614644,-104.8417043
12/7/2017,Instrumentation,Meter,Orifice Plate,Bristol,1,Freeze,,user_13,asset_2160,48.1470144,-103.6180489
5/28/2018,Flare System,Flare Header,Instrumentation,,,,Mon 25-1 SCC callout relit SCC.,user_71,asset_441,48.1470144,-103.6180489
6/19/2019,Separator,Sales Valve,Body,Valvcon,,Washed Out,Replaced sales line cyclonic valve,user_21,asset_621,46.2356189,-100.6010498
5/19/2019,Compressor - Gas Lift,Motor,Switch Gear,,,,"Call out compressor down, got to location compressor down on low oil, appeared to be fine restarted and back into service",user_63,asset_2046,,
9/25/2018,Flare System,Flare Header,Instrumentation,,,,Issue: during my walk around i found SCC # 3 down Root Cause: down on Master power failure. Fix: was able to rest and restart the Abutec SCC using there on bard controller ,user_170,asset_1383,43.56424,-91.351691
5/11/2019,Surface Location,Lease Road,,,,Weather,Culverts at entrance and exit of location have been damaged. Will write a work order.,user_55,asset_1489,,
11/4/2018,Flare System,Flare Header,Instrumentation,,,,Issue: Arrow Dispatched to location for big producer check Root Cause: during my walk around i found SCC # 3 down on flame failure. looks like with the cooler temps so the SCC's are not running as hard along with the hi winds blew the pilot out Fix: relight using the onboard auto starter ,user_170,asset_1383,48.1470144,-103.6180489
5/26/2019,Tanks/Pits,Flare/Combuster,,,,,"all scc's out, relit",user_31,asset_1103,43.56424,-91.351691
3/12/2019,Separator,Choke Valve/Loop,,,,Freezing,Cyclonic valve on sales line is leaking and needs replaced.,user_108,asset_696,,
4/17/2018,Dehy,WFS Issue,,,,,High line pressure swings in area. Unknown WFS root cause. Swings happen often causing deferral.,user_107,asset_2230,,
4/25/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash,"Issue: well still on a pinched choke from bringing it back on Root Cause: was trying to not over run the dumps. well flowing temp is 71deg, after line heater 119deg, sales temp 110deg dumps keeping up nicely Fix: pressure down and flow temps are up finished opening the choke ",user_136,asset_567,48.2595694,-102.9009394
10/20/2019,Gas Scrubber Separator,Dump Line,,,,Freezing,Drained fuel gas scrubber took about 2 seconds to 3 seconds on each scrubber and thumbed dumps ,user_76,asset_1216,46.2356189,-100.6010498
1/26/2018,Tanks/Pits,Flare/Combuster,,,,,Pilot out. Maybe caused by wind. Relit. ,user_156,asset_351,48.15584455,-103.4277558
10/26/2018,Wellhead,Cyclonic Valve,Actuator,,,Freezing,Old style actuator did not have torque limiter,user_12,asset_1368,48.1470144,-103.6180489
4/29/2019,Separator Inlet Valve (XV),Pneumatic Control System,Vent,,,,Gasket on hi/lo bad blowing gas to atmosphere. Replaced gasket and packing in hi/lo. Root cause is from extended use over time normal wear and tear,user_147,asset_609,,
10/23/2017,Instrumentation,Transmitter,3N1 MVT,ABB,1151,Calibration Issue,,user_113,asset_732,40.5262342,-113.8824849
5/24/2018,Flare System,Flare Header,Regulator,,,,"rain took scc out , adjust regulator to pilot",user_122,asset_2108,48.0614644,-104.8417043
6/7/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_1489,48.1001884,-103.5870227
10/30/2019,Separator,Fuel Supply System, Big Joe Regulator,,,freeze,Arrived onsite and found both wells esd with no interlock.attempted to jump pressure into both units but had no pressure on fuel gas scrubbers. Went over to fuel gas separator and also had zero psi. Fuel gas is frozen in between the high pressure separator and the fuel gas separator but cant identify exactly where due to the lack of bleed points in the line. Fuel gas line is clear from the high pressure separator all the way to where it drops down into the rack. Getting no pressure at the bleed point in front of the fuel gas separator. Mike and I attempted to thaw line out for several hours but we were unsuccessful. Went over to the solar glycol pumps to try and get them running since the glycol bath was still 120 degrees.(both pumps down when we got to location). Could not get either pump to start. Opened up trido boxes and found screens blank on both pumps but we have enough voltage. Spoke with team lead and maintenance team. Maintenance team informed us that this issue is caused by a high voltage??? These pumps supply heat trace to the fuel gas line (which is frozen) and the dump line to tanks (which is frozen). The team is not aware of any solution to fix these issues at this time. We decided to leave location down and shut in until we can get pumps fixed. Makes no sense to thaw out location and put wells back to sales with no glycol pumps. Blew down equipment as best as we could which wasn't very good because the dumps are frozen. Contacted team lead and asked him to get heaters out to location ,user_120,asset_2046,,
11/24/2017,Heat Medium,Surge Tank,Shell,,,,"got to location and found, liquid coming out of glycol bath, location was safe to walk in and shut pumps off , contacted team lead and contacted IBEX to come pull down level in bath and clean up any standing liquid, waited on location for IBEX to protect people and animals from harm,",user_122,asset_793,48.0614644,-104.8417043
12/29/2017,Separator,Choke Valve/Loop,,,,Freezing,"Inlet valves froze, lost unit pressure and heat trace, production tanks now froze. Unit and heat trace now up and running, will get tanks hot oiled and hauled",user_163,asset_2059,48.1470144,-103.6180489
1/15/2018,Heater Treater,Burner,BMS,,,Pilot Went Out,Issue: Sep (A) found bath was 41deg on the HMI Root Cause: found the glyocl is low so the pumps are not moving heat trace then the fuel gas flooded and froze taking it all the way down Fix: got unit back on and thawed out ,user_136,asset_793,48.2608782,-102.900126
1/29/2019,Heat Medium,Pump,Process Indicator,Texsteam,HBC1,Air Locked,"2 glycol pumps on bath A won't take a prime, possible level issue or suction line, appears to be full, wasn't able to get pumps to prime",user_31,asset_1581,43.56424,-91.351691
3/29/2018,Wellhead,Tubing,,,,,Well loaded needed a vent ,user_46,asset_1973,48.0614644,-104.8417043
3/19/2017,Gas Scrubber,Dump Line,Dump Line,Other,Other,Other,"Replaced 7 - 1"" valves on dump lines.",user_161,asset_1815,48.2648866,-102.9262095
5/20/2017,Sales Valve (PV),Elec.System,,,,,"Need to have automation look at sales line cyclonic, it is not opening. Optimizer did everything he could to open with no luck",user_141,asset_1723,48.1470144,-103.6180489
2/25/2018,Tanks/Pits,Flare/Combuster,,,,,Attempted to break freeze on fuel gas for scc’s. Thawed on it for 45min couldn’t get it to break. Left it isolated and tagged ,user_172,asset_1760,,
12/12/2018,Separator,Choke Valve/Loop,,,,Freezing,Control valve for 17-1 and 17-80 are in the front of the unit before it goes into glycol bath. This causes the cyclonic to freeze when it opens or closes and cyclonic goes down on high torque limit. Control valve needs to be moved down stream of the glycol bath or a better valve than a cyclonic needs to be installed. Thawed out cyclonic and removed cycles to free flow the well. This will hopefully prevent daily freezing and site visit. ,user_15,asset_314,43.56424,-91.351691
4/27/2018,Instrumentation,Tank Level,Probe,,,Weather, 5. Coal Gulch A 11-50 - Condo Tank #3 switch failed • Removed failed switch • Installed new switch • Tested and verified good back to RTU • Notified Operations ,user_92,asset_107,48.1470144,-103.6180489
1/26/2017,Tanks,Valving/Swedges,Seat/Ball/Piston,Other,Other,Trash,Produced water load line froze not allowing load to be hauled. Thawed load line,user_161,asset_160,48.16039936,-103.6185751
10/21/2019,Gas Scrubber Separator,Dump Line,,,,Freezing," Drained the Dezi took about 8 seconds, drained the scrubbers, drained all the drip pots, and all the pressure regulators, Thumbed the dumps and checked bath temp.",user_76,asset_1586,46.2356189,-100.6010498
12/9/2018,Dehy,WFS Issue,,,,,"Dispatched to well due to its deferment Got to location and found that well was loaded up pretty bad Also found that dehy was isolated and open to atmosphere. Contacted WFS, Pat Taylor made it over to get dehy going after i vented well Vented well and got plunger to surface as well as got well to unload RTP'd well ",user_56,asset_373,48.1470144,-103.6180489
8/9/2018,Tanks/Pits,Piping,Discharge Line,,,Corrosion,"found 2 holes in 1"" Dehy dump line",user_5,asset_240,48.1470144,-103.6180489
11/19/2017,Instrumentation,micro turbine,,,, G4 breaker trip,Breaker tripped. Reset and restarted turbine,user_141,asset_1489,48.1004977,-103.5858925
4/13/2017,Compressor,Engine,Other,CUMMINS,Other,Vibration,"Oil line broke from day tank, spilling oil on skid. Root cause likely to be Vibration and possible settling of compressor skid.",user_161,asset_183,48.2647913,-102.926247
12/27/2017,Compressor - Gas Lift,Compressor,Cylinder,Ariel,,Vibration,"5 mile 31-comp B. down on high discharge temp stage 2 throw, RTP.",user_71,asset_1620,48.1470144,-103.6180489
3/21/2017,Compressor,Other,,Other,Other,Other,Suction control valve would not close. Replaced ps30 and pr30 and fixed packing for the stem of the valve,user_100,asset_780,48.3619066,-103.2129855
11/6/2019,Pipeline/Piping,Valves,,,,human error,"Hot oil crew onsite warming up tanks and transferring water when arriving on location, walked through found all baths still up and warm along with line heater but pneumatic pumps barely pumping due to low psi from units being shut in due to high tanks. Found solar glycol pump that runs to condo tanks not working, troubleshot and found downstream valve shut, opened and reset pump, pump now working with good circulation. Was also asked to troubleshoot possible leak from load line on water tank side, found there was a slight leak coming from flange on outside of valve @ BD tank, looks as if it only leaks when tank is being pulled, just a small spot however entered WM for repair in case it did freeze @ flange and expand. Checked all tanks for possible frozen bottoms or ice shelfs, all water tanks clear and one condo tank clear but inside condo tank had an ice shelf, hot oiler was already working on condo tanks. Put more psi in all units to help out with heat, once hot oil is finished condo hauler will be dispatched to location to pull condo load and location can be rtp'd.",user_177,asset_1217,38.4425988,-95.5406131
12/15/2018,Instrumentation,Transmitter,Tubing Pressure,Cameron,3051,Weather,TRANSMITTER FROZE AT INLET,user_34,asset_1846,47.7434332,-103.4498
7/26/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_2012,40.5960545,-113.9323891
3/8/2019,Chemical System,Piping,Supply Line,,,Freezing,"found 1/2"" needle valve on tubing side of methanol injection had collected water and froze and split the valve causing a gas leak. after team lead notification was able to isolate and shut in valve, depressure and tag out. having piping and a valve where water is able to collect and freeze without being able to drain out is cause of issue. this issue will more than likely happen again, i recommend a redesign of methanol injection inlet on each well of the pad.",user_17,asset_1673,,
1/14/2017,Instrumentation,Transmitter,Tubing Pressure,,,Weather,Rodney Watkins diagnosed found that the tubing transmitter was frozen he thawed it out and verify that it was working correctly,user_74,asset_1114,47.80204404,-105.92974
9/5/2019,Instrumentation,Transmitter,Unit Pressure,Rosemount,3051,Water,Found Unit transmitter with blank screen. Replaced transmitter and verified operation.,user_169,asset_2267,46.2356189,-100.6010498
4/8/2017,Gas Scrubber,Other,,Other,Other,Other,,user_119,asset_2245,48.224585,-103.8291059
11/9/2019,Separator,Temp Control System,Electrical,,,,"Callout for High Bath Temp was false. Used temp gun, actual temp was 86 degrees. Will write a work order.",user_55,asset_173,,
12/15/2016,Gas Scrubber,,,,,Other,"Gas supply outside of cabinet hydrated off. Found 1"" balon valve partially stripped causing JT to the line for the ESDs",user_152,asset_151,,
2/21/2017,Gas Scrubber,Other,Other,Other,Other,Other,,user_179,asset_154,47.99172337,-103.5252604
1/22/2018,Separator,Choke Valve/Loop,,,,Freezing,Jumpered unit back up. Found freezes in poly line to choke and ESD. Thawed all lines and reinstalled. RTP'd well and hand over to optimizer.,user_141,asset_159,48.1470144,-103.6180489
12/26/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,,user_48,asset_1364,48.32721855,-103.6566518
9/16/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"OPT: looking back at graphs, plunger loaded up during last high line PSI event due to incorrect high line PSI criteria set point. Changed from 470 to 300PSI (common line PSI runs between 270-290) ",user_54,asset_2016,36.2543776,-91.268112
6/5/2017,Separator,Choke Valve/Loop,,,,Freezing,Freeze/hydrate in casing on the 20 well. Broke freeze/hydrate by opening blowdown valve to tank. Took approx 2 minutes for it to break. Put well back to production and notified optimizer. ,user_141,asset_1707,48.1470144,-103.6180489
2/2/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,"Drained scrubber pot while on location working on well 130 and 70. Small amount of fluid present in scrubber pot, we pull a small amount of fluid back from WFS using the buy back meter.",user_62,asset_676,48.1470144,-103.6180489
4/17/2018,Flare System,Flare Header,Instrumentation,,,,Low pressure flare igniter wire burnt off Root cause wind/improper protection from heat/inadequate materials ,user_111,asset_2274,48.10203822,-103.351821
10/24/2017,Separator,Choke Valve/Loop,,,,Corrosion,Choke was removed and rebuilt because it wasn't holding when closed,user_150,asset_473,48.1498261,-103.6212124
8/21/2019,Chemical System,Piping,Connections,,,Connections,Exhaust hose on glycol and methanol pump was rotten and broke. Replaced with new.,user_55,asset_496,,
1/9/2019,Separator,Fuel Supply System,Regulator,,,freeze,freezing in poly line from unit to esd's,user_64,asset_419,40.5262342,-113.8824849
10/25/2019,Dehy,WFS Issue,,,,,"Upon arrival noticed fluid coming out of the reboiler @ the dehy, immediately shut sales line on separator. Checked our surface equipment, verified dumps were working properly and scrubber was dry. Did find burner out for glycol bath and one glycol pump shut off, lit burner and started second glycol pump, burner shut off @ 60 degrees, turned up so it is now shutting off @ 90 degrees. Shut pilot and main line of for reboiler to stop the leak, checked dump in dehy and found it was not actuating. Contacted Mario Rodriguez with Williams to find who the tech was for this area, was informed Todd Canaday was the tech for the area, he did not answer so left a detailed voicemail with my number to return my call. Waited 30 minutes but did not recieve a call back, contacted Henry and was informed to move on, also sent Mario a text with the same information in case Todd couldn't make it to location. Spoke with optimizer to put a SI on well until dehy is repaired and back online.",user_177,asset_1438,40.5262342,-113.8824849
2/12/2018,Heater Treater,Burner,BMS,,,Pilot Went Out,"Issue: found the bath (B) was down on the HMI Root Cause: Human Error, there was no (INT) so someone had cleared it and worked on the pad but didn't verify the location was in full running condition when leaving Fix: relight the bath remotely and verified it light and warmed up",user_136,asset_1735,48.2595091,-102.9010563
2/26/2019,Instrument Air,Compressor (Recip),Process Gas Supply,,,,Snow removal hit line with equipment due to level of snow.,user_94,asset_600,43.56424,-91.351691
9/22/2019,Compressor - Gas Lift,Compressor,Regulator,Ariel,,Freezing,"Gas Lift was Not injecting, froze casing, and off skid recycle turned down too low, so adjusted off skid higher pressure, and sent casing to sales to break freeze, started injecting and selling good. ",user_2,asset_1286,49.5499678,-102.9290839
1/23/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,rinlet had a freeze in it. popped blow down open and broke freeze RTP'd well ,user_53,asset_1179,48.1602435,-103.6172092
10/6/2017,Compressor,Compressor (Recip),Panel,,,,"RTP compressor, down on EICS ( electronic ignition control system ) checked & drained control valve & recycle valves, drained scrubbers,warm up RTP/ monitor for .5 hr looked good",user_131,asset_1408,40.5960545,-113.9323891
2/10/2019,Tanks/Pits,Flare/Combuster,,,,fuel gas freeze,"all scc's out, frozen fuel gas",user_31,asset_1761,43.56424,-91.351691
11/12/2018,Compressor - Gas Lift,Compressor,Dump Valve,Ariel,,Vibration,"leak on a hammer union on hump lines, tightened union",user_31,asset_1623,48.2717879,-102.8687171
10/30/2017,Automation,Radio,Fuse,3M,,Unknown,Fuse was undersized. Replaced.,user_30,asset_2254,,
4/12/2019,Compressor,Compressor,Process Gas Supply,Boss,,Trash,"arrow dispatch. arrived on location, compressor was down and all wells were interlocked on high water tank.went and physically verified tank had been pulled. cleared interlocks. pressured up unit and relit burners.relit line heater. flowed out well on a pinched choke until pressures were low enough i could send well to compressor. drained all scrubbers on separator and line heater. compressor was down on low discharge psi.cleared alarm and restarted compressor. recycled compressor until water jacket temp reached 140 degrees .loaded compressor with all three wells and set rpms to auto.adjusted t12 on the 50 well. temps and flowrates look good.drained scrubbers on compressor. wells are currently unloading fluid, more than likely the 130 will liquid load in a day or so,need engineering support for this well. pad rtp",user_120,asset_1754,43.56424,-91.351691
4/9/2017,Gas Scrubber,Other,,Other,Other,Other,Had to thaw out DVC to the choke to get the choke to fully close,user_100,asset_1227,48.224585,-103.8291059
4/7/2018,Automation,Cable,Coax,SDX 20,,Electrical Short,"found the 110,100,& 70wells down, they have a shut in interlock for condo tank 2, I checked tanks they are good, I tried resetting & bringing wells on and they tripped right back out-wrote wo for auto tech , also found the line htr down no heat but pumps still running and lines all frosted up, the fuel gas vave was tripped out to the pilots, reaset relit, warmed up and restarted pumps",user_131,asset_1079,40.7126799,-114.1193569
10/18/2018,Separator,ESD Valve,Gas Supply Line,,,Calibration,Found the location down because we lost sufficient unit pressure to keep the ESD's open. Found the issue to be caused by the pumps and burners using all the fuel gas while the wells were in end cycle. Jumpered the units back on and RTP'd the wells. Paused the 110 on to keep sufficient gas to the units during end cycle,user_59,asset_2257,48.0703918,-104.8832854
8/23/2018,Tanks/Pits,Berm,Steel,,,Erosion,Gate to enter tank battery was left open. Closed gate.,user_15,asset_8,48.308508,-103.6755126
12/5/2018,Separator,Fuel Supply System,Regulator,Fisher controls,,freeze,"pilot regulator was frozen, thawed",user_31,asset_1600,43.56424,-91.351691
3/8/2019,Surface Location,Lease Road,,,,Weather,LEASE ACCESS ROAD PLOWED IN. NO ACCESS,user_34,asset_1665,48.1470144,-103.6180489
3/27/2019,Gas Scrubber Separator,Dump Line,,,,Freezing,Fuel gas regulators freeze due to high pressure drop across the big joe which requires methanol injection up stream causing methanol to accumulate in the scrubber which is not set up with an auto dump. ,user_174,asset_1011,35.9053984,-94.1287584
11/3/2017,Gas Scrubber Separator,ESD,,,,,Call out for a high unit. Shut well head in and blew down. Nothing lifted. Replaced high low trim set +body,user_172,asset_2062,,
3/8/2019,Separator,Liquid Dumps,Controller,Nalco,,Freezing,vessel and dumps froze due to unit going down in bad weather and snow preventing access,user_17,asset_1862,,
1/4/2019,Separator,Dump Line,,,,Freezing,Found several dumps froze on location. Got all dumps on pad cleared of freezes,user_55,asset_361,,
3/21/2017,Automation,Other,Other,Other,Other,Other,,user_162,asset_173,,
11/27/2017,Chemical System,Pump,Plunger,Goulds,HBT2,Air Locked,Western chemical pump stalled. No methaol causing fast plunger arrivals. ,user_50,asset_1736,47.99346831,-103.4438624
11/7/2016,Heater Treater,Mechanical Dump Valve,Body,,,Erosion,"Washed out pipe and nipples, hole in 90,nothing in this that has pipes, this is on the water dump, this could have gotten ugly, I took pictures, no place for pictures, crew is changing the pipeline now,",user_84,asset_415,48.15096482,-103.4977306
3/2/2017,Wellhead,Cyclonic Valve,Gate/Seat,Other,Other,Other,Damages unknown,user_154,asset_1343,48.16026564,-103.6172593
4/1/2019,Heat Medium,Furnace,Tube,,,,"Heat trace insufficient: Cyclonic was froze at 50% open, indicative of upstream valves freezing off in winter time during open/shut in/burp sequences. Heat trace not efficient enough to keep valve from freezing.",user_54,asset_1951,40.5262342,-113.8824849
10/15/2017,Separator,Choke Valve/Loop,,,,Trash,Found choke in manual and was 15% open. Closed choke and restarted well. Went ahead and vented well due to being loaded. ,user_141,asset_446,40.5262342,-113.8824849
5/3/2017,Wellhead,Cyclonic Valve,Actuator,,,Freezing,Fuel gas was shut off too soon and caused cyclonic valve to freeze and the cyclonic actuator tried to close against a frozen valve and pulled more current than normal and blew the fuse.,user_65,asset_1336,48.1470144,-103.6180489
11/29/2017,Compressor,Intrumentation,,,,,Comp B down on high discharge per Archrock controller. Pull graphs for data. Compressor went down shortly after 11:00 last night. Double checking with automation to ensure call out actuated. Was not in the night notes as a call out. If it did not I will add that failure report. Graphs do not indicate this condition. Still do not have discharge pressure reading into The system to be able to troubleshoot versus casing pressure for freezing or other cause. Checked heat trace. 70 degrees at D4 at wellhead. May have been a false shut down. Contact Archrock to troubleshoot. Restart and load compressor. Begin unloading process. Well still unloaded even after idling to line since last night. Fluid to surface at 737 psi. Pressures stabilize at 765 psi at .55 mmscfd injection rate. Well is pumped off to orifice valve. ,user_75,asset_1452,,
2/7/2019,Plunger System,Plunger,Lubricator Top,PCS,,Not Optimized, +WELL LOADED ** SURFACED PLUNGER-INSPECTED AND REPLACED WITH A NEW 2.375 BAR,user_34,asset_915,48.1470144,-103.6180489
4/6/2017,Gas Scrubber,Other,,Other,Other,Other,frozen choke on well 110 thawed and rtp well,user_100,asset_227,48.224585,-103.8291059
1/27/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Lost unit pressure between cycles ,user_156,asset_1581,48.19812769,-103.6354255
4/18/2019,Pipeline/Piping,Pipe/Components,,,,Human Error,"found missing 1/2"" plug where jumper was removed. replaced",user_17,asset_1525,,
4/12/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_2012,48.1470144,-103.6180489
6/22/2017,Compressor,Compressor,Suction Controller,Ariel,,Trash,"(Root causes need more options) Compressor went down on high suction due to a well kicking on hard with low psi on the compressor and controller not being able to close fast enough, high suction kill is 120psi trying to have controller valve shut at 90-100 range for a high",user_122,asset_1280,48.21649034,-103.6515798
7/10/2019,Chemical System,Pump,Packing,Texam,HBC1,Wear,"50 well RTP well and it's frozen, started methanol pump, replaced the PRV, ended cycles and pumping methanol down tubing. 130 well is frozen, tightened packing, pump already on, ended cycles to break freeze. 60 well attempted to RTP, well is frozen, tightened packing on pump and ended cycles to work on breaking freeze, has a bad lubricator cap that needs replaced. 120 well is frozen, replaced regulator and packing on pump and started methanol down tubing, ended cycles. Also has a bad lubricator cap. 70 well has a bad methanol pump, cycles don't look great. 10 well is frozen, started methanol pump. 160 well doesn't look great, has a bad methanol pump, replaced packing but the bottom check valves are bad. 7/10/2019 leak tested surface equipment leaking chokes on 70, 160, 20, 60, 130, 50 wells, leaking blowdown valves on the 20, 130 & 50 wells causing wells to freeze and load up. 50 well plunger is hitting top master valve and isn't coming in, top master is damaged and doesn't open or close, shut well in. Replaced methanol pump on 70 &160 wells. Methanol working on all wells except the 150 well and going down tubing. 60 well is still frozen",user_31,asset_386,48.2515616,-102.8696224
1/2/2019,Separator,Dump Line,,,,Freezing,Found all wells shut and and no unit pressure all baths on location down and baths cold. Units are at 18 degrees and frozen . Thawed out fuel gas supply to the burner control system and got burners going. I had to thawed out the big joe while we were getting the bath warm to prevent the gas from freezing. All dumps on location were frozen and a check valve on the 100 well on this pad had frozen and split apart . Replaced broken check valve on the water dump line. Electric glycol pumps are running with the bath at 85 degrees and the temperature at the tanks before it goes through the tank coils was 57 degrees .As the glycol bath gets fulling temped up to 125 the heat trace should be better but it seems that it should be warmer at the tanks . Im not sure why this pad went down.Thawed condo dump and broke freeze on the 100 but could not get the water dump thawed . We will let the pad heat up overnight and check dumps in the morning.Thawed out buyback meter on location to supply fuel gas .,user_10,asset_1422,48.1450656,-103.6159136
1/9/2017,Gas Scrubber,,,,,,Down on low unit pressure. ,user_50,asset_1733,47.99335943,-103.4436681
7/31/2018,Compressor - Gas Lift,Compressor,Valves,Ariel,,Freezing,"Arrow Well lost injection, Gas lift was still online. Suspected hydrates in the back side. Opened back side to AGT and broke hydrates. Put back to sales Injecting into well RTP'd well ",user_56,asset_345,48.1573536,-103.621648
3/22/2017,Instrumentation,Transmitter,3n1 MVT,Other,Other,Wiring,Lose wire,user_13,asset_725,48.14088185,-103.4139219
3/15/2018,Compressor,Compressor,Instrument Gas Supply,Ariel,,Trash,Issue: called out compressor down alarm Root Cause: found the whole location was down Fix :once i got the location back on i got gas back to the compressor i restarted and returned to service ,user_136,asset_1600,48.0614644,-104.8417043
4/22/2017,Wellhead,Other,,Other,Other,Other,"Well not flowing, losing production",user_141,asset_658,48.1470144,-103.6180489
5/20/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,well was missing plunger arrivals,user_179,asset_2178,48.1470144,-103.6180489
3/16/2019,Surface Location,Lease Road,,,,Weather,"Unable to get close to location, lease road drifted In and needs to be bladed. ",user_44,asset_1783,,
1/26/2019,Separator,Liquid Dumps,Controller,Norriseal,,Improper Adjustment,Condo dump controller was out of adjustment. Readjusted controller. ,user_68,asset_365,48.08157645,-103.6562584
10/21/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Dispatched to well, Found well with 260 on TBG and 739 on CSG Vented well for 1.5 hours and nothing, Decided to leave well Equalized. Tagged the CSG valve. Will need vented before RTP’ing ",user_56,asset_704,48.1470144,-103.6180489
12/8/2018,Tanks/Pits,Flare/Combuster,,,,fuel gas freeze,"Dumps and sales line where froze. Because fuel gas to line heater froze off. Unit was flooded and ball checked. Drain unit. Broke dumps. Lit bath. Broke sales line freeze. Broke dump freeze on heater treater. Glycol pumps are running. All burners lit and running. Broke freeze at scc pilot fuel gas. Left compressor down,its still froze. Moved heater put it on dumps on heater treater",user_120,asset_1754,48.37150018,-103.5207256
5/27/2018,Tanks/Pits,Flare/Combuster,,,,,1 scc out due to weather. Checked everything and all was good. Relit ,user_156,asset_140,48.27151926,-102.8691662
3/6/2019,Tanks/Pits,Flare/Combuster,,,,,"1 scc pilot out, probably due to wind, relit",user_31,asset_386,43.56424,-91.351691
6/28/2018,Pumping Unit,POC,Position Sensor,Lufkin,POC,Communication,RTP'd pumping unit in automatic.,user_161,asset_1083,48.267245,-102.9231841
10/10/2019,Chemical System,Pump,Packing,Goulds,HBT2,Wear,The methanol pump packing was leaking. The pump was replaced with a rebuilt one.,user_68,asset_530,41.474544,-90.6778637
10/20/2019,Heat Medium,Pump,Diaphragm Gears,Goulds,HBC1,Weather,"only one glycol pump on location, scrubber full of liquids and dezy, dump lines froze , thawing on dump line to drain liquids ",user_144,asset_1957,40.5262342,-113.8824849
2/5/2019,Flare System,Flare Header,Regulator,,,,"Issue: found flare out while performing my walk around Root Cause: Gusty/Wind, looks like it got blown out again Fix: without a wind break and the flare being 20' in the air its going to keep getting blown out ",user_170,asset_1915,48.1470144,-103.6180489
3/15/2017,Gas Scrubber,Other,Other,Other,Other,Other,Please replace as soon as possible ,user_175,asset_1211,47.94936709,-103.6881975
2/21/2018,Automation,Cable,Coax,SDX 20,,Loose Connection,RD 15-2 high tank callout false alarm.,user_71,asset_26,48.1470144,-103.6180489
5/3/2017,Tanks/Pits,Shell,Body,,Steel,Corrosion,Middle tank #761570w needs repaired so we only have to storage tanks and we keep hi tanking and I'm not getting the call out alarms ,user_131,asset_1624,48.01299597,-103.7321195
11/28/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_101,40.5262342,-113.8824849
9/28/2018,Gas Scrubber Separator,ESD,,,,,"unit went down on low unit pressure reason is unknown dumps seen fine, maybe SCCs used all of units fuelgas in off cycle,",user_37,asset_1793,48.16031,-103.6173485
11/20/2017,Separator,ESD Valve,Gas Supply Line,,,Freezing,unit had pressure on it the interlocks on the HMI did not give a reason for shutting in . Thawed on the big joe and cleared interlock on HMI and rtp well and restarted bath and scc location. Must have been low fuel gas supply pressure because the big joe had a partial freeze.,user_100,asset_110,48.1470144,-103.6180489
5/28/2018,Compressor,Compressor,Process Gas Supply,Ariel,,Freezing,Compressor down on low discharge pressure. Put off skid recycle back into service. ,user_156,asset_1174,48.21116855,-103.7730114
5/13/2018,Gas Scrubber Separator,ESD,,,,,"Creston 3-150 shut in on low inlet pressure, vented for an hour and well didn’t unload. Left equalized. ",user_71,asset_39,48.1470144,-103.6180489
2/1/2018,Heat Medium,Pump,Diaphragm Gears,Texam,HBC1,Wear,"Replaced 1.5"" graco 1590 glycol pump with 1"" sandpiper glycol pump.",user_161,asset_1525,48.2645245,-102.9260677
10/11/2017,Compressor,Intrumentation,,,,,"When trying to start compressor , it would not fire when turning over, had to pull fuse and wait a few minutes, then it would start, contacted Archrock about issues ",user_122,asset_97,48.21775367,-103.2680468
4/24/2018,Flare System,Flare Header,Regulator,,,,pad check all looks ok. submitting task request to build up sections of berm. blew out scc sump and cleaned out pilot tip on scc a relight scc when comm error clears.,user_11,asset_1691,40.7126799,-114.1193569
1/14/2019,Pipeline/Piping,Pipe/Components,,,,Erosion Corrosion (Internal),Piping developed erosion holes by the weld,user_21,asset_101,40.5262342,-113.8824849
6/28/2019,Separator,Controller,,,,,well down /found that the dump controller box for the condo dump was missing multiple parts and was not functioning / dump valve was closed and flagged . Got parts for the controller and installed new controller parts. Rtp'd well/ waited for plunger arrivals so that I could adjust dumps properly . This well was flooding the unit when it was getting plunger arrivals / adjusted the choke setting to regulate the fluid entering the unit so the dumps could keep up with the fluid production. I also found the gasket for the water dump controller was leaking / replaced gasket and rtp'd. Plunger making arrivals.Found three scc's out re-lit and adjusted pilot pressure.,user_10,asset_1650,40.5262342,-113.8824849
6/11/2018,Compressor,Compressor (Intergral),Block,,,,"Compressor down on high discharge psi, restarted compressor and back in operation ",user_58,asset_1421,48.40626237,-103.5808912
8/12/2019,Wellhead,Wellhead,Integrity Failure,,,,"Found well tagged out for the lubricator leaking and supposed hydrate in the WH wouldn't allow it to be checked. Top master valve was not seized, I was able to shut it and verify isolation. While bleeding off the pressure i noticed that the top puck on the bone x lubricator was loose and i was able to move it by hand. Bleed pressure off, Contacted TL and let him know what i had found. Discussed that i would send my SBA over to the OSM Once that was approved i took lubricator off and took that top puck off for inspection didn't find anything wrong. O-ring was just fine as well Installed puck and then re-installed lubricator and put pressure to it and it held. Contacted OSM for approval to removed operator tags RTP'd well",user_56,asset_204,40.5262342,-113.8824849
9/15/2017,Flare System,Flare Header,Process Indicator,,,,Probably due to weather ,user_156,asset_1903,48.17940214,-103.6564598
1/19/2018,Gas Scrubber Separator,ESD,,,,,Everything looked fine when I arrived onsite I cleared alarm brought well online and started plunger cycles.,user_51,asset_1949,48.1470144,-103.6180489
3/28/2019,Tanks/Pits,Berm,Dirt,,,Wildlife/Livestock,Repaired flags on the reserve pit,user_21,asset_298,46.2356189,-100.6010498
3/10/2019,Separator,Temp Control System,Pilot,,,,"Found 80 well bath heater out, but gas flowing. Verified against known good gauge that pilot pressure is set to 8 and burner is set to 10. Burner must have blown out, fuel gas is dry and 02 adjustment is acceptable.",user_54,asset_341,40.5262342,-113.8824849
7/10/2017,Automation,Cable,Data Cable,3M,,Electrical Short,"False high tank call out, all tank levels and live reads on location are good. Nothing on location shut in due to the live reads",user_24,asset_1553,48.1470144,-103.6180489
10/9/2017,Separator,ESD Valve,Gate/Seat,,,Trash,"High low trim set not holding, washed out , getting new trim set and replacing ",user_122,asset_398,48.3531191,-103.7751287
1/10/2018,Compressor,Compressor (Intergral),Process Gas Supply,,,,"Champ 263 B-comp down on low discharge, RTP. ",user_71,asset_2081,48.1470144,-103.6180489
4/3/2017,Compressor,Compressor,Instrument Gas Supply,Other,Other,Liquid Carryover,drained liquid and adjusted sgr12,user_11,asset_780,,
12/27/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_1633,48.1005163,-103.5858106
6/15/2018,Separator,Liquid Dumps,Seat/Ball/Piston,Norriseal,,Erosion,"Dump trim leaking, tried to repack, but still not holding. Have to order parts. Replaced and repacked dump trim. ",user_141,asset_2217,48.1001903,-103.5869983
4/4/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Drained desi while on site. Desi took 45 seconds to drain all fluid. Unknown when the last time it was drained. Buy back meter temp, 55 degrees, desi outlet temp 50 degrees, heat trace pumping around desi 90 degrees and ambient temps 54 degrees. Opened all condo tanks to operate battery as facility to maximize condo capacity onsite and align with predictive dispatch tools. ",user_62,asset_971,48.1470144,-103.6180489
3/21/2019,Surface Location,Lease Road,,,,Weather,3/21/19 Plowed location access road & turnaround. Well is ready for ops to attempt to RTP.,user_42,asset_171,46.2356189,-100.6010498
3/10/2017,Automation,Other,,Other,Other,Other,Broken pvc and damaged metallic flex hose.,user_162,asset_252,,
5/10/2018,Automation,Plunger Arrival Switch,,EDI,,,Adjusted sensitivity on cyclops plunger arrival sensor.,user_65,asset_1286,48.1470144,-103.6180489
4/8/2017,Gas Scrubber,Pnumatic Dump Valve,Seat/Ball/Piston,Other,Other,Other,,user_179,asset_2276,47.97017819,-103.5234172
7/15/2018,Flare System,Flare Header,BMS,,,,Issue: Found SCC (B) down on the HMI Root Cause: looks like the rain storm of a couple days ago flooded out the pilot and knocked it out Fix: relight and returned to service Long Term Fix: may look into putting the pilot horizontally so the rain cant flood out the pilot tip and may loose less SCC;s during rain storms ,user_170,asset_1647,48.2594901,-102.9011771
8/15/2018,Separator,Liquid Dumps,Controller,Norriseal,,Improper Adjustment,WATER AND CONDO LEVELS WERE VERY FAR OUT OF ADJUSTMENT.. ADJUSTED NOW,user_34,asset_1090,46.0240507,-101.4208674
10/21/2017,Separator,Liquid Dumps,Seat/Ball/Piston,Fisher,,Erosion,,user_156,asset_2080,48.2548106,-103.6037531
11/18/2017,Gas Scrubber Separator,Pneumatic Dump Valve,Controller,Norriseal,,Out Of Adjustment,Issue: well shut in on hi pressure in the LP Root Cause: We are flowing through a hi pressure green complete unit so nothing but gas goes to our hi pressure unit but the dump was out of adjustment and decided to dump and hung open over pressuring the LP Fix: shut the dump and backed off the dump controller and told the flow testers to watch the sight glass and if gets a level to call me,user_136,asset_580,48.0614644,-104.8417043
1/3/2018,Heat Medium,Pump,Check Valve,Goulds,HBC1,Wear,Graco glycol pumps failed,user_111,asset_1405,48.04472109,-103.3543658
11/11/2018,Heat Medium,Pump,Process Indicator,Texam,HBC1,Wear,"3 glycol pumps not pumping, one had a closed valve, bleed pumps off and restarted",user_31,asset_1686,43.252261,-115.0567324
10/30/2017,Fuel Gas/Start Gas,Regulator,,,,,well went down on low fuelgas readjusted regulators for lower operating pressures and changed fuelgas feed configure,user_71,asset_1838,48.1470144,-103.6180489
10/21/2018,Heat Medium,Pump,Process Indicator,Texam,HBC1,Power Supply,"pumps designed for about 30 psi, gauges pegged and pumps sounding like machine guns, lowered supply to about 20 psi",user_31,asset_333,43.252261,-115.0567324
1/22/2018,Fuel Gas/Start Gas,Regulator,,,,,Froze dvc,user_126,asset_1142,,
11/7/2019,SWD System,Particle Filter,Element,,,,Changed filters,user_31,asset_523,48.2714926,-102.8684019
1/3/2018,Dehy,WFS Issue,,,,,Dehy froze,user_86,asset_989,,
5/15/2019,Chemical System,Pump,Diaphragm Gears,Texsteam,HBC1,Wear,"tested the pumps before replacing, the diphram was leaking on both, still one good pump. also installed new PRV's on two of the pumps. ",user_77,asset_2076,46.2356189,-100.6010498
4/8/2019,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,froze,user_56,asset_1744,40.5262342,-113.8824849
4/4/2018,Tanks/Pits,Valving/Swedges,Body,,,Corrosion,Opened all condo tanks to operate battery as facility to maximize condo capacity onsite and align with predictive dispatch tools.,user_62,asset_469,48.1470144,-103.6180489
4/4/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,Added methanol injection to flow line,user_157,asset_602,48.2646688,-102.8941984
9/4/2018,Compressor - Gas Lift,Engine,Vibration Switch,Ajax,,Vibration,"Compressor went back down on cooler vibration, no callout. Reset and started. Didn't see any issues",user_31,asset_2138,48.1470144,-103.6180489
3/9/2018,Separator,Temp Control System,Fuel Gas Supply,,,,Burners out. Maybe from wind,user_156,asset_1644,48.1651752,-103.4490553
3/9/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Lost plunger arrivals, had to vent in.",user_95,asset_1527,48.12549556,-103.6530438
8/26/2017,Compressor,Compressor (Recip),Lubricator,,,,New compressor and compression company. Still working to get compressor dialed in correctly. Low oil level in the compressor,user_163,asset_628,48.38708651,-103.8414946
3/7/2018,Instrumentation,Meter,Orifice Plate,Bristol,2,Freeze,heat traced meter,user_173,asset_1497,48.1602856,-103.6184641
6/6/2018,Compressor,Compressor (Recip),Suction Controller,,,,Compressor B down on Low Suction Pressure. Seems that the suction valve is not reacting fast enough or possible freeze in suction line. ,user_41,asset_521,48.22041421,-103.5957891
11/29/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_2012,40.5262342,-113.8824849
1/9/2019,Gas Scrubber Separator,Dump Line,,,,Freezing,"found unit at 700psi thawed out wellhead and shut in blew down unit from needle valves because its completely froze and flooded, unit transmitter showing 1100psi false",user_37,asset_1883,43.56424,-91.351691
12/10/2016,,,,,,,Well badly loaded from cycle malfunction in data base. Contacted optimizer to fix criteria. Lost production ,user_163,asset_799,47.99681537,-103.4263016
12/27/2017,Instrumentation,micro turbine,,,, G4 breaker trip,"#1 turbine had an alarm for HETemp, High Exhaust Temp. Was able to clear alarm by resetting turbine. It did not take turbine down. Will write a work order to have it looked at. Also, we did order some new batteries for turbine. Would not light until we had another turbine running.",user_141,asset_1489,47.942078,-103.6975344
11/6/2017,Compressor,Compressor,Process Gas Supply,Compressco,,Trash,Compressor down on low suction. To many wells in off time at the same time. The two free flowing wells 70&60 are starting to load up and need a vent/psi build. Drained scrubbers and cleared alarm restarted compressor ,user_172,asset_785,,
2/23/2017,Gas Scrubber,Other,,Other,Other,Other,"No damage, thawed and opened esd, rtp",user_88,asset_993,48.26317197,-102.8996031
2/28/2018,Separator,Liquid Level Control,,,,,Found water dump controller door open. Closed controller door.,user_62,asset_635,48.1507625,-103.6206926
3/26/2019,Heat Medium,Pump,Instrumentation,Texam,HBC1,Air Locked,Found Glycol pump C with Damaged pump; Replaced,user_139,asset_365,,
9/11/2017,Automation,Cable,Coax,SDX 20,,Electrical Short,False reading ,user_156,asset_2227,48.18067317,-103.651116
12/5/2017,Plunger System,Plunger,MSO,IPS,,Wiring Shorts,Surfaced plunger but didn't show arrival on HMI need automation to look at it,user_0,asset_342,48.252204,-102.7573696
12/1/2017,Tanks/Pits,Flare/Combuster,,,,,3 out of 4 scc out drained pilot and relit three scc,user_172,asset_1800,,
1/7/2018,Gas Scrubber Separator,ESD,,,,,Champ 533 pad ESD on high scrubber level at 2:00. scrubber drained and RTP site. Was down for about 30 min. beaned back up and choke is at 24/64th ,user_71,asset_1780,48.1470144,-103.6180489
10/31/2017,Heater Treater,Burner,Fire Tube,,,Loss Of Fuel Gas,lit line heater and checked burners onsite.,user_71,asset_876,48.1470144,-103.6180489
10/31/2019,Automation,Cable,Coax,SDX 20,,Electrical Short,"Started skimming oil to North oil tank, added 2 quarts oil to PD pump. Changed filters. 10/31/2019 changed filters and added a quart of oil. Hand scanner isn't working, tried to power cycle and it didn't help",user_31,asset_569,48.2933408,-102.8507808
11/30/2018,Heat Medium,Pump,Process Indicator,Sunpumper,HBC1,Weather,"glycol pump was on when glycol temp was 30 degrees, got burner going again",user_31,asset_793,43.252261,-115.0567324
1/27/2019,Flare System,Flare Header,BMS,,,,"Issue: found flare out while on location Root Cause: Human Error, when the foam got to surface and re inactivated it foamed everything out including the fuel gas. with the wind and temps it froze at the flare Fix: I was able to thaw out drain the line drop the boom relight and returned to service ",user_170,asset_705,49.5499678,-102.9290839
2/10/2019,Instrumentation,Controller,,,,,Fisher DVC6000 : I/P and relay choked with liquid because it is being operated with wet fuel gas.,user_12,asset_1347,40.5262342,-113.8824849
9/15/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ajax,,Freezing,#10 well froze in casing taking down comp on high discharge.,user_37,asset_2055,48.1498583,-103.6212065
3/8/2019,Tanks/Pits,Flare/Combuster,,,,,"Location was shut in to remove unneeded equipment. Once work was completed, I lit all 3 SCC's.",user_15,asset_2001,39.2506642,-92.4357879
12/2/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Vented plunger to surface and put back on plunger cycles,user_51,asset_1355,40.5262342,-113.8824849
9/12/2019,Tanks/Pits,Piping,Discharge Line,,,Debris,Verified lines were unplug and returned to service,user_21,asset_969,40.5262342,-113.8824849
3/12/2018,Flare System,Flare Knockout,Instrumentation,,,,Abutec scc out due to liquids dropping out of fuel gas lines to pilots. Causing pilot to plug and burner management system not seeing a flame. Might look at additional knockout pot or filters in fuel gas lines. ,user_58,asset_1421,48.40601326,-103.5804475
10/28/2017,Flare System,Flare Header,Process Indicator,,,,,user_48,asset_701,,
3/7/2018,Separator,Temp Control System,Thermostat,,,,"Lit and warmed up glycol bath. T-12 for bath was set for 115. The well has 2000 PSI on it, turned up T-12 to 140 to help get heat into the system while bringing well online. Root cause- There is no failure on this, i needed more heat due to high pressures so I adjusted bath temp up.",user_62,asset_2258,48.1470144,-103.6180489
11/21/2017,Plunger System,Plunger,Plunger,PCS,,Corrosion,Plunger worn,user_126,asset_500,,
7/23/2017,Compressor,Compressor,Scrubber Level,Ajax,,Liquid Carryover,Once I was able to get the unit to dump to the LP then the unit stopped caring fluid over to the compressor ,user_136,asset_1574,48.0614644,-104.8417043
12/8/2016,Chemical System,Piping,Discharge Line,,,Freezing,"Sales line and cyclonic valve froze, no heat trace on sales line, I will put in a task request to get it heat traced",user_84,asset_1169,48.06015884,-103.512458
10/3/2018,Wellhead,Tubing,,,,hydrate,Issue: Flexing to turn well on Root Cause: well was ready to come back on and get plunger equipment installed. When i opened up the well i found its froze tubing and casing Fix: left well equalizing and will get some methanol ordered ,user_170,asset_2243,43.252261,-115.0567324
10/8/2018,Separator,ESD Valve,Gate/Seat,,,Fouling,"found unit at 1030 psi, shut in wellhead and blew down seperator. hiilo wasn holding",user_37,asset_1338,43.252261,-115.0567324
12/11/2017,Instrumentation,Communication Card,,,,,Issue: compressor callout alarm Root Cause: COMMS are in and out making a ghost callout for a compressor that is already down Fix: left as is,user_136,asset_2270,48.1470144,-103.6180489
11/3/2019,Gas Scrubber Separator,Dump Line,,,,Freezing,"Drained the Dezi took about 8 seconds, drained the scrubbers, drained the drip pots, Thumbed the dumps and checked bath temp.",user_76,asset_996,46.0240507,-101.4208674
12/7/2016,Gas Scrubber,Shell,,,,,"Scc out from fluid carryover, thawed and blew out fluid relit",user_87,asset_1586,47.93781252,-103.5044555
3/10/2018,Heater Treater,Burner,BMS,,,Corrosion,"Issue: found Bath (B) at 100deg on the HMI and wells flowing over 90deg Root Cause: the warming up of ambient temp is causing the bath temp to creep up as well Fix: turned the T-12 down Along with the warmer weather i was able to get all the ESD filters drained and blew all of them dry, Choke filters drained and blew all of them dry, Desi drained, Scrubbers on all three separator, Comp drained all three scrubbers as well ",user_136,asset_1713,48.1470144,-103.6180489
2/8/2019,Fuel Gas/Start Gas,Coalescer/Filter,Instrumentation,,,,"FOUND UPON ARRIVAL+FOUND UPON ARRIVAL+ +ALL QUAD PACK ESD'S CLOSED +NO PRESSURE TO THE FUEL GAS SCRUBBER **RELYING ONLY ON BUY BACK GAS-BUY BACK LINE FROZEN **FUEL GAS COMING FROM QUAD PACK HAD BEEN SHUT OFF. *****OPENED UP QUADPACK FUEL GAS TO BIG JOE **** OPENED ESD'S TO WELLS +BURNER OUT DUE TO FUEL GAS ISSUES ** RELIGHTED BURNER **VERIFIED DUMP LINES OPEN AND LIQUID DUMPS FUNCTIONING PROPERLY ***RTP'D AND STARTED CYCLES ON WELLS 60, 80, 150 *** WELL 140 BADLY LOADED, UNABLE TO VENT. SIPB FOR ANOTHER ATTEMPT TO VENT NOTIFIED OPTIMIZER **** OPENED ESD'S TO WELLS +BURNER OUT DUE TO FUEL GAS ISSUES ** RELIGHTED BURNER ",user_34,asset_660,48.1470144,-103.6180489
11/13/2017,Heat Medium,Pump,Packing,Goulds,HBC1,Wear,Graco 1050 glycol pump was venting glycol when stroking - replaced pump.,user_161,asset_725,40.5481548,-114.0112915
4/3/2018,Tanks/Pits,Flare/Combuster,,,,,Wind yesterday blew out SCC.,user_95,asset_1191,48.08062958,-103.6015508
1/2/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Desi can needed thawed and and drained. Pull graphs to troubleshoot remotely before dispatching to location. Compressor discharge at 1000 psi. Compressor discharge recycle set at 998 psi with kill at 1100 psi. Csg pressures well below this value on both the 120 and 150 wells. Suspected freeze between compressor discharge and injection point. Check injection valve position and meter reading. Valves indicate 100% open with no injection rate. Suspect a fuel supply line at injection valve to be froze. Dispatch to location. Confirm freeze in fuel supply line. 120 and 150 are farthest downstream on fuel gas supply line from take off point at compressor. 120 is the farthest. Break freeze and resume injecting. Discharge recycle closes as set and wells begin accepting injection rate. Thaw and drain desi. Approximately 1-2’ of fluid in desi. Adjust separator A bath up at T12. Current bath temperature 74 degrees. Ambient air temp -7. Tanks temperatures good. Wellhead temperatures 60 degrees. Checked with laser. ,user_75,asset_1452,,
9/1/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash,"Inlet valve not opening/ very far out of calibration. Found pressure sending unit/ bourdon tube full of liquid, sand and mud. Dumps are actually set correctly but the unit was flooded",user_163,asset_1815,48.3619066,-103.2129855
3/21/2019,Surface Location,Lease Road,,,,Weather,3/21/19 Plowed location access road & turnaround. Well is ready for ops to attempt to RTP.,user_42,asset_1063,46.2356189,-100.6010498
11/6/2019,Separator,Temp Control System,Fuel Gas Supply,,,,"Well was showing a deferral PTL asked me to go to site and troubleshoot equipment. Arrived onsite and found well down and interlocked on high scrubber liquid level for the ko pot at the flare. Drained ko pot, took 11 five gallon buckets worth of oil out of line. Attempted to pressure up high pressure separator. Found freeze in flowline/ hi lo. Back blew freeze to agt. Thawed out hi/lo with thaw tube. Hp separator fuel gas scrubber was ball checked. Drained pot and got ball to drop. Dump to LP was frozen, thawed out line. Line is now clear to LP but the displacer inside unit is frozen in vessel so it continually trys to dump. Lit bath on hp unit. Lp scrubber pot was also ball checked. Both dumps are free to tanks but displacers are frozen. Held dump open on hp to sweep out flare line. Well then esd again on high liquid level. Took another 8 Buckets of fluid out of line and dumped them in t huh e top of the tank. Got everything pressured back up and relit both burners. Lit both abutecs. Let baths get up to temp and tried selling some gas to increase temperature inside vessel. Well was selling for around five minutes and I was manually dumping fluids. Well then esd on high liquid level again. Took six buckets worth out of line and didn't see any progress in sight glass. Ran out of time in the day. Pulled the heater from the monument 11-150H over to location and placed it on both units. Entered new voltage in the controller for the solar glycol pump. Will need to return to location tomorrow and continue draining flare ko pot",user_120,asset_2034,,
8/6/2019,Sales Valve (PV),Sales Valve,Body,Valvcon,,Washed Out,"The salesline cyclonic valve was leaking out the stem and the 2"" ball valve was seized open on the upstream side of the cyclonic. Both valves were replaced.",user_68,asset_1430,46.2356189,-100.6010498
2/18/2018,Gas Scrubber Separator,ESD,,,,,Siberia 30 pad down on valve fault scrubbers were ball checked. Drained scrubbers and jumped pad on RTP and started cycles RTP comp.,user_71,asset_2241,48.1470144,-103.6180489
4/11/2018,Dehy,WFS Issue,,,,,Well will flow for a few minutes and then stops. Suspect a lateral freeze. Contacted Robin with Anadarko. He advised will have someone here in the morning.,user_141,asset_554,48.1470144,-103.6180489
1/24/2019,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Arrived on location and did walk down. Found scrubber pot was full of fluids and caused the check ball on top of scrubber to lift and shut off gas to all end devices. Location already has cold fingers, not sure why there was so much fluid in scrubber. Got scrubber drained and got burner lit up. ",user_15,asset_919,40.5262342,-113.8824849
12/19/2018,Wellhead,ESD Valve,Actuator,,,Fouling, 6. Champlin 263 B-80 - ESD actuator bad • Found actuator blowing gas out of vent • Removed bad actuator • Had a hell of time installing new actuator and getting it to align with the mounting bolt holes • Installed new actuator • Tested and verified good • Notified operations ,user_38,asset_1364,48.16027286,-103.6180987
11/1/2017,Compressor,Compressor (Intergral),Process Gas Supply,,,,Compressor down on low suction. ,user_50,asset_876,48.39012302,-103.5820325
3/18/2018,Wellhead,Tubing,,,,,Issue: found well down on the HMI Root Cause: tag on inlet well froze and is equalized Fix: unequalized and turned well back on found is still froze so i re-equalized ,user_136,asset_2167,48.1470144,-103.6180489
6/20/2018,Separator,Fuel Supply System, Big Joe Regulator,Fisher controls,,wear,Big Joe regulator was over pressuring the scrubber pot and the PSV was releasing. The nipple and button were replaced. ,user_41,asset_521,48.27333071,-102.8698638
2/12/2019,Separator,Dump Line,,,,Freezing,Was able to get on turn around at location. Got stuck twice trying to make it in to location. Please blow access round and around separators so operator can get close enough to thaw out dump lines.burners are still up and running. Drained scrubbers.Please code appropriately when location has been plowed.,user_120,asset_1780,48.38459847,-103.533378
2/19/2018,Fuel Gas/Start Gas,Regulator,,,,,"Drained Kim Ray drip pot at DVC for choke. Fluid was present, drip pot was froze. Used thaw tube to thaw drain and empty liquids. Ambient temperature is -2 at time of this surface failure. The choke DVC uses gas to open and close, causing liquids to drop out at these ambient temps. There is insulation on the drip pot, but there is no source of heat to prevent freezes. The insulation is holding in the cold temps.",user_62,asset_1452,48.1470144,-103.6180489
4/3/2018,Instrumentation,Controller,,,,,"Compressor down on low discharge. Compressor recycled for too long while all the wells were on off cycles causing it to go down on low discharge. Kelvin failure. Issue has been brought up Restarted compressor, let it warm up once it was up to temp i loaded compressor. Compressor immediately went down on high suction. Suction controller is reacting slow, found gas froze from sitting down for 6 hours! Temp was also 10 degree Fahrenheit Broke out the thaw tube and thawed the kimray fuel pot. Finally was able to break freeze and blew line out. Restarted compressor again and loaded. RTP'd compressor and well ",user_53,asset_1996,48.2614528,-102.8936593
2/16/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Drained desi while on location bringing pad back on line after COMM ERROR was repaired.,user_62,asset_2222,48.1470144,-103.6180489
7/1/2018,Compressor,Compressor (Intergral),Dump Valve,,,,Low suction ,user_86,asset_1346,,
4/27/2018,Flare System,Flare Header,Regulator,,,,"i bex pulled the sump, had ro relight the scc",user_122,asset_1882,48.0614644,-104.8417043
7/7/2019,Wellhead,ESD Valve,Actuator,,,Corrosion,blowing from lower vent,user_12,asset_1670,38.4425988,-95.5406131
7/27/2017,Flare System,Flare Knockout,Shell,,,,SCC extinguished by Rain last night- Relit,user_138,asset_1960,48.07728374,-103.4416463
12/12/2017,Separator,Choke Valve/Loop,,,,Trash,Stem and seat show signs of wear,user_105,asset_1785,48.32741813,-103.6573289
5/17/2019,Plunger System,Plunger,Plunger,PCS,,Corrosion,replaced bypass plunger 1.85,user_10,asset_627,46.2356189,-100.6010498
7/14/2018,Gas Scrubber Separator,Mechanical Dump Valve,Mechanical Linkage,Kimray,,Out Of Adjustment,Issue: called out well shut in alarm Root Cause: found water dump stuck open Fix: was able to move and get deactivated working again and returned the well to service ,user_170,asset_660,48.1470144,-103.6180489
3/31/2018,Sales Valve (PV),Sales Valve,Body,Automax,,Freezing,Went to location to troubleshoot production equipment. Found fuel gas scrubber ball checked and froze. Water dump line froze. And a freeze in sales line cyclonic. Isolated wellhead. Shut choke on unit. Isolated fuel gas and blew down got ball to drop after thawing on it. Got fuel gas running. Lit burner got pumps stroking. Opened well head masters.Cracked choke to keep burner and pump. Bled pressure off of dump line thawed on line. Pressured back up and got freeze to break. Isolated sales line and back blew freeze. Got bath up to temp. Had optimizer force open down stream cyclonic to flow off some pressure on tubing. Currently has 1340. He’s gonna put cycles back in when pressures reach normal. Rtp well,user_172,asset_602,,
10/26/2017,Heat Medium,Pump,Check Valve,Texsteam,HBC1,Set Screw,"Set screw lock down was not set for the gas supply going to glycol pump for tanks on separator B, so it backed out and pump was not stroking. Adjusted regulator and set set screw lock down. ",user_62,asset_635,48.1470144,-103.6180489
10/22/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Corrosion,Packing Leak,user_5,asset_468,43.252261,-115.0567324
1/21/2018,Chemical System,Pump,Plunger,Texam,HBC1,Wear,East glycol pump was stalled out. Bleed off and restarted ,user_156,asset_2239,48.22171022,-103.7497411
11/6/2019,Separator,Choke Valve/Loop,,,,Freezing,"Well was showing a deferral PTL asked me to go to site and troubleshoot equipment. Arrived onsite and found well down and interlocked on high scrubber liquid level for the ko pot at the flare. Drained ko pot, took 11 five gallon buckets worth of oil out of line. Attempted to pressure up high pressure separator. Found freeze in flowline/ hi lo. Back blew freeze to agt. Thawed out hi/lo with thaw tube. Hp separator fuel gas scrubber was ball checked. Drained pot and got ball to drop. Dump to LP was frozen, thawed out line. Line is now clear to LP but the displacer inside unit is frozen in vessel so it continually trys to dump. Lit bath on hp unit. Lp scrubber pot was also ball checked. Both dumps are free to tanks but displacers are frozen. Held dump open on hp to sweep out flare line. Well then esd again on high liquid level. Took another 8 Buckets of fluid out of line and dumped them in t huh e top of the tank. Got everything pressured back up and relit both burners. Lit both abutecs. Let baths get up to temp and tried selling some gas to increase temperature inside vessel. Well was selling for around five minutes and I was manually dumping fluids. Well then esd on high liquid level again. Took six buckets worth out of line and didn't see any progress in sight glass. Ran out of time in the day. Pulled the heater from the monument 11-150H over to location and placed it on both units. Entered new voltage in the controller for the solar glycol pump. Will need to return to location tomorrow and continue draining flare ko pot",user_120,asset_2034,,
9/26/2017,Wellhead,Manual Valve,Ball,,,Trash,Old Valve internals leaking,user_119,asset_891,48.1602792,-103.6173592
12/12/2018,Fuel Gas/Start Gas,Regulator,,,,,"Pad down, continues to lose pressure. and shut in. Jumped pad back on. I have the 160 sales line valve closed and choke open. Using this to keep the pad up. Line pressure drops to 70 - 80 psi. Not enough to keep the pad up. I also have the 40 and 60 sales line valves closed and chokes open. These are the wells that had rod pumps that are out of service. I have the valves on top of separators closed except these 3 wells. Will monitor and see if this will keep pad up. I vented the 70 well. Got busy and forgot to listen for the plunger. I don't think it came in but will also monitor this well.",user_55,asset_317,,
1/29/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Fuel gas froze to line heater. This is almost an every day thing. Thawed on regulator to motor valve. Pilot line was clear main was not running. Got freeze broke. ,user_172,asset_1213,,
5/21/2018,Plunger System,Plunger,Catcher,Ferguson,,Not Optimized,Plunger catch was very stiff when setting it. Greased catch and ran it in and out several times getting it working much smoother. ,user_62,asset_425,40.7126799,-114.1193569
11/27/2017,Compressor,Engine (Gas),,,,,Root cause not listed. Engine vibration fault. Dispatch to location to troubleshoot gas lift compressor down time. Check graphs to check well condition and pressures. Check panel for down code. Comp A for the 31-90 well down on engine vibration switch alarm. Comp B for the 31-120 well down on low suction pressure. Comp A and B went down on previous days for same codes. Contact Archrock to troubleshoot engine vibration. They troubleshooted the unit and adjusted the sensitivity of the sensor. A new sensor was installed yesterday. Root cause of downtime new install set points. Comp B low suction troubleshoot to set points on unit. Current csg injection pressure on the 31-120 only 620 psi. With injection rates and pressures the low pressure kills are close to being met. Suction controller is adjusted close to full open and struggling to maintain 70 psi with current rates and motor RPM. Contact PE to update on new design and resizing project already currently in progress. Plan forward to continue to optimize rate on the 31-90 and 31-120 and make run adjustements as needed to ensure compressor operability until project is engineered approved and completed. Target completion date to be discussed tomorrow 11/28/2017. ,user_75,asset_1452,,
1/20/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_1633,48.1470144,-103.6180489
7/25/2019,Separator,Dump Line,,,,Freezing,The dump check valves on both water and condo lines had froze and broke. They were replaced.,user_68,asset_1697,48.1470144,-103.6180489
7/27/2017,Flare System,Flare Header,Regulator,,,,Relit SCC. Pilot was extinguished after evening rain fall. ,user_41,asset_1686,48.17817884,-103.6170576
2/16/2018,Separator,Choke Valve/Loop,,,,Freezing,Glycol pump stalled causing freeze in flow line,user_126,asset_1486,,
5/30/2018,Compressor,Compressor,Process Gas Supply,Ariel,,Vibration,"down on low inter stage, no issue found, checked all equipment , ",user_122,asset_1383,,
2/17/2019,Flare System,Flare Header,Regulator,,,,"Regulator looks to have frozen due to liquids in fuel gas, breaking internal diaphragm and causing the regulator to fail. ENG engaged to determine installing cold fingers and re-install water dump on line heater/fuel gas dryer to ensure fuel gas is properly dried and equipment is able to auto dump any liquids that may build up.",user_54,asset_793,46.2356189,-100.6010498
1/10/2019,Heat Medium,Pump,Instrumentation,Texam,HBC1,Freezing, 5. Tierney 5-150 - glycol pump issue • Found solar controller in LVD • Tested batteries and all were between weak and bad • I removed all 4 bad batteries and installed 4 new batteries • I verified batteries charged up over 28 volts • I started pump and left it running at 1.4 amps • I will check back tomorrow and make sure the batteries lasted over the night ,user_38,asset_764,46.2355104,-100.6413984
1/21/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,kicked well on and paused flowing achived plunger arrival and cycles resumed. please check cycles,user_11,asset_471,48.1470144,-103.6180489
10/7/2019,Flare System,Flare Knockout,Instrumentation,,,,"Changed ESD valve on SCC A, re-lit pilot and verified operations with optimizer",user_44,asset_1442,46.2356189,-100.6010498
3/5/2018,Tanks/Pits,Flare/Combuster,,,,,"Lit SCC C. While on location, noticed SCC's were not lit. Pilot light on all 4 SCC's were out. Shut down all SCC's to let them purge, lit pilots and put them back in service. Cannot Identify root cause as to why they were out, i did not have to thaw or repair any thing to get them on.",user_62,asset_6,40.5960545,-113.9323891
4/20/2018,Heater Treater,Burner,BMS,,,Loss Of Fuel Gas,Issue: bath (A) down Root Cause: when the pad ran out of fuel gas the burner ESD's shut in on valve fault Fix: once the pad was pressured back on i was able to relight remotely,user_136,asset_932,48.0614644,-104.8417043
3/27/2019,Wellhead,Manual Valve,Master Valve,,,Freezing, +BOTH WELL HEAD MASTER VALVES FROZE IN THE OPEN POSITION,user_34,asset_1143,48.1470144,-103.6180489
9/20/2018,Separator,rupture disk,,,,premature rupture,Rupture disk and housing were both rusted and housing seized ,user_33,asset_652,48.00700921,-103.5824857
9/3/2017,Compressor,Cooler,,,,,Down on high suction level. 1st stage,user_156,asset_1675,48.38739517,-103.8413932
12/5/2017,Instrumentation,Switch,,,,,"False call out , low flow well is flowing 1.6mcfd ",user_122,asset_1212,48.36148398,-103.7912185
1/15/2018,Flare System,Flare Header,BMS,,,,Issue: found the SCC was down on the HMI Root Cause: hi winds blew pilot out Fix: relight and returned to service ,user_136,asset_932,48.2608782,-102.900126
5/1/2018,Gas Scrubber Separator,ESD,,,,,Scrubber pots were balled off with fluid I cleared scrubber pots and regulators onsite and and brought well back online.,user_51,asset_350,47.9418861,-103.6976002
8/31/2018,Instrumentation,Controller,,,,,WELL IS CYCLING NOT FLOWING FOUND DVC IS NOT ALLOWING OPERATING GAS THROUGH TO THE CHOKE INTERLOCK ON THE CHOKE IN YOKOGAWA CAN'T GET IT TO CLEAR ,user_34,asset_333,48.1470144,-103.6180489
2/14/2017,Sand Separator,Other,,Other,Other,Other,Glycol pump needs to be replaced and vent hose also,user_39,asset_1683,47.99924562,-103.7086693
4/25/2017,Instrumentation,Other,,Other,Other,Other,Deferal - Communication failure - problem was blown fuse caused by cyclonic actuator trying to close against an frozen valve.,user_65,asset_731,48.1470144,-103.6180489
11/7/2017,Flare System,Flare Knockout,Instrumentation,,,,"Fuel gas on all processes has liquid carry over causing knock out pots to fill up, lines to pumps get carry over causing pumps to shut down and froze off fuel gas to scc's, compressor and flare. We really need to figure out away to dry out fuel gas before it really starts to get cold. ",user_58,asset_876,48.31292867,-103.5273081
10/9/2019,Separator,Temp Control System,Thermostat,,,,"Hi Bath Alarm Call Out, came to location to verify temp and it was at 87 Degrees, false Hi Temp",user_22,asset_942,46.2356189,-100.6010498
2/24/2018,Gas Scrubber Separator,ESD,,,,,Issue: well called out shut in alarm. (INT) valve fault Root Cause: the ESD lost status of open or closed and showed stuck in travel. Fix: got the status to show closed and turned the well back on restarted the shut in cycles ,user_136,asset_612,48.2594705,-102.9010554
11/1/2016,Automation,RTU,Fuse,,,,No damage. RTU had no communication. Must have been powered down for site work. Radio currently communicating. ,user_30,asset_2102,48.07651298,-103.4737187
7/25/2019,Separator,Pipe/Components,,,,Erosion Corrosion (Internal),"There was a weld-olet on the salesline, the threads were stripped out and it was replaced.",user_68,asset_830,48.1511744,-103.6275517
6/27/2018,Gas Scrubber Separator,ESD,,,,,Champ 263 B-50 RTP unit after choke calibration. checked units RTP and started cycles. ,user_71,asset_774,43.252261,-115.0567324
11/1/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Trash,Gas lift down on Low Suction. Walk through and learn compressor. RTP'd. Will have Colton confirm valve alignment.,user_55,asset_345,,
9/22/2019,Plunger System,Plunger,Plunger,Well Master,,Corrosion,"plunger in hole for 14 months, starting to miss and drop production, replaced bar for bar and RTP",user_106,asset_294,40.5262342,-113.8824849
1/25/2019,Separator,Dump Line,,,,Freezing,"Well has been shut in since November 24, 2018. Verified, water tank has been hauled. Pressured up unit, got the burner going. There was some pressure on the flow line, around 150 psi. Got to investigating more, found that the dumps are froze. Dump floats appear to be froze in separator, which leaves me to believe separator is froze. Contacted Team Lead and discussed with him. Shut well back in at well head, and left tag on master valve. Will need a heater on separator.",user_55,asset_1336,,
12/17/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Hydrate in wellhead. Meth is going. Broke and RTPd well ,user_107,asset_382,47.88792825,-103.4698826
4/22/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,kicked well on got plunger to come in. turned off burp settings,user_11,asset_80,40.7126799,-114.1193569
4/19/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"well gets very fluid loaded, vented, plunger fnally came in after 90 min. Will watch cycles, pressure building slowly",user_88,asset_630,48.2573151,-102.9114096
4/15/2018,Pumping Unit,Pumping Unit,Polish Rod,Weatherford,Model 640,Weather,Pump had no oil in oil box. Filled it up. The wicks where old and worn do replaced those also,user_172,asset_1197,,
7/5/2019,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Vented well for 2 hours but could not get to unload. Left well shut in for pressure build,user_18,asset_657,,
4/20/2018,Wellhead,Wellhead Piping,,,,hydrate,"Well head has 3 flow paths for tubing and is configured for plunger. The top 2 flow paths were open and the bottom was closed. With the well being shut in for a long time, the well has high pressure and flow rates. The plunger in the well head was causing a big restriction, opened the bottom flow path so the well can fully flow and unload. ",user_62,asset_398,48.1470144,-103.6180489
3/31/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,Plunger needs vent because of high line pressure last night due to the Williams Dry Lake compressor going down.Vented plunger to surface and rtp well,user_100,asset_1319,48.1470144,-103.6180489
6/28/2019,Tanks/Pits,Flare/Combuster,,,,,well down /found that the dump controller box for the condo dump was missing multiple parts and was not functioning / dump valve was closed and flagged . Got parts for the controller and installed new controller parts. Rtp'd well/ waited for plunger arrivals so that I could adjust dumps properly . This well was flooding the unit when it was getting plunger arrivals / adjusted the choke setting to regulate the fluid entering the unit so the dumps could keep up with the fluid production. I also found the gasket for the water dump controller was leaking / replaced gasket and rtp'd. Plunger making arrivals.Found three scc's out re-lit and adjusted pilot pressure.,user_10,asset_1650,40.5262342,-113.8824849
9/27/2017,Compressor,Compressor,Scrubber Level,Ariel,,Liquid Carryover,"Well went down on high h2o tank levels, had water hauled and brought pad and compressor back online RTP",user_109,asset_1735,48.3272862,-103.6577475
2/28/2017,Instrumentation,Transmitter,3n1 MVT,Rosemount,3095,Other,None found,user_113,asset_1740,48.22197349,-103.6360757
12/16/2017,Gas Scrubber Separator,ESD,,,,,Issue: well called out on shut in alarm Root Cause: well shut in on low unit pressure from the compressor pulling them down so far Fix: turned back on reviewed the sales set points to make sure they were correct ,user_136,asset_1193,48.2609773,-102.899974
11/20/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Dispatched to well ENG wanted well online so they could set 12 hour cycles Got to location and found unit didn't have any pressure and inlet valve was tagged Got OSM approval to remove tags Got unit pressured up and started burner Allowed unit to get up to temp before have OPT open the cyclonic Well was flowing just good OPT asked me to stay onsite until liquids hit surface. Let them know then left, I was halfway to my next stop, OPT called me and told me well did not unload Got back to location and vented well for 28 mins and got it to unload a bit then put it back to sales RTP'd well for ENG",user_56,asset_1181,48.1470144,-103.6180489
3/21/2018,Separator,Temp Control System,Pilot,,,,Plunger lost arrivals and optimization had the well shut in. I checked the methanol which was pumping. The burner was out on the line heater due to the wind blowing the pilot out. I relit the line heater. I checked that bath heater on the unit was still lit. Contacted optimization to turn the well on. The plunger did arrive but we are still holding some back pressure on the tubing. Once the line heater gets to temp this should take care of the problem. ,user_50,asset_38,48.33981572,-103.6365724
11/27/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Check all fuel pots and scrubbers for fluids. No fluid present in ESD or choke Kimray pots from winterizarion project. 4-pac scrubbers dry as well. Considerable fluid present in desi. Drained desi. Root cause appears to be liquid carryover from high LGR wells. Dumps are in good order and dumping as quickly as they can with flow from wells. ,user_75,asset_919,,
6/25/2018,Flare System,Flare Header,Instrumentation,,,,"Flare and 2 SCCs out, relit and returned to service ",user_58,asset_2069,48.36527109,-103.5204534
4/11/2019,Tanks/Pits,Piping,Supply Line,,,Freezing,Replaced Hammer Union that froze and broke / Closing out for Danny M.,user_5,asset_1623,48.1511744,-103.6275517
8/17/2018,Tanks/Pits,Flare/Combuster,,,,,"While on location, found SCC C was down. Pilot had pressure, unknown reason why it was down. Lit SCC",user_15,asset_2237,48.1470144,-103.6180489
9/27/2019,Tanks/Pits,Berm,Dirt,,,Erosion,Rebuilt berm and clean up,user_21,asset_2118,46.2356189,-100.6010498
5/9/2019,Tanks/Pits,Tank Level,Probe,,,Weather,Plunger needs vented but blow down tank is 12’,user_18,asset_317,,
11/16/2017,Compressor,Compressor,Lubricator,Ariel,,Liquid Carryover,Compressor down on low oil pressure. Restarted compressor. ,user_48,asset_1600,,
3/24/2017,Automation,Plunger Arrival Switch,,TripMate,Other,Other,tripmate tests good but does not detect plunger,user_92,asset_853,48.0614644,-104.8417043
1/22/2017,Automation,POC,Relay,Cameron,VSD,Loose Connection,Dvc holding choke open needs trouble shot repaired or replaced,user_175,asset_603,48.10722608,-103.6003163
6/23/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash,"CL 29-160 beaned up to 40/64th dayshift will need to finish opening choke, well is producing as much fluid as separator can handle right now.",user_71,asset_1035,48.1470144,-103.6180489
12/7/2017,Automation,RTU,Relay,ABB,Bristol 3310,Wear,"well called out on high static pressure, well has rig on it and isn't flowing. left as is.",user_71,asset_1754,48.1470144,-103.6180489
3/20/2018,Separator,Fuel Supply System,big joe regulator,,,fluid,well was in int didnt give a reason. looked over t-pack kicked well on achieved plunger arrival. cycles resumed,user_11,asset_647,40.7126799,-114.1193569
11/9/2018,Tanks/Pits,Tank Level,Probe,,,Calibration Issue,"Found that the tank we are pulling out of went empty causing the pump to shut down. This is the new tank, water should siphon out of old tank into the new one. Something happened, not sure what. Had to shut power off to PLC, it was froze up and wouldn't work. Got the PLC going. Purged all lines after I got some water in the tank. Levels are low, slowed pump down.",user_55,asset_1633,,
8/22/2017,Compressor,Compressor (Intergral),Process Gas Supply,,,,,user_71,asset_1678,48.3619066,-103.2129855
5/28/2019,Separator,Shell,Body,,Steel,Corrosion,The original hinges were seized up and needed replaced. ,user_68,asset_518,40.5262342,-113.8824849
12/23/2017,Dehy,Meter (BP Check),,,,,Cold dehy. Williams meter is ok. Thawed bp 4302 5way valve and tubing. Meter zeroed,user_163,asset_2016,48.35595507,-103.6519335
3/28/2017,Wellhead,Other,,Other,Other,Other,no sales,user_39,asset_390,48.224585,-103.8291059
5/7/2019,Pipeline/Piping,Valves,,,,End Of Design Life,"freezing is not a choice, but the valve had to have been leaking, and filled with water. froze and broke, seen this on several locations, froze surface casing valves, ",user_77,asset_164,40.5262342,-113.8824849
3/27/2019,Compressor,Intrumentation,,,,,"Found compressor down on high discharge due to WFS line spike, pressure is down, restarted compressor and location back to normal ops.",user_63,asset_1574,,
2/15/2018,Heat Medium,Pump,Cam,Texam,HBC1,Wear,Regulator failed/leaking,user_111,asset_57,48.0678103,-103.3833473
5/3/2017,Instrumentation,Transmitter,3N1 MVT,Rosemount,4088,Recalibrated,,user_99,asset_414,48.1470144,-103.6180489
2/22/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Vented well due to being loaded. Plunger arrived, RTP'd well, started cycles, and return to optimizer.",user_141,asset_414,40.5481548,-114.0112915
5/27/2018,Tanks/Pits,Liquid Level Control,,,,,"CG 19,20,21 called out on high tank. tank # 33169W at 19-5x18-2, called ibex and shut in #21 well it was the only well open. Dayshift will need to RTP.",user_71,asset_1311,48.1470144,-103.6180489
10/19/2017,Pipeline/Piping,Pipe/Components,,,,Erosion Corrosion (Internal),,user_167,asset_838,48.1602624,-103.6172962
11/19/2017,Fuel Gas/Start Gas,Regulator,,,,,"Liquids froze in scrubber to esd, thawed and rtp well",user_73,asset_1961,48.0854354,-103.6397298
12/14/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drained scrubber and drip pots on esd and dvc found drip pot for well 100 for the dvc had about 2 ounces of fluid in it.,user_100,asset_28,48.1470144,-103.6180489
12/13/2018,Heat Medium,Pump,Housing,Sunpumper,HBT1,Wear,"one of the 1040 glycol pumps was leaking really bad from the diaphragm, some one shut it off and no tag. water dump lines were frozen because that. Replaced pump and heat up the lines for a day and get them clear up, returned wells to sales ",user_21,asset_848,48.1470144,-103.6180489
4/25/2019,Separator,Choke Valve/Loop,,,,Corrosion, +INVALCO INLET VALVE INSTALLED BACKWARDS AND LEAKING SLIGHTLY- *CHECKED GRAPHS AND VERIFIED UNIT OVERPRESSURE LAST NOVEMBER DUE TO VALVE CONFIGURATION- **WM ENTERED TO CHANGE FLOW DIRECTION,user_34,asset_1607,40.5262342,-113.8824849
6/2/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,wellnot meeting load ratio,user_172,asset_1103,48.1470144,-103.6180489
12/7/2017,Compressor - Gas Lift,Compressor,Cylinder,Ariel,,Freezing,gas lift down on high cyc 2 discharge temp. tweaked louver and left on door open to help with cooling. also called bob with jw and left a message to inform him of the issue,user_11,asset_1264,48.1470144,-103.6180489
7/6/2019,Plunger System,Plunger,Plunger,PCS,,Corrosion,Found well was missing plunger arrivals / after looking at the graphs it look like a line spike caused the plunger to load up and the dvc was not responding when the well was going into a on cycle. Vented plunger to surface and inspected and replaced then drained fuel gas line to dvc and cleaned I/P and function tested the choke. Rtpd well confirmed plunger was making arrivals and choke was functioning properly.,user_10,asset_1949,39.2506642,-92.4357879
9/27/2019,Automation,Plunger Arrival Switch,,Tripmate,,,Verified that MSO (Tripmate) was not operational. Replaced (MSO) Tripmate with (MSO) Cyclops. Installed and terminated MSO and RTU. Verified operation of MSO. ,user_169,asset_110,46.2356189,-100.6010498
3/8/2017,Gas Scrubber,Other,,Other,Other,Other,Fuel gas supply shut off,user_161,asset_245,36.2541889,-91.2478009
12/27/2016,Compressor,Compressor,Process Gas Supply,,,Liquid Carryover,"Compressor went down on low suction, ",user_84,asset_276,48.06461571,-103.5054641
5/14/2019,Separator,Burner,Fire Tube,,,Pilot Went Out,"site check, Had to light 10 40 burner, but everything else went good",user_2,asset_793,,
1/2/2019,Separator,Fuel Supply System, Big Joe Regulator,Fisher controls,,freeze,"Pad down since 1/1/19, no fuel supply out, big Joe and scrubber froze. Thawed and broke freezes,verified fuel supply out. Spoke with optimizer to open esd's and main burner on glycol bath. ",user_44,asset_1294,,
7/22/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Corrosion,Choke on separator failed to close properly causing rupture disc and PSV to release.,user_150,asset_1211,,
4/5/2017,Automation,Other,,Other,Other,Other,Diaphragm bad,user_162,asset_1517,,
11/5/2018,Flare System,Flare Header,BMS,,,,Issue: Arrow Dispatch for SCC down Root Cause: SCC # 1 down on flame failure. Looks like as the pressure came down and the SCC wasn't burning the wind blew out the pilot Fix: relight but the pilot needs a better wind box installed. I will get some duck tape tomorrow and see if i can cover the hole a bit better ,user_170,asset_1754,48.1470144,-103.6180489
3/31/2018,Tanks/Pits,Flare/Combuster,flare knockout drain pot,,,,Drained knock out pot for gas from tanks to SCC's. No fluids present.,user_62,asset_2046,48.1470144,-103.6180489
3/8/2018,Instrumentation,End Device,Topworks,,,Water,"install cold fingers to reduce water carryover to instruments, thus minimizing freezing",user_39,asset_1461,48.1470144,-103.6180489
2/28/2017,Gas Scrubber,Other,,Other,Other,Other,Thawed out regulator to the pilot gas,user_100,asset_1892,48.21013158,-103.6494521
2/12/2018,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,Issue: Called out shut in alarm Root Cause: all the wells were in off cycles for so long the pumps used up the fuel gas. Then the compressor went down on low discharge and as soon as it shut down the suction controller shut and we ran out of fuel gas Fix: left one well running to keep gas moving to the comp and keep the pad up. ,user_136,asset_1413,48.0614644,-104.8417043
8/14/2017,Gas Scrubber Separator,Pneumatic Dump Valve,Controller,Norriseal,,Out Of Adjustment,"dump stuck open causing well do shut in on low psi, adjusted controller and will monitor",user_87,asset_568,40.7126799,-114.1193569
4/17/2019,Separator,Liquid Dumps,Body,Kimray,,Corrosion,Condo dump body was washed out and has a pin hole in it. Valve was replaced along with a rebuilt bonnet.,user_68,asset_368,48.1483424,-103.6290208
9/9/2019,Separator,Liquid Dumps,Body,Fisher,,Erosion,"Bonnet tension nut maxed out, indicating bonnet has lost spring tension, valve body and trim set are washed out due to sand production from the well.",user_54,asset_887,40.5262342,-113.8824849
2/18/2019,Separator,Dump Line,,,,Freezing,"blow down valve is froze , heat trace was low temp when arrival to location , adjusted t12 , should thaw out in a day or two, ",user_144,asset_318,48.0881279,-104.0266781
11/16/2017,Automation,Antenna,,Bluewave,,Loose Connection,"was asked to check the line heater pilot out from day shift, found everything working fine but OE Emerson program has been messed up half the day which could have called out, they just got it fixed looks like",user_131,asset_551,40.7126799,-114.1193569
12/11/2017,Compressor,Cooler,,,,,"WFS had lateral freeze on 12-10-17, compressor went down on high discharge pressure. Compressor had dead batteries and would not take a charge with vehicle trying to jump start it. Called out arch rock to replace batteries.",user_62,asset_1495,48.1470144,-103.6180489
1/31/2019,Compressor,Engine,Battery,Caterpillar,,Weather," Kalter and I walked down location and found the fuel gas to the line heater frozen with the line heater down which took down the heat trace on the location and caused all the water dumps on the location to freeze . Used thaw tube on the truck and BP heater on all above ground pipping on the water dump lines to break freezes. Water dump was frozen from the unit all the way to the check valve at the water tanks. Finally got all dumps free from the production unit to the tanks clear. Got fuel gas to the line heater thawed out and started the heat trace system. Contacted Team Leader and eng. (Avery) was instructed to flow well through one unit, watched dumps on unit to make sure they would keep up and everything looked good. Then started troubleshooting the compressor on location found the water dump frozen from the compressor to the main water dump thawed and cleared line . Tried starting compressor and discovered the batteries were dead, these looked to be new batteries for the compressor / contacted Avery about possible battery issue after finding out that they were only 2 week old batteries. Got snow removed from compressor building so that we could jump the batteries , after charging we restarted compressor and loaded set rpms to 1300/ informed Avery of the set points. Rpt'd well and compressor.",user_10,asset_1600,40.5262342,-113.8824849
2/2/2018,Compressor,Compressor,Lubricator,Ajax,,Electrical Short,"compressor keeps going down on false ""no lube flow"", Archrock is trouble shooting the no flow timer on the lubricator",user_24,asset_609,48.1470144,-103.6180489
6/19/2019,Separator,ESD Valve,Gate/Seat,,,Corrosion,"esd was leaking, replaced trim set",user_31,asset_514,43.56424,-91.351691
8/10/2019,Instrument Air,Compressor,Instrument Gas Supply,Compressco,,Trash,Air compressors for instrument air are down again. They continue to over heat on a weekly basis. Spoke with Bob fox and he has not performed a PM on these compressors in awhile. We need to get him out here so he can further troubleshoot the dryer and air compressors ,user_120,asset_516,,
5/27/2019,Flare System,Fuel Supply System,Regulator,Fisher controls,,wear,"found both scc's down , had water in bottom off scc, found pilot fuel gas valve pinched, opened valves and relit pilots ",user_144,asset_268,48.1475232,-103.6191904
11/18/2017,Heater Treater,Burner,BMS,,,Pilot Went Out,Issue: seen on the HMI separator (B) had no flow Root Cause: the pilot location inside the burner is poorly placed and the wind can blow it out easily. once that happened the dumps froze and the unit flooded then it froze. Fix: I adjusted the pilot to try and keep it from blowing back out. long term fix is the pilot needs to be relocated correctly ,user_136,asset_2001,48.1470144,-103.6180489
11/12/2017,Separator,Temp Control System,Pilot,,,,Pilot plugged ,user_156,asset_2239,48.22232239,-103.7509734
12/28/2017,Fuel Gas/Start Gas,Coalescer/Filter,Level Controller,,,,"Issue: Pad shut in alarm. (INT) valve fault Root Cause: Human Error, found the fuel gas flooded out and the desi full causing the scrubbers to ball check off Fix: thawed out and got everything drained ",user_136,asset_628,48.2525318,-102.9484357
8/28/2019,Instrumentation,Meter,Orifice Plate,Control Micro,1,Passed Function Test,Check Communications from Meter to PLC; Collect data and confirm test thru SAMS System.,user_139,asset_128,,
2/12/2018,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,Issue: Called out shut in alarm Root Cause: all the wells were in off cycles for so long the pumps used up the fuel gas. Then the compressor went down on low discharge and as soon as it shut down the suction controller shut and we ran out of fuel gas Fix: left one well running to keep gas moving to the comp ,user_136,asset_932,48.0614644,-104.8417043
12/15/2017,Compressor,Compressor,Process Gas Supply,Ariel,,Trash,Issue: called out compressor down alarm Root Cause: went down on low suction pressure. this is a VRU compressor Fix: Well doesn't make enough gas to support this compressor any more. should be reevaluated and removed ,user_136,asset_1675,48.1470144,-103.6180489
3/18/2018,Flare System,Flare Header,Instrumentation,,,,Issue: gaugers found flare out last couple of days Root Cause: the sparker is burnt up from the flame when the hi winds are blowing the flame burns more in the wind deflector and get it glowing hot and that's where the porcelain burns out of the sparker and then is no good after that Fix: lowered the boom and relight it manually ,user_136,asset_2274,48.1470144,-103.6180489
8/17/2018,Wellhead,Manual Valve,Body,,,Fouling,"Found out side casing valve left open. Ball valve down stream in casing sweep has small leak, closed outer casing valve to prevent loading of the well. ",user_15,asset_2237,49.5499678,-102.9290839
4/11/2018,Flare System,Flare Header,Instrumentation,,,,"Flare will not light using ignitor. Dropped flare and found the wires are no longer hooked up. And the ceramic insulator is completely cracked and won’t carry a current to spark. Attempted to light flare manually. Will not stay lit like my enough to get it raised back up. Wind blows it out. Automation is aware of this issue, and is currently waiting on parts to fix this issue. Left flare down and tagged out. Until we can come up with a plan on getting it lit ",user_172,asset_261,,
11/22/2017,Heat Medium,Pump,Diaphragm Gears,Texam,HBC1,Wear,Replaced graco 1050 glycol pump & RTP'd,user_161,asset_1462,48.2643026,-102.926208
3/23/2018,Instrumentation,Communication Card,,,,,Issue: found well down on the HMI (INT) watch dog timed out Root Cause: the RTU's keep quit talking to each other Fix: i kept resting it and turning the well back on but i wrote a work order for automation to take a better look at it,user_136,asset_297,48.0614644,-104.8417043
11/9/2017,Compressor - Gas Lift,Engine,Cooler,Cummins,,Overheat,shut louver 11/8/17 to help with cooler freezing weather warmed up enough to cause high discharge cylinder 2 overheat opened louvers one notch to help hopefully it will not get a cooler freeze overnight,user_11,asset_1264,48.1470144,-103.6180489
2/21/2018,Separator,Dump Line,,,,Freezing,changed out split hammer union it appears this happened during the last cold snap. put well back into service,user_11,asset_940,40.5481548,-114.0112915
1/21/2018,Chemical System,Pump,Plunger,Texam,HBC1,Wear,North large graco pump had stalled out. Bleed off and restarted ,user_156,asset_1927,48.17178362,-103.5950079
2/10/2017,Tanks,Other,,Other,Other,Other,"pin hole in 4"" tee",user_149,asset_1184,48.3619066,-103.2129855
1/29/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Trash,GL compressor down on LOW DISCHARGE. Adjusted discharge valves going to well head and closed chokes to 30%. Will watch throughout the day. I have advised optimizer of same. RTP'd compressor and hand over to optimizer.,user_141,asset_1264,48.1470144,-103.6180489
6/9/2017,Wellhead,Tubing,,,,,"Well was loaded and needed a vent, was able to regain tubing psi ",user_39,asset_87,48.1587202,-103.6172839
7/10/2018,Instrument Air,Compressor (Recip),Process Gas Supply,,,,"LD 11-10 #130 gaslift control valve wasn’t opening blew out meter and fuelgas and got it working. #110 control valve is stuck partially open tried blowing out meter and fuel gas but it would open back up when fuel gas supply returned, might need calibrated.",user_37,asset_1976,48.0614644,-104.8417043
2/17/2018,Tanks/Pits,Flare/Combuster,,,,,Several scc out. Relit three of them. They won’t stay lit wind keeps blowing it out ,user_172,asset_1574,,
2/23/2018,Separator,Dump Line,,,,Trash,Location shut in on low unit pressure. Found that the dehy dump was hung open and had taken the pad down. Reset dehy dump and jumped whole pad back on all wells back on and in cycles,user_100,asset_28,40.5481548,-114.0112915
2/5/2019,Flare System,Flare Header,Regulator,,,,Issue: while performing my walk around i found SCC # 4 down Root Cause: went down on pilot fault Fix: relight using the onboard remote lighter. if we made these SCC's stop shutting down on low pressure and run all the time it would stop pretty much all the failures we have and unreliable issues ,user_170,asset_1915,48.1470144,-103.6180489
7/21/2018,Automation,Antenna,,Bluewave,,Electrical Short,Power bump caused Land shark to loose comms. Reset alarm and that restarted land shark,user_55,asset_1322,40.5262342,-113.8824849
9/10/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Well was loaded due to cycles. No other issues found ,user_107,asset_960,48.06769534,-103.3837258
9/23/2017,Compressor,Compressor (Recip),Cylinder,,,,Compressor down on Low Suction Pressure. Restarted compressor and loaded it. ,user_41,asset_1761,48.20250522,-103.5987394
3/22/2017,Gas Scrubber,Pnumatic Dump Valve,Controller,Other,Other,Other,,user_179,asset_1967,47.92049902,-103.4945947
2/12/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,"Compressor down on low suction, pad compressor down as well, compressor ran out of suction pressure over time. Bled down compressor found hydrate in the 3rd sage as well, traced out methanol injection lines and double checked methanol rates, found pump turned off, turned pump back on check rates and verified at compressor, injecting methanol prior to 3rd stage cooler, also bled down each meter on the 10 and the 150 and found no hydrates/ Started the compressor and RTP'd verified injection rates with optimizer",user_115,asset_1264,,
2/9/2018,Chemical System,Pump,Plunger,Texam,HBC1,Wear,Repacked methanol pump and pump would not re-prime after an hour of attempting to RTP. OPS ordered a new methanol pump to replace this one. Plunger is likely been worn down enough to no longer contact packing and get a good seal.,user_6,asset_1475,36.2541889,-91.2478009
4/30/2018,Tanks/Pits,Liquid Level Control,,,,,High tank,user_86,asset_1714,,
12/15/2016,Wellhead,ESD Valve,,,,Freezing,Supply gas to SCC thawed unit back on ,user_176,asset_92,48.21103859,-103.6486584
3/16/2018,Compressor,Compressor,Process Gas Supply,Ariel,,Vibration,"Issue: Called out compressor down alarm Root Cause: down on code # 19 hi discharge pressure. Found the auto louvers were still open on the cooler with the out side temp of 30deg and a 7mile an hour breeze along with the hi humidity possibly caused a cooler freeze. Fix: I adjusted the T-12 to close the louvers, recycled the compressor long enough to verify the freeze was gone and returned to service. I also pinched the side doors down to keep the wind from blowing across the lines but left the roof open so if it gets warm during the day it can still exspell some of the residual heat from the compressor ",user_136,asset_296,48.2594738,-102.9011108
12/3/2017,Compressor,Compressor,Scrubber Level,Ariel,,Liquid Carryover,Drain scrubbers pots on compressor,user_109,asset_1600,48.3606083,-103.6350132
11/25/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Cleared scrubber and fuel pots to ESD's ,user_51,asset_1561,48.1470144,-103.6180489
12/11/2017,Plunger System,Plunger,Plunger,IPS,,Scale,plunger was froze in lubricator. i shut in well head and depressure flow line. plunger thawed. repressured and heard plunger fall down hole cycles started in an off,user_11,asset_1281,48.1470144,-103.6180489
4/5/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,wear,"Multiple gauges on front end fuel supply not working, parts ordered",user_35,asset_768,48.18429608,-103.4264528
12/29/2017,Fuel Gas/Start Gas,Coalescer/Filter,Level Controller,,,,Desi was full of liquid. Drained,user_156,asset_1108,48.19956992,-103.6184819
3/17/2018,Tanks/Pits,Flare/Combuster,,,,,Large flare pilot was out. Possible it went out when compressor was running and only pilot was on. Some liquid in regulator. ,user_156,asset_1383,48.38779817,-103.8109224
3/9/2019,Separator,Dump Line,,,,Corrosion,"Dump trim from high pressure unit to LP unit packing was bad and leaking. These go bad over time just from use. Replaced packing, leak tested dump line. All is good. ",user_15,asset_787,48.2816347,-102.8553854
4/9/2018,Wellhead,Wellhead Piping,,,,,returned well to production after a pressure build,user_11,asset_821,40.7126799,-114.1193569
5/12/2018,Tanks/Pits,Flare/Combuster,,,,,SCC was shut in. Sump pull?,user_163,asset_1274,48.1470144,-103.6180489
11/16/2017,Wellhead,Cyclonic Valve,Gate/Seat,,,Fouling,LEAKING TO TANKS ,user_119,asset_2191,48.1602747,-103.6173515
12/28/2017,Heater Treater,Burner,BMS,,,Plugging,Issue: found bath was 46deg on the HMI Root Cause: the pilot plugged off Fix: cleaned out the pilot tip relight and returned to service ,user_136,asset_546,48.1470144,-103.6180489
3/28/2019,Separator,Fuel Supply System,Regulator,Fisher controls,,freeze,"regulator filled with fluid and froze, causing gasket to be expanded and allowed gas to leak by. replaced regulator and put back into service. liquid drop out may have increased due to running bath temps higher for solar glycol pumps, will need site visit more often as temps drop",user_17,asset_1143,,
4/4/2019,Tanks/Pits,Piping,Load Line,,,Freezing,Water tank load line had froze and split. Load lines were removed and camlock fittings with dust covers were installed.,user_68,asset_1742,48.1470144,-103.6180489
9/30/2017,Flare System,Flare Header,Process Indicator,,,,,user_48,asset_1419,,
2/13/2018,Separator,Dump Line,,,,Corrosion,replaced choke stem and seat also rebuilt condo and water dump trims,user_11,asset_407,48.1470144,-103.6180489
3/18/2018,Compressor,Compressor (Recip),Scrubber Level,,,,Flange going to the sight glass on the 1st stage scrubber leaking ,user_46,asset_1346,48.0614644,-104.8417043
10/23/2019,Fuel Gas/Start Gas,Regulator,,,,,Pilot tip plugged up. Manually cleaned tip,user_147,asset_2278,,
4/11/2019,Separator,Temp Control System,Heater/Burner,,,,"Burner and pilot both out, close valves and vent relight pilot return to service",user_109,asset_1406,48.20576589,-103.5011558
3/18/2017,SWD System,Other,Other,Other,Other,Other,,user_117,asset_1489,40.5481548,-114.0112915
7/20/2019,SWD System,Particle Filter,Element,,,,Replaced filters and restart pump. Will monitor throughout the day. Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_101,,
11/21/2017,Separator,Liquid Dumps,Seat/Ball/Piston,Norriseal,,Corrosion,replaced trim and seat,user_87,asset_926,40.7126799,-114.1193569
1/21/2019,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,"Issue: found ESD open but well not cycling Root Cause: Human Error, verified the dumps were all open and valves are properly lined up. Fix: started the cycles and turned the well back on to confirm flow and everything looks good other than the surface equipment I will write a WM for ",user_170,asset_608,43.56424,-91.351691
3/26/2018,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,"Knock out pots, to flare, fuel gas to flare, line heater, and line heater scrubber had liquids. Wells flowing over 110deg carries liquids through the gas stream which drop out in these pots and scrubbers. ",user_58,asset_1421,48.40624754,-103.5809682
1/23/2018,Automation,Solar Panel,Glass,BP Solar,,Weather,Cleared snow off solar panels while on location responding to SCC call out.,user_62,asset_903,48.1470144,-103.6180489
1/4/2019,Recirc Pump,Pump,Instrumentation,Goulds,HBT2,Freezing, • North pump ? Found a bad motor ? Replaced bad motor ? Tested and verified pump now stroking Left pump running at 2.3 Amps,user_38,asset_1978,46.2355104,-100.6413984
2/25/2018,Automation,Charging System,,,,,"ASC solar regulator failed. Unknown cause, likely just end of useful life.",user_134,asset_168,40.5481548,-114.0112915
8/29/2018,Gas Scrubber Separator,Pneumatic Dump Valve,Seat/Ball/Piston,Invalco,,Wear/Tear,"Got to location found compressor down, Restarted compressor, relit one SCC Vented the 30 well for 30 mins while it was venting i found that the water dump was leaking. Well is extremely loaded ROOT CAUSE, leaking water dump. Replace trim and seat RTP'd well ",user_56,asset_345,48.1470144,-103.6180489
11/30/2016,Wellhead,,Stem/Seat,,,,Vented up and changed out plunger in effort to increase production,user_35,asset_1551,48.05345055,-103.668374
7/29/2019,Pipeline/Piping,Valves,,,,Corrosion (Internal),Replaced all blow down valves and one choke on the 160 well,user_157,asset_505,46.2356189,-100.6010498
7/28/2018,Wellhead,Tubing,,,,hydrate,"Well has been long term shut in, when i went to put it on, found it to be froze down hole. Well was equalized for 48 hours then I was able to break the freeze. ",user_15,asset_574,48.1470144,-103.6180489
1/27/2017,Gas Scrubber,Dump Line,Dump Line,Other,Other,Trash,-21 and bad design. Frozen lines,user_163,asset_1586,47.93865766,-103.5041047
11/30/2016,Wellhead,,,Other,Other,,Pulled graphs found the 130 was not flowing check will head down casing valve shut on pump Rod well opened casing valve and put it back to sales,user_122,asset_2246,48.36330407,-103.7893408
5/14/2019,Tanks/Pits,Dump Line,,,,Corrosion,UKNOWN: Leak is below grade and will require a maintenance crew to dig up and RCFA.,user_54,asset_410,40.5262342,-113.8824849
3/10/2017,Automation,Other,,Other,Other,Other,Broke isolation pvc ,user_162,asset_1331,,
1/3/2019,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_1633,,
11/30/2017,Separator,Temp Control System,Heater/Burner,,,,blew out ,user_53,asset_1689,40.5262342,-113.8824849
7/18/2019,Site Power,External Supply,,,,,"Call from IBEX Pusher around 4:15 am. He advised that there were a couple of drivers on location when there was a loud boom and big flash. This immediately set off red lights and ESD'd location. Pusher stated that this startled the drivers and they immediately left location. Said it could have been a transformer or something of that nature. Arrived to location. Had contacted night shift operator to meet me here. He started checking poles in the area. Found one with fuses hanging loose. This pole was located off of location, about 200 yards from entrance. After further investigation, this was the only pole we could find with fuses tripped. Contacted OSM and advised of findings. Contacted Rocky Mountain Power about fuses. Gave them pole number and directions. Left my number with RMP service dept call center. Was contacted later by their tech about location, pole number and directions. We stayed in contact throughout the morning. Did come back to location and cleared alarms to shut off red lights. Kept location down per conversation with OSM until we hear differently from RMP. Tech did advise that he had a crew coming this way with new transformers. This pole got a hard hit of lightning which caused all transformers to fail, even melted a hole in the side of one of them. His words. He advised that we are good to operate normally, this was around 10:30 am. Contacted OSM and advised of findings. We have to have location down for maintenance work anyway. ",user_55,asset_101,,
5/16/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Venting plunger to surface, 3 times. To get casing psi down , brought up 27 bbl in two runs, going for one more, then Rtp, gauge tanks and enter in vent log",user_84,asset_412,47.95856066,-103.5098499
6/18/2018,Tanks/Pits,Flare/Combuster,,,,,RIG REQUEST RTP well. ARROWPLUS scc out. Well is open to sales. Took pilot apart and checked. Adjusted pilot head since it had been tampered with. ,user_156,asset_2138,48.30947457,-103.6584135
3/19/2018,Instrumentation,Meter,Orifice Plate,Bristol,FB100 RS232,Calibration Issue,"Meter showing false flow in the off time. OPS shut in the well and the separator to see if vaves were leaking over a five minute test and well continued to false flow. OPS emptied less than an ounce of fluid out of the meter plate housing and meter continued to false flow. MEAS to further RCFA, WR entered.",user_6,asset_461,36.2541889,-91.2478009
1/15/2017,Compressor,Compressor,Suction Controller,,,Freezing,Compressor went down on low suction due to the 70 esd freezing and closing. Thawed supply gas to esd on 70 returned to service. Put compressor back online ,user_11,asset_573,,
9/4/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_1633,48.3619066,-103.2129855
12/15/2016,Wellhead,Primary Choke,,,,,"Found Hi-low was hydrated off, glycol pumps stalled and heat trace system was not functioning correctly. Relieved pressure from pumps and re-applied pumps started functioning correctly, cleared hydrate in hi low and RTP'd ",user_115,asset_2173,48.04140337,-103.6621722
11/9/2019,Wellhead,Manual Valve,Master Valve,,,Freezing,"Upon arrival found unit up with bath @ temp, noticed good pressures, pulled graph on well and seen that it had not been flowing. Spoke with optimizer and found that well had a SI command on it but could not find a reason why, optimizer removed SI and kicked off well. Shut back in after a couple minutes because it registered an arrival, plunger was hung in lubricator. Started thawing on lubricator, attempted to shut master valves so I could hear plunger when it dropped but could not move, valves were also froze. Swapped thaw tube to master valves, while thawing on valves noticed the bypass valve for the glycol at the wellhead was open so the wellhead was not getting any heat, closed bypass and verified discharge and return were both open but still could not hear anything moving through the lines. Checked valve alignment at unit and found there was only 5 psi going to pump, adjusted regulator and pump began working. Also noticed the pump going to the tanks was pumping fast, gauge was pegged out, backed off regulator. Walked to tanks to check heat trace valves there and found the bypass for the heat trace at the condo tank was also open, closed and verified all other valve alignment was correct. Started noticing good warm circulation at tanks and wellhead, bath temp was @ 110 degrees but separator temp was 90, adjusted t-12 down slightly. Checked master valves again and was able to get positive isolation, swapped thaw tube back to lubricator, shut top and bottom flow path, after 20 minutes opened tbg masters slightly, could not hear the plunger but could hear ice moving, shut choke, opened top and bottom flowpath and equalized well. Left equalized for another 20 minutes and could hear plunger dropping, returned all valving to normal operating position, patched up the insulation where I cut and let the optimizer know so cycles could be reset. However the plunger will freeze in cap again because there is no methanol tank or methanol pump on location, I completed the winterization checklist for this site and put in a request for a tank and pump, will speak with TL about getting methanol set up on location.",user_177,asset_1545,38.4425988,-95.5406131
3/21/2018,Fuel Gas/Start Gas,Regulator,,,,,"Checked all scrubbers, separator A had some fluid in it. Dumped scrubber. Checked all dumps and adjusted a few. Baths are good",user_141,asset_1350,48.1494385,-103.6217589
12/12/2017,Instrumentation,Communication Card,,,,,Issue: callout low flow alarm (OFF) Root Cause: well is flowing fine keeps calling out but the alarm has cleared before i ever even get the callout Fix: refine the callout for better reliability ,user_136,asset_1035,48.1470144,-103.6180489
3/26/2018,Dehy,Contactor,Trays,,,,after troubleshoot found that the dehy is shut in waiting on dehy flush. left as is,user_11,asset_945,40.7126799,-114.1193569
1/13/2019,Compressor - Gas Lift,Engine,Cooler,Baldor,,Misalignment,"cooler louvers weren't actually closing 100%, probably open 1"", adjusted controller so it closes",user_31,asset_1049,43.56424,-91.351691
12/22/2016,Wellhead,ESD Valve,Gas Supply Line,,,Freezing,Freeze in sales line took pressure off both sides cleared back on,user_176,asset_33,48.19681022,-103.6330395
3/29/2018,Wellhead,Tubing,,,,,"Very loaded well, well equalized ",user_35,asset_1964,48.18248203,-103.5381473
1/10/2017,Automation,Radio,,,Other,Other,,user_134,asset_201,48.1581465,-103.6169782
3/28/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"second vent, loaded from choke hanging open",user_88,asset_220,48.2574684,-102.9114636
4/17/2017,Compressor,Other,,Other,Other,Other,,user_35,asset_2186,48.32423942,-103.6008608
2/5/2018,Instrumentation,Meter,Orifice Plate,Control Micro,4203DR,Wiring,,user_13,asset_72,36.2541889,-91.2478009
10/28/2016,Instrumentation,Tank Level,Sensing Cable,,Other,Weather,Level switch failed,user_65,asset_2254,,
7/14/2018,Separator,Liquid Dumps,Controller,Norriseal,,Freezing,Found water dump conroller door left open. Closed door.,user_62,asset_2142,43.252261,-115.0567324
2/8/2017,Tanks,Valving/Swedges,Seat/Ball/Piston,Other,Other,Other,761563W load line split and leaking,user_23,asset_82,48.1602882,-103.617253
3/17/2018,Gas Scrubber Separator,ESD,,,,,buy back line was froze from dehy I broke freeze and put wells back online,user_51,asset_915,48.0614644,-104.8417043
1/26/2019,Automation,RTU,Fuse,Schneider/Scadapack,Scadapack P4A,Weather,3A automotive fuse blown. cause unknown.,user_12,asset_994,40.5262342,-113.8824849
11/2/2017,Compressor,Intrumentation,,,,,Proublem:Compressor keeps going down on low discharge pressure. Root Cause: is possibly two different issues. with the newer line pressure when the comp goes into recycle it bumps the low discharge pressure set point and shuts the comp down Archrock may need to lower the set point. I also found the inlet control valve has been adjusted down so low it wouldn't fully open and was causing the recycle to always be open. possibly not knowing the issue was line pressure and not the compressor using up all the recycle. Fix: I adjusted the suction control valve to open up enough to just use well gas until the pressure comes down enough to use recycle and that should help the comp stay running and will get with an Archrock operator to take a look at it.,user_136,asset_2241,48.1470144,-103.6180489
4/9/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Drained desi. Not a lot of liquid. Scrubber and regulators had a mist. Not sure desi is working at 100%,user_156,asset_102,48.32393222,-103.6179887
3/8/2018,Instrumentation,Controller,,,,,"Kelvin controlled well. Kelvin lost plunger arrivals, well was doing just fine. Once kelvin lost arrivals, it continued to add off time but never added flow time to attempt to get plunger to surface. This well requires a double vent to get back. TBG at 340 CSG at 626 BDT at 6' 5"" Opened to AGT First vent duration was 24 mins. Did get plunger to surface. Shut BD valve and allowed plunger to fall for 60 mins. Second vent TBG at 500 CSG at 628 Duration 8 mins Restarted plunger cycles and RTP'd well ",user_53,asset_181,48.2649339,-102.8791315
2/21/2019,Separator,Dump Line,,,,Freezing,"Attempted to RTP well. Found that the scrubber was ball check. Drained scrubber, and got the ball to drop. Got the burner relit on Sep A. Started checking dumps, found that dumps are froze. Checked a few others and all are froze. Will write a work order to have steamer come and thaw dumps.",user_55,asset_44,,
4/23/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash,Issue: well is starting to low flow and the tubing was climbing Root Cause: found there was some junk plugging up the choke on the line heater Fix: worked choke and got to pass through then i worked the choke open to a 38,user_136,asset_567,48.1470144,-103.6180489
1/16/2017,Gas Scrubber,,,,,Other,diaphragm in glycol pump was bad. pump replaced with a rebuilt pump. ,user_149,asset_363,48.3619066,-103.2129855
1/18/2019,Separator,Dump Line,,,,Freezing,water and condo dump freeze request steamer to thaw ,user_57,asset_515,48.0531581,-104.872299
8/6/2018,Compressor - Gas Lift,Compressor,Valves,Ariel,,Freezing,"PV Well lost injection, gas lift compressor was still online. Methanol tank had some methanol in it, pump was pumping. Back blew the injection line and got hydrate to break. RTP'd well ",user_56,asset_910,48.2726117,-102.8735904
6/18/2018,Tanks/Pits,Flare/Combuster,,,,,CALLOUT SCCs out. Location check. A scc was out. Checked it out. Took apart. No issues. Relit ,user_156,asset_854,48.19911152,-103.617348
1/17/2018,Separator,Choke Valve/Loop,,,,Corrosion,"Choke leaking past, TR entered with MAINT to replace, ESD shut, OPT informed and well status recoded.",user_6,asset_2138,36.2541889,-91.2478009
1/26/2018,Flare System,Flare Header,Regulator,,,,CL 29-160 SCC callout. Relit SCC,user_71,asset_1035,48.1470144,-103.6180489
12/12/2017,Tanks/Pits,Piping,Supply Line,,,Freezing,Blow down line to tanks frozen. Found pump had stalled out due to discharge line was shut causing pump to stall. Opened discharge line and pump started stroking. Thawed out blow down line with pump.,user_62,asset_1168,48.1470144,-103.6180489
4/9/2017,Wellhead,Primary Choke,Stem/Seat,Other,Other,Other,choke had a hydrate. broke freeze and started cycle,user_11,asset_963,,
7/1/2019,Sales Valve (PV),Sales Valve,Body,Valvcon,,End Of Useful Life,The blowdown valve was leaking by internally and it was replaced.,user_68,asset_58,48.1470144,-103.6180489
12/4/2018,Tanks/Pits,Flare/Combuster,,,,,"main valve to scc was shut, might have been from a sump pull, opened",user_31,asset_563,43.252261,-115.0567324
5/19/2018,Sales Valve (PV),Sales Valve,Body,Automax,,Washed Out,2” sales line valve was replaced but leaking 2” ball valve right beside it was not. Ordered parts and replaced bad valve and rtp unit. ,user_35,asset_2003,48.17914917,-103.4307498
3/19/2017,Wellhead,Primary Choke,Stem/Seat,Other,Other,Erosion,choke eroded replaced with new choke and stem,user_11,asset_2089,,
6/18/2019,Automation,Solar Panel,Glass,BP Solar,,End Of Useful Life,cows have destroyed to solar panels and pulled one completely off CP,user_144,asset_2019,40.5262342,-113.8824849
4/21/2017,Compressor,Compressor,Panel,Other,Other,Other,Compressor was down on low interstage pressure. Restarted and loaded.,user_62,asset_1394,48.1470144,-103.6180489
11/2/2017,Separator,Choke Valve/Loop,,,,Trash,"Root cause is not trash, choke may need re calibrated its hanging open afterbwell flows",user_103,asset_1785,48.32740517,-103.6574691
2/18/2019,Pipeline/Piping,Valves,,,,Corrosion (Internal),Balon check valve threads corroded and leaking,user_33,asset_1600,48.33586705,-103.59849
6/11/2019,Pipeline/Piping,Pipe/Components,,,,Overpressure,WFS compressor station down causing high line pressure at 200psi above normal.,user_63,asset_705,,
3/5/2018,Compressor,Compressor (Recip),Dump Valve,,,,"Compressor went down on HI scrubber level. Closed the suction valve, and drained compressor through scrubbers. Found out that the water dump line is clear and not froze. Will have to get with ArchRock when they come out to do a PM to look into that dump controller. Compressor went down a few times while troubleshooting Started the compressor and let it warm up. Once it got up to temp I loaded it. RTP'd compressor",user_53,asset_204,40.5960545,-113.9323891
3/16/2017,Instrumentation,Transmitter,3n1 MVT,Rosemount,4088,Passed Function Test,,user_113,asset_1623,48.06822043,-103.3856008
7/27/2018,Tanks/Pits,Liquid Level Control,,,,,Issue: called out well shut in alarm. (INT) low bath level Root Cause: when i got to location i found the glycol truck there finishing up Fix: once i found out it was him that shut the wells in i turned back on and restarted the plunger cycles ,user_170,asset_1892,48.2595184,-102.9009315
2/19/2019,Surface Location,Lease Road,,,,Weather,"Cannot access location due to drifted in road, could not access location last week to switch tanks due to drifted in road, ",user_25,asset_365,,
3/7/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,changed out worn rapid flow plunger with new bar plunger,user_11,asset_1792,40.7126799,-114.1193569
3/5/2019,Plunger System,Plunger,Flow Tee,PCS,,Not Optimized, +GRAPHS INDICATE THE WELL IS VERY LOADED AND THE PLUNGER QUIT RUNNING- ARROW INDICATES PLUNGER REPLACED OVER A YEAR AGO,user_34,asset_1740,43.56424,-91.351691
11/20/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,"choke is froze, cannot open to tank to break freeze due to tanks being at 13.5 feet ",user_53,asset_1867,48.160134,-103.6170233
8/27/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,adjusted max choke open from 60 percent to 75 percent and paused flowing plunger came in on its own cycles resumed,user_164,asset_993,48.224585,-103.8291059
10/12/2017,Compressor,Compressor,Regulator,Ariel,,Trash,"Found pad not flowing, found compressor recycling, found 30 HPG out of adjustment, adjusted regulator verified repair , flowing 1.6mcfd",user_122,asset_2108,48.36297135,-103.7896123
10/31/2018,Compressor,Intrumentation,,,,, Compressor down on low discharge I went to location and found that the dump on interstage #2 had stuck open I was able to get the dump to stop hanging open cleared alarm and restarted.,user_159,asset_1383,43.252261,-115.0567324
5/18/2017,Wellhead,Tubing,,,,,"Well has had coil tubing freeze for awhile finally got it broke and flowing up tubing/shut the tubing side down b and flowed casing with the heat trace going yesterday, this morning I closed casing and popped tubing to tank and got it broke unloaded well and rtp'd-so a lot of the times it takes a couple of times going to well not just once !!!!!!!",user_131,asset_87,48.02484458,-103.7386746
7/9/2018,Instrumentation,Transmitter,Tubing Pressure,Rosemount,3051,Weather,Transmitter completely dead,user_134,asset_2120,43.252261,-115.0567324
1/24/2017,Automation,RTU,Fuse,ABB,Total flow Micro,Electrical Short,No damage. Fuse was blown for glycol pump controller. ,user_30,asset_1821,47.92007142,-103.4942229
4/20/2019,Water Transfer,Transfer Pump,,,,Corrosion," +FILTER POT #2, ALMOST THE SAME ISSUE, GASKET STARTING TO UNWIND AND WAS NOT SALVAGEABLE.",user_34,asset_523,40.5262342,-113.8824849
2/19/2018,Gas Scrubber Separator,Back Pressure Valve,Sensing Line,Kimray,,Corrosion,LD 8-70 #30 pilot out Didn’t make it to location dayshift will need to check.,user_71,asset_699,48.1470144,-103.6180489
3/26/2019,Instrumentation,Meter,Orifice Plate,Nuflo,1,Weather,"Found Liquids in Sensing Lines, Blew down Lines and check zero",user_139,asset_1460,,
5/18/2018,Flare System,Flare Header,BMS,,,,Issue: found flare out Root Cause: without both wells running the flare doesn't go off as much and it looks like the wind blew it out Fix: relight and returned to service ,user_136,asset_705,40.7126799,-114.1193569
10/24/2017,Plunger System,Plunger,MSO,ETC,,Wiring Shorts,MSO not detecting arrivals ,user_3,asset_1521,47.9337809,-103.5068983
10/23/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,unit lost pressure and well went down,user_179,asset_872,40.5262342,-113.8824849
2/7/2018,Heat Medium,Pump,Valves,Goulds,HBT2,Weather,Found heat trace at well head bypassed and not tagged as to why. Well head was frozen due to heat trace valves not lined up propperly. Corrected valve positions and validated heat trace was warm and no leaks. Will have to come back later after well head thaws out.,user_62,asset_1510,48.1470144,-103.6180489
6/4/2019,Dehy,Piping,Discharge Line,,,Freezing,"Dump line from Dehi to the tank is leaking in several places I believe, liquid is squirting out from the insulation.",user_22,asset_2009,46.2356189,-100.6010498
8/5/2019,Safety Systems,rupture disk,,,,premature rupture,Started to pressure up separator. Rupture disk is blown. Shut well head and choke tagged out ,user_90,asset_1419,48.19702828,-103.557773
6/1/2018,Flare System,Flare Header,BMS,,,,Issue: found SCC (A) down on the HMI Root Cause: buy the look of all the water in the bottom of the SCC and in the ditches it looks like it rained really hard and flooded out the pilot and knocked it out Fix: relight SCC and returned to service. Long Term Fix: May want to look at putting the pilot horizontally that way the rain wont be able to go down the pilot tip and flood out the pilot flame ,user_136,asset_991,48.1470144,-103.6180489
8/10/2017,Gas Scrubber Separator,Pneumatic Dump Valve,Seat/Ball/Piston,Norriseal,,Wear/Tear,dump trim wore out and leaking,user_87,asset_608,40.7126799,-114.1193569
3/10/2018,Compressor,Compressor (Recip),Scrubber Level,,,,Drained scrubbers,user_46,asset_276,48.0614644,-104.8417043
4/8/2017,Sand Separator,Other,Other,Other,Other,Other,Loss of prod. Hi Lo wouldn't open after scrubber float shut off flow ,user_175,asset_1683,47.94926106,-103.6510388
3/18/2018,Separator,ESD Valve,Actuator,,,Corrosion,Asco solenoid inoperable due to loose conduit fittings allowing liquid to rot away wires.,user_134,asset_1564,48.1470144,-103.6180489
3/1/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,Have hand dig crew remove snow for techs to perform work.,user_125,asset_2083,48.1511744,-103.6275517
11/1/2017,Compressor,Compressor,Suction Controller,Ariel,,Freezing,compressor down on low suction pressure. 10/31 i shut the 70 well in for a pressure build so i could change out pacemaker sleeve 11/1 and there was quite a bit of fluid that i drained out of the suction control valve. i drained suction control valve and ensure proper function and changed out worn pacemaker sleeve. returned compressor back into service.,user_11,asset_573,48.1470144,-103.6180489
11/26/2017,Chemical System,Pump,Housing,Texam,113,Wear,Glycol pump is not working. ,user_141,asset_1591,,
4/28/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_1633,48.1002316,-103.5870123
5/9/2018,Wellhead,Tubing,,,,hydrate,Froze ,user_86,asset_1688,,
10/22/2017,Compressor,Compressor (Recip),Transmitter,,,,Compressor down on low 1st stage pressure. Rtpd compressor an wells 110 and 120. Equalized pressure build wells 70-20-130,user_163,asset_995,48.35319818,-103.7749185
1/6/2019,Separator,Temp Control System,Heater/Burner,,,,Burner out relit remotely ,user_63,asset_1525,48.33490027,-103.6422922
3/29/2019,Separator,Choke Valve/Loop,,,,Freezing,"Dvc sticking not allowing choke to open, tapped on dvc and choke opened. Well flowing. ",user_44,asset_1202,,
10/13/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_1633,,
6/11/2019,Separator,Choke Valve/Loop,,,,Trash, Location shut in on low unit pressure I went to location and found that the #90 dvc was fluid locked shut I was able to get the choke to operate correctly and brought pad back online.,user_159,asset_255,43.56424,-91.351691
4/1/2018,Fuel Gas/Start Gas,Coalescer/Filter,Regulator,,,,Fluid inside red kimray drop pot on ESD. Estimate of fluid was 1/4 of the way full. Manually drained fluid.,user_107,asset_1059,,
9/2/2017,Flare System,Flare Header,Process Indicator,,,,Relit 5 SCCs ,user_156,asset_1525,48.33925136,-103.6376125
1/21/2019,Heater Treater,Burner,BMS,,,Loss Of Fuel Gas,"Issue: found Bath (B) down. Root Cause: Human Error, fuel gas was routed from the wells rather than the buy back so when the units ran out of gas it took the burner down Fix: routed the fuel gas to the desi and back but found its froze. was able to get the other unit feeding this unit as well. then relight the bath and got the pumps running to start thawing some of this stuff out. ",user_170,asset_608,43.56424,-91.351691
11/14/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Desi and fuel gas of liquids,user_109,asset_1677,48.327245,-103.6565
3/15/2019,Wellhead,Tubing,,,,hydrate,"Attempted to thaw out location utilizing steamer crew. Well was shut in from night ops.green complete unit is filled with fluid but can not get pressure over to green complete to drain fluids.both top master valves were frozen open. Thawed out valves using steamer. Flowline/sand can are still froz3.well has 1500psi on tubing and valve manifold has zero. Put gauge on can and got zero. Got permission to remove larry Bateman lock on both plug valves on sand can blow down line. Attempted to blow well to pit using this line and still got no pressure. Eventually used all the water steamer crew had. Heater is on sand can,put some more tarps on can. Contacted team lead and requested a steamer tomorrow morning and another heater on location to be placed on green complete unit. Location is shut in and tagged out",user_120,asset_796,48.39006308,-103.5865716
11/27/2018,Gas Scrubber Separator,ESD,,,,,Wells shut in on low unit pressure I went to location and jumped pad back online while on site #80 ESD wouldn't open and was leaking out the weep hole I put in work order for automation.,user_159,asset_217,48.3619066,-103.2129855
3/21/2018,Wellhead,Wellhead Piping,,,,hydrate,cleared flow line freeze and put well back into service,user_11,asset_1526,40.7126799,-114.1193569
8/26/2018,Tanks/Pits,Tank Level,Sonar,,,Calibration Issue,Real high tank 770080,user_31,asset_1675,48.38772584,-103.841106
8/25/2019,Automation,RTU,Io,Emerson,Bristol 3310,Weather,"Well was interlocked on WD Timeout. Thought I would try resetting and seeing if I could get well to flow. Was able to reset interlock. Well started cycles, RTP'd",user_55,asset_395,,
12/8/2016,Gas Scrubber,,,,,,Frozen in the temp. Divert valve thawed the divert rtp well,user_100,asset_2168,48.12587744,-103.6163603
1/12/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,"Freeze Hi-lo valve, not getting pressure into seperator. Thawed on hi-lo valve and Inlet of seperator, broke freeze and verified gas flow into seperator. ",user_44,asset_609,,
3/3/2018,Chemical System,Piping,Discharge Line,,,Connections,Plunger well appeared to be froze in the tubing. Found all the bypasses open on the electric methanol pumps. Closed all of the bypasses and ensures pumps were purged to begin pumping methanol on the plungers. Leaving the well shut in to allow methanol to pump on the freeze. Will have weekend guy RTP on Sunday. ,user_50,asset_197,47.99287215,-103.4222499
8/14/2018,Chemical System,Pump,Check Valve,Texsteam,HBT1,Debris,"ARROW PLUS Dispatched to well because it is deferring, looks like it could be froze in the back side. Back blew back side and got hydrate to break Methanol pump stalled out had to work on it and got it going again RTP'd ",user_56,asset_634,48.2744209,-102.8765361
1/3/2018,Fuel Gas/Start Gas,Regulator,,,,,Wells began shutting in on location due to freezing at DVC knock out pots ,user_102,asset_446,48.1111294,-103.7133239
10/31/2019,Separator,Fuel Supply System, Big Joe Regulator,,,freeze,TRIDO PUMPS ARE BLANK SCREEN AND WILL NOT TURN ON SO LOCATION HAS NO GLYCOL CIRCULATION. thawed out water dump on LP. broke freeze in sales line. thawed out sales meter and started cycles. location wont stay up for long with no pumps.,user_120,asset_2069,40.5262342,-113.8824849
12/5/2016,Gas Scrubber,,,,,,Dehy is froze. Contacted WFS. ,user_50,asset_379,48.06153418,-103.4718774
8/2/2018,Separator,Choke Valve/Loop,,,,Trash,"Unit went down on low unit pressure. Opened up bypass, but it wouldn't flow over 300. Acting like I had a freeze in Hi/Lo, thawed on it. It did help a little, but still couldn't get a good flow. Removed Hi/Lo trim set, looked good. Reinstalled, flowed backwards to try and break in freezes, wouldn't do that part of the time. Continued troubleshooting, sounded like something in the choke loop. Finally removed Hi/Lo trim again. Found the stem in 2 pieces. Reinstalled bonnet with top part of trim cage installed. Opened KF valve and flowed the loop through thinking if there was something in the loop, at least now it is in the separator. Reinstalled trim set and RTP'd well. This trim set was not that old, the last 3 or 4 months I replaced it. Will need to monitor.",user_55,asset_647,48.1573536,-103.621648
1/13/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"Liquid loaded, vent required, optimizer tried to get it back yesterday",user_84,asset_738,48.02054207,-103.5150934
1/13/2018,Gas Scrubber Separator,ESD,,,,,call out well shutting in-shut in on valve fault low unit psi-rtp/boc,user_131,asset_231,40.7126799,-114.1193569
1/27/2019,Wellhead,Tubing,,,,,"drained flare scrubber and RTP well, engineering ordered 75 gal of foamer today and well is bringing up lots of foam and its getting carried to scrubber pot, well logged off an hour later, i had covenant tech vent well to pit.. well is unloading lots of foam got unloaded enough to flow and sent back to sales.",user_37,asset_705,43.56424,-91.351691
1/13/2018,Gas Scrubber Separator,ESD,,,,,call out well shutting in-shut in on low wet gas-caught it remotely-rtp,user_131,asset_1180,40.7126799,-114.1193569
3/15/2018,Flare System,Flare Header,BMS,,,,Issue: Called out SCC alarm. but all look to be running Root Cause: found SCC # 4 pilot was out but the mains were still burning making it look like it was running. Fix: cleaned out the pilot tip and relight returned to service ,user_136,asset_857,48.0614644,-104.8417043
4/9/2018,Compressor,Cooler,,,,,"Issue: called out compressor down alarm Root Cause: Human Error, found the side door open and all insulation pulled out of the cooler. The insulation needs to be put back in or at least half of the cooler until way warmer weather Fix: had to break cooler freeze and thaw out the rest then returned to service ",user_136,asset_1914,48.1470144,-103.6180489
5/12/2018,Pumping Unit,Engine,Fuel Gas Supply,Cummins,,Human Error,pumping unit went down due to the regulator on the fuel gas supply being set at to low of a pressure. turned fuel gas up to 8psi. and restarted pump jack,user_172,asset_1083,48.1470144,-103.6180489
8/16/2018,Gas Scrubber Separator,ESD,,,,,"ARROW PLUS TL asked me to check location and see why it lost unit pressure, found condo dump stuck open. gauged before RTP found water tank at 16-0x5-5 deferring back to ops to RTP tomorrow",user_37,asset_166,48.224585,-103.8291059
12/29/2018,Fuel Gas/Start Gas,Regulator,,,,,THE FUEL SUPPLY LINES FROM THE TOP OF THE VESSEL TO THE BIG JOE NEED TO BE RE-ROUTED THROUGH THE GLYCHOL BATH ON EACH SEPARATOR *** THE BIG JOE REGULATORS KEEP FREEZING UP IN THESE COLD TEMPERATURES,user_34,asset_764,48.1491616,-103.6224672
6/4/2018,Compressor - Gas Lift,Compressor,Panel,Compressco,,Electrical Short,"Hi temp, left doors open",user_86,asset_387,,
3/25/2018,Fuel Gas/Start Gas,Coalescer/Filter,Level Controller,,,,Desi full Cabinet “C” scrubber ball checked,user_111,asset_1363,48.03773243,-103.3448334
11/18/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,"call out for gl compressor down, found it down on high discharge , blew down & drained everything, started it to warm up , let it thaw out, rtp done walk through , pumps running but bath temps low, adjusted,man cold as hell in these buildings!!!!!!!!!!!! we need some heaters installed!!!!!!!!!!!!",user_131,asset_1350,40.7126799,-114.1193569
1/15/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,after equalizing well i paused flowing and got plunger to surface. inspected and changed out worn dual pad with new dual pad,user_11,asset_1885,48.1470144,-103.6180489
4/26/2017,Separator,Dump Line,,,,Freezing,Flow line had freeze ,user_7,asset_1967,47.97855095,-103.5435702
8/18/2017,Instrumentation,End Device,Durag,,,Wildlife/Livestock, 6. Creston 3-10 Pad - Bath A durag wiring damaged by Cows • Wiring is intact • Metallic flex is broken • I removed damaged metallic flex and installed new metallic flex • Durag not powering up after flex repair • I found a blown fuse for Bath A durag and ignitor • Replaced blown fuse • Found Flame on signal not coming into HMI • Found blown fuse for flame on signal in PLC • Replaced blown fuse Verified Durag now working correctly back to HMI,user_92,asset_386,48.3619066,-103.2129855
4/16/2019,Pipeline/Piping,Pipe/Components,,,,Human Error,Sat. wells are a failure and need equipment on location!!!!!!!!!!,user_63,asset_38,,
4/8/2018,Instrumentation,Communication Card,,,,,Locked meter,user_86,asset_2116,,
8/10/2019,Instrument Air,Compressor,Instrument Gas Supply,Compressco,,Trash,Air compressors for instrument air are down again. They continue to over heat on a weekly basis. Spoke with Bob fox and he has not performed a PM on these compressors in awhile. We need to get him out here so he can further troubleshoot the dryer and air compressors ,user_120,asset_76,,
12/20/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Desi and fuel gas scrubber of liquids daily routine auto dump may be a solution to issue ,user_48,asset_1785,48.32663169,-103.6563524
1/21/2019,Instrumentation,Switch,,,,,glycol pump keeps going down and needs fixed. WM entered,user_63,asset_0,,
1/2/2019,Separator,Liquid Dumps,Seat/Ball/Piston,Norriseal,,Freezing,"water and condo dumps frozen, probably from burner being out",user_31,asset_1477,48.1475232,-103.6200096
1/31/2019,Separator,Fuel Supply System,Regulator,,,freeze," Kalter and I walked down location and found the fuel gas to the line heater frozen with the line heater down which took down the heat trace on the location and caused all the water dumps on the location to freeze . Used thaw tube on the truck and BP heater on all above ground pipping on the water dump lines to break freezes. Water dump was frozen from the unit all the way to the check valve at the water tanks. Finally got all dumps free from the production unit to the tanks clear. Got fuel gas to the line heater thawed out and started the heat trace system. Contacted Team Leader and eng. (Avery) was instructed to flow well through one unit, watched dumps on unit to make sure they would keep up and everything looked good. Then started troubleshooting the compressor on location found the water dump frozen from the compressor to the main water dump thawed and cleared line . Tried starting compressor and discovered the batteries were dead, these looked to be new batteries for the compressor / contacted Avery about possible battery issue after finding out that they were only 2 week old batteries. Got snow removed from compressor building so that we could jump the batteries , after charging we restarted compressor and loaded set rpms to 1300/ informed Avery of the set points. Rpt'd well and compressor.",user_10,asset_1600,40.5262342,-113.8824849
12/27/2017,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,"Issue: Called out for well shut in alarm. Root Cause: well shut in on low unit pressure from all the wells being in off cycles at the same time. When all the wells are off at the same the pumps, burners, SCC's use up all the unit pressure and then it shuts in on low unit pressure Fix: cycles need adjusted so that all wells are not off at the same time. left one well flowing to keep pad pressured up. Long Term: needs buy back put into service ",user_136,asset_1838,48.2525001,-102.948456
4/6/2019,Pipeline/Piping,Valves,,,,End Of Design Life,10K cyclonic was leaking to atmosphere and got replaced for 5K balon ,user_28,asset_1570,48.153479,-103.6394512
1/15/2018,Flare System,Flare Header,Regulator,,,,"Keep losing scc’s maintenance is doing work an has the heat trace locked out , got scc to relight but they will go back down with out heat trace ",user_122,asset_1323,48.35541452,-103.7502311
12/1/2017,Plunger System,Plunger,Plunger,PCS,,Corrosion,,user_126,asset_165,,
1/4/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,waiting on vendor to deliver methanol ,user_53,asset_1732,40.7126799,-114.1193569
10/3/2019,Sales Valve (PV),Pneumatic Control System (3Pgra),,,,,found supply regulator to d4 had been backed off to the point where d4 couldnt function. adjusted supply pressure and closed valve that was stuck open. vented well to unload,user_17,asset_2211,,
4/10/2018,Automation,Radio,Wiring,Bluewave,,Unknown,This is for a Phoenix Contacts 5-port network switch. Unknown failure cause. WHAT IS THE POINT OF THE DROPDOWNS IF THEY CAN'T BE ACCURATE? DOES ANYONE FUCKING READ THIS? I'M REALLY SICK OF MAKING THIS POINT!!! ,user_134,asset_780,48.1470144,-103.6180489
12/1/2017,Separator,Dump Line,,,,Corrosion,90 degree elbow washed out on water dump line. loto blew down and replaced,user_87,asset_1272,40.5262342,-113.8824849
3/8/2019,Heater Treater,Burner,BMS,,,Freezing,"line heater at satellite freezing in scrubber and supply to burner, flooding out, wo in to insulate instruments",user_64,asset_1257,39.2506642,-92.4357879
12/14/2017,Fuel Gas/Start Gas,Coalescer/Filter,Level Controller,,,,Drained desi dryer.,user_62,asset_2138,48.1470144,-103.6180489
1/31/2017,Gas Scrubber,Back Pressure Valve,Body,Other,Other,Other,"Thaw supply lines to scc, relight",user_87,asset_1736,47.99285605,-103.4439186
3/18/2019,Surface Location,Well Pad,,,,Weather,needs plowed ,user_56,asset_1240,48.224585,-103.8291059
2/10/2018,Tanks/Pits,Flare/Combuster,,,,,Flare blew out from the high winds. Drained fuel gas relit flare ,user_172,asset_2046,,
5/6/2018,Separator,Choke Valve/Loop,,,,Freezing,Broke and rtp’d ,user_86,asset_2229,,
4/2/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,kicked well on paused and got plunger to come in. called optimizer and got cycles resumed,user_11,asset_667,40.7126799,-114.1193569
12/8/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,completions team were done putting new tubing in and needed well RTP. started at 11:30,user_71,asset_261,48.1470144,-103.6180489
8/12/2019,Plunger System,Plunger,Plunger,Well Master,,Corrosion,Changed plunger and inspected lubricator.,user_153,asset_669,48.2022663,-103.5987872
3/15/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,corrosion,High low bonnet is bad needs replace will replace tomorrow ,user_46,asset_503,48.0614644,-104.8417043
8/21/2018,Wellhead,Tubing,,,,,Loaded,user_94,asset_1664,,
12/25/2017,Recirc Pump,Pump,Check Valve,Sunpumper,HBT2,Freezing,"Line heater glycol pump for the 70, 80, 110 and 140 wells fuel gas was frozen. Thawed and RTP'd pump. ",user_41,asset_2256,48.22144702,-103.56405
2/28/2019,Automation,RTU,CPU,Emerson,Scadapack P4A,Loose Connection,"well was in INT lock MVT COMM Fail, this happens alot on this pad. cleared alarm and well started flowing , ",user_144,asset_995,39.5516576,-92.4788896
8/3/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_2012,48.1470144,-103.6180489
11/25/2017,Separator,Choke Valve/Loop,,,,Corrosion,Choke was not closing all the way,user_150,asset_171,48.0568262,-104.9072345
10/28/2018,Flare System,Flare Header,BMS,,,,Found 2 SCCs out on location. Both lit remotely and are back in service.,user_55,asset_1208,,
1/17/2018,Tanks/Pits,Tank Level,Sensing Cable,,,Weather,"alarm log tank level alarm-no call out no live reads-verified it is false, reset shut in rtp well ",user_131,asset_1558,40.7126799,-114.1193569
12/25/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_101,48.1603927,-103.6171977
10/14/2019,Instrumentation,End Device,Thermocouple,,,End Of Useful Life,"Replaced thermocouple and cleaned orifice, re-lit pilot and verified operations in RTU. Verified operation with optimizer.",user_44,asset_983,46.2356189,-100.6010498
10/7/2018,Separator,Liquid Level Control,,,,,"water dump was leaking through. Set too low, adjusted controller",user_31,asset_1405,43.252261,-115.0567324
12/7/2017,Gas Scrubber Separator,Dump Line,,,,Freezing,stopped in to drain scrubbers onsite,user_71,asset_1213,48.1470144,-103.6180489
3/23/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,fluid,While I was letting compressor warm up went over and drained dezy. Dezy probably had around 10 gallons in it. Temps looked good around 63 degrees on dezy. Both baths lit on units,user_172,asset_1124,,
4/12/2018,Fuel Gas/Start Gas,Regulator,,,,,"h/low shut, tubing had a freeze I blew out and RTP well",user_88,asset_1948,48.2629592,-102.8997155
2/1/2019,Gas Scrubber Separator,PSV,Piping,,,Incorrect Set Point,the fuel gas to both quad paks are interconnected. the valves on the fuel gas system from the hot pass and from the wells were misaligned causing the scrubber to overpressure and lift the PSV. I put all the valves in the correct positions and the PSV pressure returned to normal,user_22,asset_2146,46.2356189,-100.6010498
10/13/2018,Instrumentation,Meter,Orifice Plate,Nuflo,Wonder Card RS232,Weather,"Looking at graphs, found well showing false flow. Drained liquids out of meter run, validated no flow showing now when well shuts in. ",user_15,asset_1758,48.2814817,-102.8554293
4/11/2017,Gas Scrubber,Shell,Other,Other,Other,Other,NO DAMAGES FIXED ON SITE,user_119,asset_1496,48.2774223,-102.8789555
1/19/2018,Automation,RTU,Board,ABB,Bristol 3310,Electrical Short,Cg 36-pad high tank alarm. False alarm highest tank 10-3. HMI showing tank 1 at 19-0ft. ,user_71,asset_2191,48.1470144,-103.6180489
8/31/2017,Pipeline/Piping,Pipe/Components,,,,End Of Design Life,Reinsulated and retapped pipe insulation. ,user_41,asset_259,48.19712391,-103.5577815
8/31/2018,Wellhead,Manual Valve,Stem/Seat,,,Erosion,WELLHEAD GATE VALVES WERE LEAKING BADLY OUT OF THE STEM AREA. INSTALLED PACING UNTIL THE LEAKS STOPPED. MORE PACKING WILL NEED TO BE INSTALLED AS THE VALVE IS USED,user_34,asset_425,48.1470144,-103.6180489
4/12/2018,Compressor,Motor,Switch Gear,,,,oil level control switch had vibrated loose and control arm fell off. Robert with JW Power corrected the problem and RTP'd the compressor,user_167,asset_2089,47.9648549,-105.0939328
10/27/2017,Wellhead,Tubing,,,,,"Freeze broken, well rtp'd",user_141,asset_2244,48.1470144,-103.6180489
3/31/2017,Wellhead,Primary Choke,Stem/Seat,Other,Other,Erosion,damaged or cracked seat,user_154,asset_545,48.224585,-103.8291059
2/16/2018,Separator,Temp Control System,Electrical,,,,"Pad was down on COMM ERROR. Contacted automation, they reset the PLC remotely. They stated the Radio card is going bad and have one on order. It should be in next week. Until the card comes in and gets installed, power cycling the PLC resets the COMM ERROR for a few days and we can run the pad. RTP well on plunger cycles. Restarted Bath A.",user_62,asset_2222,48.1470144,-103.6180489
12/9/2016,Automation,,,,,,Cyclonic actuator would not respond to commands properly because the open and close command wires were swapped. I corrected the wiring and verified operation.,user_134,asset_1438,48.1582527,-103.6168321
11/11/2017,Separator,Choke Valve/Loop,,,,Freezing,"Found choke had a freeze in it. Closed KF valve and opened vent line. Blew pressure off between valve and choke. Opened choke, freeze broke. Returned well to production. Tubing and casing had around 1300 psi on it. It caused gas lift compressor to go down on High Discharge Pressure. Opened choke to around 20% and let it flow to lower pressures. Got pressures down to below 1000 psi and restarted compressor. Will watch throughout the day. RTP'd well and compressor.",user_141,asset_1264,48.1469003,-103.6177299
5/9/2017,Separator,Choke Valve/Loop,,,,Freezing,"light burners, clear choke",user_39,asset_260,40.5960545,-113.9323891
4/11/2019,Separator,Choke Valve/Loop,,,,Freezing,"Well had been shut in for winter/ completed checklist . Found the fuel gas line to the choke and the esd frozen and full of fluid , thawed supply line and drained all fluids from the fuel gas supply system. Function tested esd and choke before opening wellhead valve . After pressuring up the flowline found that there was a freeze between the esd and choke , thawed and broke freeze .Checked dumps and heat trace system then rtp'd well, plunger making arrivals contacted optimizer to review cycles.",user_10,asset_330,40.5262342,-113.8824849
3/16/2017,Gas Scrubber,Other,Other,Other,Other,Other,"Burer was out, found the pilot tip plugged up. Cleaned out pilot and relit burner.",user_62,asset_1815,48.3619066,-103.2129855
1/16/2018,Gas Scrubber Separator,ESD,,,,,"call out 1st of shift wells shutting in valve fault-woudn't open remotely, had to go there found scrubber ball checked and full of liquids, drained everything & reset, drained desi,rtp wells,relit bath b and scc's ",user_131,asset_536,40.7126799,-114.1193569
3/16/2018,Flare System,Flare Header,BMS,,,,Issue: SCC (A) down Root Cause: fuel gas on the separator ball checked again Fix: once got the location back on relight and returned to service,user_136,asset_1600,48.2594738,-102.9011108
8/28/2017,Wellhead,Wellhead Piping,,,,,Casing KF Valve Bad replaced with New Balon 5000 PSI,user_119,asset_1023,48.3619066,-103.2129855
11/30/2017,Separator,Choke Valve/Loop,,,,Corrosion,Suspected corrosion on stem through packing but as cause. Choke will still need tear down after replacement. Dispatch to location. Shut ESD to begin troubleshoot on auto choke. Send close command. Appears to actuate closed. Send open commmand. Choke makes a popping sound after stalling while opening. Check gas pressures to controller. Good. Check for fluid in controller. Non present. Send shut command to choke. Does not close fully. Tap on actuator to finish closing choke. Able to get stem to seat. Send open command. Same results as before with stall then pop sound before opening. Then not fully closing after. Send WM to maintenance team to repair auto choke. ,user_75,asset_1168,,
1/20/2019,Fuel Gas/Start Gas,Regulator,,,,,"Main burner was out when i got to location. Dumps frozen, seperator may be frozen. Got main burner kicked on, T-12 was set extremely high which is why burner went out, it did the same thing to me re-adjusted t-12 and burner is shutting off at 105 degrees. Unit is up and warming. There was also a choke freeze that wouldn't allow choke to shut all the way, loading well up, when that warmed up it closed all the way and is building pressure. Tomorrow this unit should be ready to go. I will code to ops to kick on after checking dumps and unit.",user_106,asset_1103,48.1470144,-103.6180489
1/4/2019,Separator,Temp Control System,Pilot,,,,"pilot was plugged from liquid, cleaned out and drained scrubber",user_31,asset_2135,48.257296,-102.8647072
4/2/2018,Separator,ESD Valve,Actuator,,,Fouling,checked choke and it is holding. i did noticed that the esd is starting to leak out of the bottom weep hole internal diaphram is starting to fail. got esd to open and started cycles,user_11,asset_1249,40.7126799,-114.1193569
4/18/2018,Pipeline/Piping,Pipe/Components,,,,hydrate,Found hydrate occupying 50% of flow line upstream of meter orifice plate. Allowed hydrate to thaw and clear.,user_99,asset_1707,48.1470144,-103.6180489
12/12/2017,Wellhead,Wellhead Piping,,,,,Flowline has a hydrate in it ,user_102,asset_1444,48.08647382,-103.6601323
12/17/2018,Separator,Temp Control System,Heater/Burner,,,,"burner was shut off, started burner",user_31,asset_4,48.1802912,-103.5241632
5/24/2019,Pipeline/Piping,Valves,,,,Corrosion (Internal),"Noticed there was a big difference between wellhead pressure and discharge pressure, 100+ psi. Not normal. Shut pump down and blew down discharge pressure transmitter. Had small amount of black sludge like substance. Blew it down until I got some clearer water. Restarted pump, no change. There is a 2"" valve outside of building that I had closed for LOTO. Started turning it some, pressures back to normal. ",user_55,asset_2012,,
2/20/2018,Automation,Cable,Coax,SDX 20,,Loose Connection,CG 3-30 high water tank callout. False alarm.,user_71,asset_1168,48.1470144,-103.6180489
1/24/2018,Fuel Gas/Start Gas,Regulator,,,,,"thawed on regulator to DVC for choke actuator, froze up",user_88,asset_368,48.2628414,-102.8996751
12/7/2017,Compressor,Cooler,,,,,"Compressor down on low coolant level. Contacted arch rock to top off, compressor RTP.",user_62,asset_163,48.1470144,-103.6180489
9/6/2018,Flare System,Flare Header,Regulator,,,,"relit scc, adjusted supply psi from regulator and re positioned the pilot",user_144,asset_482,48.1470144,-103.6180489
10/2/2019,Separator,Choke Valve/Loop,,,,Trash,"Pad went down on low unit pressure,this well will need a downstream valve installed to keep the pad up when running the glycol baths and pumps running. Work order was already turned in but i wrote another work order for the downstream valve. Pressured up units and functioned tested chokes and rtp'd. found that the choke on the 40 well was not responding, removed and cleaned I/P and put well back into service and function tested. Restarted all scc's and baths on location did not start pumps because of fuel gas issue.",user_10,asset_478,40.5262342,-113.8824849
3/27/2017,Instrumentation,Transmitter,3n1 MVT,Other,3095,Other,,user_13,asset_2237,48.18443384,-103.4264997
4/24/2019,Compressor - Gas Lift,Compressor,Lubricator,Ariel,,Trash,Down on low pilnlevel,user_109,asset_2046,48.37134805,-103.5209357
7/9/2018,Wellhead,Wellhead Piping,,,,hydrate,broke casing freeze in 20 well and put back into service opened casing methanol pass,user_11,asset_1707,43.252261,-115.0567324
1/10/2019,Fuel Gas/Start Gas,Regulator,,,,, SURFACE FAILURE**BIG JOE NOT HOLDING,user_34,asset_1645,43.56424,-91.351691
1/9/2017,Gas Scrubber,,,,,,"Night operator reported that the separator vessel psv was leaking out of discharge pipeing, psv inspection was requested and mercer 1100 psi 1x2 psv passed inspection and was returned back to service. ",user_112,asset_247,48.3675915,-103.5272595
5/30/2019,Wellhead,Manual Valve,Master Valve,,,Freezing,Master was not completely shut and piping between well and vessel had 1200 psi sitting on Hi Lo,user_22,asset_783,46.2356189,-100.6010498
10/25/2017,Instrumentation,Communication Card,,,,,Replaced faulty wonder card. Verified data updating in Reflections.,user_99,asset_1551,40.5262342,-113.8824849
10/10/2017,Pumping Unit,Engine,Battery,Ford,,Weather,"Engine too cold to run and battery did not have enough cranking amps to turn motor over. Jumped engine, warmed engine, and RTP'd.",user_161,asset_1789,40.7126799,-114.1193569
9/18/2019,Separator,Choke Valve/Loop,,,,Corrosion,The DVC on the automated choke was not reacting to commands. It was replaced and calibrated. There were some program other issues but have been resolved.,user_68,asset_1957,48.1470144,-103.6180489
4/2/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,fluid,Turned buy back gas off at seperator and running off vessel pressure per team lead,user_109,asset_793,48.3594972,-103.777084
3/2/2017,Wellhead,Primary Choke,Stem/Seat,Other,Other,Other,"choke was in bind causing it to stick open, found steam and seat worn, stem showed signs of damage ( pipe wrench teeth markings)",user_115,asset_1388,48.224585,-103.8291059
7/1/2018,Separator,Temp Control System,Pilot,,,,Pilot tip was plugged. Cleared debris ,user_107,asset_1906,,
7/4/2017,Separator,Liquid Level Control,,,,,sight glasses were damage/cracked. replaced and RTP well,user_39,asset_230,48.1470144,-103.6180489
11/22/2016,Chemical System,Pump,,Sub pumper,hbc1,,Screen filter clogged took out screen and put back together on meth chemical pump ,user_53,asset_1668,48.06767829,-103.3836493
8/26/2019,Instrumentation,Meter,Orifice Plate,Bristol,Wonder Card RS232,Passed Function Test,Found Issues with WFS Wonder Card; Reset- Configuration and Test thru Sams System;,user_139,asset_1613,,
3/19/2019,Wellhead,Manual Valve,Wing,,,Freezing,"upper tubing master valve froze open, due to well not flowing and weather, shut in for winter ops",user_17,asset_1594,,
3/18/2018,Fuel Gas/Start Gas,Regulator,,,,,"DVC to choke cold, gummed up did not acutate chke closed all the way, loaded well, needed vent",user_88,asset_1348,48.1470144,-103.6180489
9/26/2019,Separator,Liquid Level Control,,,,,Repaired dump controller and checked operation,user_55,asset_142,,
7/6/2017,Compressor,Compressor,Process Gas Supply,Ariel,,Trash,Too many wells on off time at the same time and compressor runs out off suction pressure ,user_122,asset_1280,48.32757877,-103.6572005
9/28/2019,Plunger System,Plunger,Plunger,IPS,,Corrosion,"Last entry showing plunger was changed 23 months ago and had a dual pad. Information was incorrect, it has a bar stock in it. Replaced due to failed inspection with a new 2 3/8 bar stock.",user_55,asset_2118,,
1/19/2018,Chemical System,Pump,Valves,Texsteam,113,Power Supply,"Thump screw to tight, opens just a little to exhaust, and started pumping, ",user_84,asset_1967,47.97860858,-103.5436531
4/5/2017,Gas Scrubber,Other,Other,Other,Other,Other,Entire pad down due to frozen supply ,user_87,asset_2086,47.96758328,-103.4471139
10/26/2019,Separator,Temp Control System,Fuel Gas Supply,,,,"glycol pump fittings broken and leaking gas when you turn pump on, got replaced parts and replaced all fittings and poly fuel gas line to the glycol pump.Function tested and restarted pump.",user_10,asset_315,40.5262342,-113.8824849
11/14/2017,Plunger System,Plunger,Catcher,Well Master,,Corrosion,,user_35,asset_1181,48.29633287,-103.4077389
12/6/2017,Chemical System,Pump,Valves,Texam,HBT2,Debris,Methonal line from tank to pump clogged,user_1,asset_763,47.92620136,-103.392969
10/9/2017,Chemical System,Pump,Packing,Texsteam,HBC1,Wear,"Meth pump lost prime, tightened packing its back in service. Will pump meth overnight and RTP 10-10",user_3,asset_1902,47.9661643,-103.4051641
7/9/2018,Wellhead,Tubing,,,,,"Frew 17-30 down on low inlet pressure, RTP remotely.",user_37,asset_1021,43.252261,-115.0567324
9/6/2017,Wellhead,Wellhead Piping,,,,,Wellhead insulation has failed and needs replaced. ,user_41,asset_1424,48.19725404,-103.7502081
7/4/2018,Wellhead,Tubing,,,,hydrate,Hydrate in tubing. Caused by no methanol. Methanol delivered. Pumping on hydrate to mitigate freeze.,user_107,asset_81,,
2/28/2018,Separator,Dump Line,,,,Freezing,"While doing walk through of location, found water dump line closed with out tag. Spoke with operator that was out here this weekend to see if they closed it. Dump line was closed because vessel was frozen and they did not want the dump to hang open when the dump line thawed. Opened valve, validated the unit and dump line was thawed. ",user_62,asset_635,48.1507625,-103.6206926
3/30/2019,Pipeline/Piping,Pipe/Components,,,,End Of Design Life,Insulation on production piping was deteriorated and needed repaired or replaced to maintain containment of heat. ,user_68,asset_2034,48.1470144,-103.6180489
9/23/2019,Separator Inlet Valve (XV),Pneumatic Control System,Hi/Lo Pressure Controller,,,,"Found the block and bleed not operating properly. Replaced with truck stock, ordered a new one. ",user_55,asset_1587,,
1/26/2019,Separator,Liquid Dumps,Controller,Nalco,,Improper Adjustment,*REPLACED TENSION SPRINGS ON TWO DUMP CONTROLLERS,user_34,asset_787,43.56424,-91.351691
2/7/2019,Chemical System,Piping,Discharge Line,,,Connections,,user_34,asset_915,48.1470144,-103.6180489
4/13/2019,Separator,Liquid Level Control,,,,,found leaking gasket on the dump controller/ replaced,user_10,asset_638,40.5262342,-113.8824849
4/19/2019,Sales Valve (PV),Pneumatic Control System (3Pgra),,,,,,user_34,asset_1297,43.56424,-91.351691
3/24/2018,Instrumentation,Transmitter,Casing Pressure,Rosemount,3051,Wiring,Cord grip was loose and wires were twisted and broken.,user_134,asset_1817,48.1470144,-103.6180489
8/22/2017,Plunger System,Plunger,Plunger,IPS,,Not Optimized,Plunger was not arriving vented plunger up and restarted cycles ,user_52,asset_1964,48.20091136,-103.5555028
11/8/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,fluid drop out and hydrates built up in supply line to scc's. was able to open to atmosphere and get hydrate to break. blew out remainder of fluids to scc's and relight both pilots. reset one durag that was not reading flame. opened both esd's. will need done periodically during periods of temp change,user_17,asset_1669,,
3/11/2018,Chemical System,Charging System,,,,,ASC solar regulator failed. Unknown cause.,user_134,asset_164,48.1470144,-103.6180489
5/16/2019,Tanks/Pits,Containment,,,,Weather,Pressure washed tanks from overflow raked soil inside berm,user_157,asset_314,46.2356189,-100.6010498
11/8/2019,Tanks/Pits,Valving/Swedges,Body,,,Corrosion,Replaced drain valve on tank and returned to service,user_21,asset_1525,46.2356189,-100.6010498
12/20/2017,Heat Medium,Pump,Seals,Sunpumper,375,Wear,"No place to pick a glycol pump so this was a HUSKY 1"" and we replaced it with a Husky 1"" re-built pump",user_119,asset_1481,48.1470144,-103.6180489
3/11/2017,SWD System,Other,Other,Other,Other,Other,,user_117,asset_1633,36.2541889,-91.2478009
3/20/2019,Wellhead,Manual Valve,Master Valve,,,Freezing,"Shut in lower Master Valve but could not get upper master to close, it is either frozen or needs greased. The tubing wings are both closed and tagged as well as the ground valve, choke and hi lo at the vessel. the piping between the well and vessel is blow down also.",user_22,asset_622,46.2356189,-100.6010498
12/9/2017,Chemical System,Pump,Plunger,Texam,HBC1,Air Locked,Graco pump. Had to bleed of supply pressure then restarted pump,user_156,asset_6,48.22342461,-103.6197422
12/25/2018,Tanks/Pits,Valving/Swedges,Body,,,Trash,"761586C both valves on tank no darts, replaced darts and seals",user_31,asset_255,43.56424,-91.351691
3/15/2018,Gas Scrubber Separator,Shell,Body,,Steel,Corrosion,Crew replaced hinge on cabinet door.,user_161,asset_923,48.2625169,-102.9396022
3/25/2018,Gas Scrubber Separator,ESD,,,,,Issue: well called out shut in alarm Root Cause: shut in for the low low bath level. Fix: once i adjusted the level i was able to bring the well back on and return to service ,user_136,asset_270,48.1470144,-103.6180489
1/8/2018,Plunger System,Plunger,Plunger,IPS,,No Liquid,Well was loaded and deferring. Surfaced plunger rtp well on plunger cycles ,user_172,asset_785,,
9/11/2017,Pipeline/Piping,Valves,,,,End Of Design Life,Replace leaking check valve in sump pump line. Check valve was allowing processed water from sump to charge pump inlet to backfeed into sump causing it to overflow if valves where left open. ,user_141,asset_2012,48.1464006,-103.6153827
1/17/2019,Instrumentation,Micro Turbine,,,,GBR Status Fault," #3 turbine down for GBR Status Fault. With the fog gone, shouldn't have this issue. Was frosting up the fronts of the GBRs causing them to overheat and trip out. Restarted turbine and loaded.",user_55,asset_1489,,
7/9/2018,Tanks/Pits,Liquid Level Control,,,,,pad down on high condo tank. checked tank levels confirmed tank levels. false. pressured up pad started cycles,user_11,asset_371,43.252261,-115.0567324
3/23/2018,Instrumentation,Transmitter,Tubing Pressure,Rosemount,2088,Calibration Issue,Issue: called out well shut in alarm (INT) bad transmitter Root Cause: One of the transmitters is going in and out shutting the well in Fix: i wrote a work order to have automation look at it. i was able to clear the alarm for now so i turned the well back on and returned to service ,user_136,asset_855,48.1470144,-103.6180489
9/27/2017,Separator,Liquid Dumps,Seat/Ball/Piston,Nalco,,Liquid,,user_27,asset_185,48.1600713,-103.617123
1/17/2019,Separator,Liquid Dumps,Float,Norriseal,,Freezing,"Coal Gulch J 50- Looks like the Hi Lo is froze up, put thaw tube on front unit assembly, open bypass on hi lo, got hi lo bypass open, thawing out choke, dumps froze open due to vessel being froze, got pilot lit and main burner, unit is mouse infested so next person might bring some killer with them, got hi lo open and operating, pumps to the tanks and wellhead are going, we either need a heater for the unit or just time with the fire and heat trace to thaw things out, got choke thawed out and operating at 1 1/2 turns open, tbg and csg both at 630 psi, left it this way to warm up. ",user_97,asset_295,40.536336,-114.0492448
11/8/2018,Instrumentation,End Device,Spa2,,,Installation Design,TUBING TRANSMITTER NOT READING CORRECTLY ** FOUND TRANSMITTER ON THE LOW SIDE OF THE TEE INSTALLATION ALLOWING LIQUIDS TO ACCUMULATE. TURNED THE FITTINGS SO THE TRANSMITTER IS ON THE HIGH SIDE AND DRAINED THE LIQUIDS OUT OF IT ALLOWING IT TO ZERO. WIRED FITTINGS TO HELP SUPPORT THE WEIGHT.,user_34,asset_704,48.224585,-103.8291059
3/13/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Forgot to kick well on after last work done. RTP'd well and return to optimizer.,user_141,asset_1683,48.1470144,-103.6180489
12/5/2017,Flare System,Flare Header,Regulator,,,,"Regulators froze , thawed out and relit scc, work order submitted to extend heat trace to scc regulators and insulation ",user_122,asset_1220,48.34937218,-103.7014665
11/3/2019,Plunger System,Plunger,Plunger,IPS,,Corrosion,"Had to vent well to get plunger in. Well was loaded. Vented in plunger, caught and removed. Inspected and failed. Replaced with 2 3/8 bar stock. RTP'd well",user_55,asset_1921,,
12/7/2017,Pipeline/Piping,Pipe/Components,,,,Human Error,Flow line had freeze operator got broke and Rtp ,user_7,asset_485,48.0219375,-103.5635975
7/29/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,"No clear reason for compressor going down. Talked with optimizer, suspect freeze at discharge valve",user_141,asset_972,40.5960545,-113.9323891
2/21/2019,Surface Location,Well Pad,,,,Weather,Turn around on location is drifted in and cannot get a truck over to equipment to vent wells and thaw. Coded for plowing. ,user_15,asset_1485,43.56424,-91.351691
2/22/2018,Flare System,Flare Knockout,Process Indicator,,,,"flair knock out pot had a high level of liquid in the sight glass , found auto dump and sandpiper pump not working , found root cause in poly line from regulator at scrubber pot to auto dump was froze. ice blockage not supplying dump with supply gas , thawed out line with thaw tube and pump begain working and pulled level down, i will enter a work management request to have heat traced line with insulation.",user_122,asset_1317,40.5481548,-114.0112915
10/9/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_2012,40.5960545,-113.9323891
11/11/2018,Compressor - Gas Lift,Engine,Coils,Ajax,,Freezing,"Found compressor down, went back in history and compressor went down on high discharge pressure, was sitting at 246lbs when i showed up. Opened unit blowdown valve and blew out a decent amount of fluid. Restarted the compressor and started to injection gas both the 10 well and the 20 well did not have hydrates in the casings on meter runs. With the fluid the was blown down and no presence of hydrates in the casings, must have had a minute hydrate in cooler and it cleared itself out once pressures EQ'd in the compressor when it went down and then i completely cleared i after i blew down the unit. ",user_25,asset_2055,,
10/25/2019,Compressor,Compressor,Process Gas Supply,Compressco,,Freezing,"pulled wells on emerson 50 was not flowing anything and it was showing compressor down shut the 50 and 130 in for a pressure build until i could get to location. arrived onsite and found compressor down. looks like its been down for awhile.found the 50 well burner out, scrubber was ball checked.drained scrubber and relit bath.turned up heat on line heater. both solar pumps are running but only one is moving heat. compressor was down on low suction. shut louvers all the way on cooler. drained suction controller.restarted compressor. put the 50 and 130 free flowing to compressor but they dont look very good ",user_120,asset_1574,40.5262342,-113.8824849
2/17/2018,Fuel Gas/Start Gas,Regulator,,,,,Fuel gas separator was ball checked again today. Has been building a lot of fluid. All dumps on location are good though. Drained scrubber and fuel gas. Re lit bath.,user_172,asset_298,,
12/5/2017,Gas Scrubber Separator,ESD,,,,,Freeze in fuel gas system which caused the esd to shut and unit to go down .Broke freeze and rtp well,user_100,asset_497,40.5262342,-113.8824849
11/12/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_101,48.1470144,-103.6180489
2/1/2018,Heat Medium,Pump,Housing,Texam,113,Air Locked,Found glycol pump had stalled out. Regulator set pressure to pump was set to 10 PSI. This is not enough to run the pump. Turned pressure up to 20 PSI and pump began to run. Walked through location and validated heat trace had no leaks and was warm all across location.,user_62,asset_779,48.1470144,-103.6180489
1/11/2019,Automation,Radio,,Cambium,Force200,Unknown, 4. Champlin 533 B 3-80 - comm failure • Found everything on location powered up • I power cycled radio and switch and radio was not connecting to the tower • I plugged into radio and I could not access webpage • Radio is failed and needs replaced • I drove to North tower and grabbed a new radio • Drove back to Ch 533 B 3-80 • Removed failed radio • Installed new radio • Configured new radio • Removed ML repeater frequency out of radio so it wouldn’t sync up there • Verified radio now connecting to Continental tower • Verified Location now updating in OE Notified operations,user_38,asset_1780,46.2356189,-100.6010498
5/14/2018,Separator,ESD Valve,Gas Sensing Line,,,Liquid Plugging,Block and bleed was plugged probably when scrubber filled with liquid. Replaced ,user_156,asset_1251,48.10275383,-103.4551165
6/13/2019,Flare System,Burner,Fire Tube,,,Corrosion,pilot plugged cleaned,user_64,asset_787,41.4332083,-112.058189
4/21/2019,SWD System,Particle Filter,Process Indicator,,,,replaced lid gaskets,user_31,asset_523,40.5262342,-113.8824849
3/29/2019,Heat Medium,Pump,Instrumentation,Texam,HBC1,Air Locked,Anaheim Automation MDC150 controller (probably) failed. Unknown cause.,user_12,asset_1999,40.5262342,-113.8824849
3/31/2018,Sand Separator,Manual Drain Valves,Body,,,Corrosion,"Drained sand can, sand was present but cannot quantify how much. drained to pit.",user_62,asset_876,48.1470144,-103.6180489
5/10/2019,Separator,Burner,Fire Tube,,,Plugging,"Found unit with no pressure and burner out. After pressuring up the unit notice that there was excessive gas blowing through the pilot. After troubleshooting the root cause found the regulator that control the the gas to the pilot with a blown diaphragm, and the gas blowing to the pilot line, about 60psi with the potential of overheating the unit just with the pilot lit. Regulator was replaced and unit and burner rtpd.",user_83,asset_1707,40.5262342,-113.8824849
10/26/2019,Gas Scrubber Separator,Dump Line,,,,Trash,Drained scrubbers Desi 35 seconds scrubbers in unit 5 seconds.,user_128,asset_886,48.3076003,-103.6410837
11/3/2019,Separator,Liquid Dumps,Supply Line,Fisher,,Freezing,pilot blew out in wind froze separator and dumps,user_97,asset_2198,46.2356189,-100.6010498
12/16/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Vented well due to being loaded. Plunger arrived, RTP'd well, started cycles, and return to optimizer.",user_141,asset_96,48.1470144,-103.6180489
5/1/2017,Automation,RTU,Relay,Schneider/Scadapack,CWM,Wear,"Cyclonic out of sync, called John Marley",user_84,asset_1289,47.85168745,-103.5420397
10/6/2017,Separator,Temp Control System,Pilot Valve,,,,"Igniter failed to light pilot, adjusted and got it to lit. ",user_3,asset_896,47.97956462,-103.4582888
6/16/2017,Dehy,WFS Issue,,,,,,user_35,asset_885,48.35770102,-103.5155193
5/8/2017,Instrumentation,Transmitter,3N1 MVT,Rosemount,4088,Recalibrated,,user_99,asset_176,40.5960545,-113.9323891
4/29/2019,Separator,ESD Valve,Gate/Seat,,,Corrosion,"On location to RTP, pad was shut in on WFS lateral freeze. All separators no pressure and cold. Opened up buy back and got burners going on 90, 100, 140, 160 wells. 160 well pilot was plugged, cleaned out and RTP. 140 well RTP, 100 well rebuilt big joe and and hi low was leaking, replaced trim set, found bonnet to be leaking left shut in until tomorrow. 90 well is frozen or super loaded. The rest of the pad needs lots of attention to RTP",user_31,asset_647,48.257296,-102.863888
4/6/2017,Gas Scrubber,Shell,Other,Other,Other,Other,Ice in valve would not allow it to open,user_41,asset_2242,48.1964889,-103.6193385
8/1/2019,Flare System,Flare/Combuster,,,,,"Found well down and loaded, walked down location found all scc's out and bleed valve on the load lines open with out bull plug. Re lit scc's and cleaned pilots , shut 1inch bleed valve and installed new bull plug.",user_10,asset_255,46.2356189,-100.6010498
4/28/2018,Separator,rupture disk,,,,premature rupture,Replaced rupture disc and RTP’d well.,user_141,asset_250,48.1002316,-103.5870123
12/22/2017,Separator,Dump Line,,,,Freezing,Found frozen dump line gylcol bath was running and pumps are on thawed and rtp well,user_100,asset_1974,48.1470144,-103.6180489
1/26/2018,Separator,Dump Line,,,,Freezing,Hammer union failure ,user_60,asset_1831,48.1470144,-103.6180489
10/17/2019,Sales Valve (PV),Sales Valve,Body,Valvcon,,End Of Useful Life,Replaced cyclonic valve on sales line and returned to service,user_21,asset_503,46.2356189,-100.6010498
9/26/2019,Compressor - Gas Lift,Compressor,Suction Controller,Copeland,,Trash,"arrived onsite and did LOTO on gas lift compressor. removed suction controller and spool piece. removed witches hat. witches hat was plugged up with debris. cleaned screen and installed witches hat back in suction line. put everything back together and pressure tested work. found no leaks. purged compressor. and reset suction controller. gas lift is running good now and injecting around 650 in both wells, went through equipment and relit bath and scc.",user_120,asset_1417,40.5262342,-113.8824849
11/21/2018,Separator,Choke Valve/Loop,,,,Freezing,Found well down /Jumped units back up and got burners going . Thawed out water dump and choke on the unit put well back into cycles plunger making arrivals.Rtp'd,user_10,asset_1742,43.252261,-115.0567324
3/23/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,fluid,Did site visit. Checked dumps. Drained scrubbers. Drain KO pots. Check pit. ,user_172,asset_1213,,
1/17/2019,Wellhead,Tubing,,,,hydrate," pulled up on location called to get a plow, walked to the wellhead and made sure all was open, tbg- 193, csg- 805, might have a freeze down hole, checked unit, no psi but looks like it didn't go down or fires went out to long ago, can't get psi passed hi lo due to by bypass being froze, broke through the snow, put thaw tube on bypass, got gas to unit and hi lo open, called Brett the optimizer and wanted to leave not flowing due to thee differential on the csg and tbg, got methanol pump on and heat trace going, fire is lit, there was something stuck in the seat of the water dump so it was leaking, tripped dump all the way open and cleared out, blow down line is clear to the tank. ",user_97,asset_1028,48.1498389,-103.6211858
5/30/2019,Automation,Cyclonic Valve,Actuator,,,Freezing,Wyolectric found gears stripped. Replaced actuator and verified functionality.,user_108,asset_871,,
9/7/2019,Separator,Liquid Level Control,,,,,"While doing winterization, I checked each separator and dump. I could hear gas leaking in the water dump controller. I pulled it apart thinking it was a bad gasket, once I got it apart I found that the dump controller manifold was broken into 2 pieces and was leaking. I replaced the dump controller manifold and function tested, working good now. ",user_15,asset_293,40.5262342,-113.8824849
9/6/2018,Separator,Liquid Dumps,Controller,Norriseal,,Improper Adjustment,"Gauged tank and found 1'4"" of water in oil tank. Checked water dump and found it was out of adjustment. Water level was out of the top sight glass. Adjusted dump and dump opened and dumped water. Watched dump for a few more minutes, and made sure it was functioning correctly. ",user_15,asset_304,48.2816521,-102.8554217
7/11/2018,Flare System,Flare Header,Instrumentation,,,,heavy rain store has took out 3 out of 4 scc's location still has water on location.,user_122,asset_1761,49.5499678,-102.9290839
4/26/2019,Separator,ESD Valve,Gate/Seat,,,Corrosion,"hi lo trim washed out, replaced",user_64,asset_727,40.5262342,-113.8824849
3/26/2019,Heater Treater,Burner,BMS,,,Plugging,"Light Line Heater, and Check T12 Controller,Adjusted T12 Controllers to achieve High Temp shutoff at 130 DegF ",user_139,asset_764,,
4/9/2017,Wellhead,Other,,Other,Other,Other,,user_179,asset_1104,47.98185782,-103.5396548
9/27/2019,Fuel Gas/Start Gas,Regulator,,,,,Big joe on fuel gas was not holding pressure causing pop off,user_20,asset_2268,46.0240507,-101.4208674
2/1/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Drained desi dryer, choke drip pot, ESD drip pot and commissioned the WFS buy back meter while on location.",user_62,asset_1599,48.1470144,-103.6180489
1/6/2019,Separator,Liquid Dumps,Seat/Ball/Piston,Norriseal,,Freezing,"water and condo dump frozen, not sure why, burner was probably out",user_31,asset_315,43.56424,-91.351691
7/20/2018,Wellhead,Tubing,,,,,"Cg 25-100 optimizer asked me to watch a cycle and open to tank if plunger stalled. Well made one arrival then I had to help in on the second cycle, let well pressure build for a couple hours and tried to cycle again and had to help plunger in again. Will probably need swab or someone to spend the day working on to get running right. ",user_37,asset_1826,48.1498846,-103.6211812
10/30/2019,Fuel Gas/Start Gas,Coalescer/Filter,Instrumentation,,,,"Found line heater fuel gas frozen at satellite site. Scrubber full of liquids and checked with 2 gallons sitting at ambient due too line heater not having a cabinet or heat trace for fuel gas components and both solar and pnuematic pumps on satellite out of commission, wm in for repairs to be made. Fuel gas supply for well comes from 17-1 host scrubber and liquids drop out. ",user_54,asset_314,40.5262342,-113.8824849
2/7/2017,Instrumentation,Transmitter,Flow,Other,Other,Other,None,user_166,asset_1784,48.04292037,-103.5056035
12/5/2017,Separator,Temp Control System,Heater/Burner,,,,Root cause not listed. Burner was not responding to call for fire from T12. Checked fuel supply. Good. Tore down burner assembly and find the nuts on the main burner at the fuel/gas mixture point all back off causing leaking preventing a good mixture and combustion causing the weak burner performance. Retighten assembly and function test. All is well in the world. Root cause - Inadequate fuel gas mixture caused by vibration backing off assembly at main burner. ,user_75,asset_293,,
11/17/2016,Chemical System,Pump,Check valve,,,Debris,Turned glycol pump on yesterday. Noticed this morning had quit. Took cover off of air valve and it was full of paraffin. Cleaned up air valve system and sprayed with a lubricant. Rtp'd pump. Will confirm that it is still running later. ,user_141,asset_1612,48.11062221,-103.6689517
12/2/2018,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,"valves on water tanks are leaking, need to be replaced",user_31,asset_1892,43.252261,-115.0567324
5/30/2018,Tanks/Pits,Liquid Level Control,,,,,"Night operator found water tank at 18’ shut well in, water has been pulled to 8’9”” well rtp’d ",user_58,asset_1197,48.32664854,-103.5840982
2/27/2018,Flare System,Flare Header,Regulator,,,,Issue: found SCC (C) down on the HMI. (INT) valve fault Root Cause: temp changes have caused more fluids to drop out in the fuel gas and start freezing in the regulators Fix: was able to relight remotely. but an operator needs to get by and drain all the regulators ,user_136,asset_1001,48.0614644,-104.8417043
1/4/2018,Separator,Choke Valve/Loop,,,,Trash,Stem appeared to be worn,user_119,asset_1826,48.1470144,-103.6180489
12/23/2018,Compressor,Compressor,Scrubber Level,Ariel,,Freezing,Issue: comp has dump line freeze Root Cause: no heat to the compressor. walked back through the glycol system and cant find out why the glycol wont got to the compressor or is ice cold by the time it gets there. Fix: location absolutely needs to get a line heater added to sight that all the glycol pumps pull from and out of the units to allow better heat trace. with this being a compressed sight raising the temps causing so many other issues. I also think we should add in the size of the location and designate one pump strictly to the desi and compressor only. the compressor and desi are an add on that wasn't part of the existing sight so maybe giving them there own pump will eliminate longer runs for colder glycol and easier to trouble shoot issues with kinked lines and allows for removal if the compressor goes away at some point. ,user_170,asset_1914,43.56424,-91.351691
1/18/2019,Heater Treater,Vessel,Fuel Gas Scrubber,,,Weather,Separator had 185 psi; blew scrubber and light burners; choke is frozen. ,user_139,asset_881,48.23974116,-103.6225879
2/7/2017,Gas Scrubber,Mechanical Dump Valve,Body,Other,Other,Corrosion,"2"" Valve leaks needs replaced",user_86,asset_1877,48.05694819,-103.5265233
10/20/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_1633,,
4/1/2018,Sales Valve (PV),Sales Valve,Body,Valvcon,,End Of Useful Life,"Seals in the stem of valve are leaking between valve body and actuator, WM done and unit is shut in atbthe well and blown down. Flag and tagged as well",user_109,asset_1959,48.2279108,-103.6247539
4/26/2019,Dehy,WFS Issue,,,,,CYCLES HELD OUT DUE TO HIGH LINE PRESSURE+,user_34,asset_206,40.5262342,-113.8824849
3/17/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Lost unit pressure due to well shutting in because false high tank. 100’ of tubing needed to install jumper to pressure separator back up. Bad design. No valves that can be used on inlet. ,user_156,asset_1675,48.38747023,-103.8410259
12/28/2017,Fuel Gas/Start Gas,Regulator,,,,,Pressured up unit,user_86,asset_142,,
9/7/2018,Compressor - Gas Lift,Compressor,Regulator,Quincy,,Trash,Issue: found comp down on the HMI Root Cause: down on hi discharge pressure. so once i restarted i checked the recycle and i was working but then it stopped and i couldn't get any gas through the regulator. Fix: pulled regulator off and found metal shavings in it keeping it from working. cleaned out the regulator verified the controller was working and returned to the comp to service ,user_170,asset_1992,49.5499678,-102.9290839
12/13/2016,Sand Separator,,,,,,Dump valves inside cabinet were shut causing the scrubber to flood . ,user_102,asset_87,48.02479169,-103.738739
12/16/2017,Tanks/Pits,Flare/Combuster,,,,,C scc. Pilot orfice was plugged with water and garabage. Cleaned out,user_156,asset_140,48.34678376,-103.6555856
7/19/2017,Gas Scrubber Separator,Dump Line,,,,Trash,Replaced 10 K Cyclonic Valve with a new one,user_119,asset_559,48.1602777,-103.6172875
12/15/2016,Automation,,,,Other,Other,,user_134,asset_1627,36.2541889,-91.2478009
11/30/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,choke DVC was hung open due to fluids in the supply gas,user_179,asset_1561,40.5262342,-113.8824849
11/24/2017,Automation,Plunger Arrival Switch,,EDI,,," 6. Champlin 226 D-8 - MSO issue • Found Cyclops set at 6 and not resetting • Adjusted Cyclops setting down to a 4 • Moved Cyclops down about 2"" on lubricator • Tested Cyclops 5 times and received 5 counts on Scada • Notified operator ",user_92,asset_141,48.1470144,-103.6180489
4/2/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,fluid,"Found and drained approximately 1/2 OZ of fluid in first scrubber on line heater. This is due to warm temperatures of fuel gas upstream (well flows at 120F) and the end devices (line heater scrubber) sitting at ambient temp (47 F). ENG to further trouble shoot and supply plan forward. There is a shut in sivals unit onsite that does not appear to be doing anything, we could utilize it as a fuel gas scrubber.",user_6,asset_1675,36.2541889,-91.2478009
3/6/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Plunger not arriving: Bled down well head and found plunger frozen in the lubricator. After flow needed to unload the well keeps plunger in lubricator long enough to hydrate into the upper flow path. Found glycol circulating (80 F return from wellhead) but found methanol shut in with no tags. RTP'ed pump and checked methanol storage tank and found it 3/4 full. Adjusted rate and confirmed pump functionality. Methanol should remediate hydrate during after flow and allow the plunger free movement. Pulled plunger and inspected, plunger failed inspection due to out of Specc conditions from wear. Replaced plunger and RTP'ed well.",user_6,asset_873,36.2541889,-91.2478009
3/26/2018,Wellhead,Tubing,,,,hydrate,"Issue: found well was a no flow Root Cause: found the well head froze off and i could not move any of the well head valves. The well just came back on yesterday and it had a freeze in the well head that did not thaw out and the gas rate across it caused it to finish freezing off. Fix: I used my thaw tube to get one of the flow paths open on the well head to get gas to the unit. once i got the unit warmed up and had my exhaust running on the well head i started flowing the well using my exhaust to keep it open and the well flowing. once i got the well on and stable i started opening the choke up more, when i got fluid coming up i was able to use the heat of the well and get the rest of the well head thawed out and all the freeze broke free. During this process i had to manually move the choke back and forth the hole time keeping the hydrate moving threw the unit and to keep the well from stacking up behind the choke. that's when the second problem happened the well started to want to hydrate off again and i went to the unit to figure out what was going on and that's when I seen the sales cyclonic was starting to pinch the well back and slow the flow and the well started building pressure and the fluid stopped coming which caused the flow temp to drop dramatically. I throttled the well back to get the sales valve to open back up and started working the choke back open again and that is what I figured happened yesterday and caused the well to freeze off so solid in the well head. The well is now flowing stable and doing good ",user_136,asset_1817,48.2608832,-102.8985072
3/20/2019,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Vented 40 min,user_94,asset_2069,48.113936,-104.12136
2/23/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Used well for sacrifice when pad lost pressure. Vented well and surfaced plunger, rtp and turned over to optimizer ",user_35,asset_31,48.18292124,-103.5377478
4/6/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"line pressure spike, loaded ,vented RTP",user_88,asset_1469,48.2628959,-102.8996592
10/6/2019,Plunger System,Plunger,MSO,PCS,,Corrosion,"plunger will not surface, attempted to flow and vent and would not come in or unload, casing dropped a few pounds, turned over to engineering for further evaluation this well has had a lot of time spent on it.",user_106,asset_770,40.5262342,-113.8824849
6/17/2019,Automation,Wire,,,,,MTL 7787 intinsically safe barrier failed. Unknown cause,user_12,asset_827,40.5262342,-113.8824849
7/22/2017,Flare System,Flare Header,Process Indicator,,,,SCCs out probably due to weather ,user_156,asset_2256,48.22113413,-103.5643292
11/14/2016,Wellhead,Primary Choke,,,,,"Found deny choke pinched back far enough to stop plunger from arriving, seht has 1.5""plate was pinched back only to allow 30DP through it, opened it up and watched tonmake sure sales line valve would control Over ranges, plunger also started to come in",user_115,asset_1791,48.28520623,-102.8585177
4/25/2018,Separator,Choke Valve/Loop,,,,Trash,"Choke was sticking open still after being rebuilt last week. Isolated well head sales dump buy back and fuel gas. Bled down sales,unit.”, flowline. Pulled choke and seat out. Found the wrong choke seat in the yoko choke. Also found some shards of metal cleaned choke out. Replace seat,stem and packing. Waiting on automation to calibrate before rtp",user_172,asset_1103,,
11/4/2019,Tanks/Pits,Shell,Body,,Steel,Corrosion,"went to location to check tank levels, condo tank #770047 at 17-5x1-2, was checking location and noticed water tank #770045 had a small puddle bubbling and a soft spot right next to the inner side of the tank isolated tank and called ibex to bottom tank notified Colten and Henry",user_37,asset_648,43.56424,-91.351691
1/24/2018,Compressor,Compressor (Recip),Scrubber Level,,,,"Down on high scrubber level due to glycol pumps failing. WO was submitted, Maintenance team and crew replaced pumps 24JAN18. RTP'd compressor ",user_53,asset_1744,40.7126799,-114.1193569
1/7/2019,Fuel Gas/Start Gas,Regulator,,,,,Colder temperatures causing fluids to fall out out of gas stream. Scrubber for fuel gas and all the regulators had fluid in them. Manually drained,user_147,asset_425,,
4/6/2018,Fuel Gas/Start Gas,Regulator,,,,,Fuel gas for the pilot line on line heater froze. Thawed on regulator and catch pot. Hot line clear and relit bath,user_172,asset_876,,
3/1/2019,Wellhead,Wellhead Piping,,,,hydrate,"Found valves shut at well head. Well had a tag on it, but couldn't read it. Jumped pad online. Contacted WFS hand to see if he would have time to come by and open up dehy.Ready steamers here to thaw dumps. Got separator pressured up. After thawing on dump lines, dumps working and clear. WFS hand showed up, opened dehy. Well was frozen in well head. Had steamers thaw it out. Got it open, looked at graph again and realized I had looked at the wrong one. Well hasn't flowed in over 515 days. Contacted optimizer. He will code back to engineering. ",user_55,asset_529,,
10/13/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_55,asset_1489,,
11/24/2017,Compressor,Compressor (Intergral),Scrubber Level,,,,comp down on high suction scrubber level 2nd time in 2 days adjusted dump RTP.,user_71,asset_1159,48.1470144,-103.6180489
9/23/2019,Plunger System,Plunger,Plunger,PCS,,Corrosion,"replaced plunger, came in on cycle no issues, RTP on cycles",user_106,asset_147,40.5262342,-113.8824849
10/18/2018,Separator,ESD Valve,Gas Supply Line,,,Calibration,Found the location down because we lost sufficient unit pressure to keep the ESD's open. Found the issue to be caused by the pumps and burners using all the fuel gas while the wells were in end cycle. Jumpered the units back on and RTP'd the wells. Paused the 110 on to keep sufficient gas to the units during end cycle,user_59,asset_1962,48.0703918,-104.8832854
5/11/2018,Pumping Unit,Engine,Emissions Control,Ford,,Wear,Replaced air filter on pumping unit engine & RTP'd.,user_161,asset_1644,48.267245,-102.9231841
5/3/2019,Tanks/Pits,Tank Level,Sonar,,,Calibration Issue,"well had 3800 psi and was shut in for winter ops. vented well to tank until pressures were low enough to split flow through unit. plunger came in while venting pulled 2 3/8 bypass out of well.pressured up unit and got burner and pumps going. cyclonic was shut and had an alarm for high tank, checked tank levels all of them were low. was unable to clear alarm. shut well back in. sent work request to automation. auto tech came out and replaced barrier. got cyclonic open and brought well back. line pack jumped up to 580. shut down again and contacted williams. williams came out and attempted to break lateral freeze,but we were unsuccessful. shut well back in at wellhead. williams left lateral open to atmosphere and locked out. this is lease holder well that needs to be rtp",user_120,asset_1300,40.5262342,-113.8824849
9/6/2017,Tanks/Pits,Valving/Swedges,Body,,,Corrosion,"2"" drain valve cap on the condo tank is rusted in and can't be remove. Attempt to remove cap from valve turns valve out of tank. ",user_41,asset_48,48.19405823,-103.7559323
5/11/2019,Separator,Transmitter,Tubing Pressure,Rosemount,1151,Weather,Found tubing transmitter froze and full of fluid,user_18,asset_1308,,
12/5/2017,Compressor,Compressor,Dump Valve,Ariel,,Freezing,"Found dump valve froze, found heat trace not working, swapped valves and heat trace is warming up the dumps ",user_122,asset_226,48.37025808,-103.8094127
3/15/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"well is loaded, due to burners and pumps vented and RTP",user_88,asset_150,48.2574996,-102.9118189
9/2/2018,Instrumentation,Controller,,,,,"Dispatched to well, code stated that choke hung open and loaded well up When i got to location, I pulled a graph and found that the well was cycling plunger was making arrivals. Looked over the choke and DVC pressures look good, no moisture in the fuel supply. Will have to engage Kelvin to see if their burp setting is active on this well and if it hung the choke open Left as is.",user_56,asset_1957,48.1470144,-103.6180489
9/27/2019,Separator,Fuel Supply System,Regulator,,,debris,"The buy back for the separator was tied in on the flow line where it dives into the ground, there are 4 separators on location. I cleaned and rebuilt Big Joe two days ago, when I turned on buy back everything pressured up fine but then the vessel would loses all pressure, initially I thought Big Joe was plugged. After troubleshooting some more I figured out that there must be a check valve in the flow line somewhere and when one of the wells is not flowing the vessel uses all the gas in the line up to the check. to remedy I tied the buy back in just down stream of the separator on the 140 well just before it goes to the automated sales valve, working good now.",user_22,asset_900,46.2356189,-100.6010498
11/15/2017,Separator,Temp Control System,Pilot,,,,"Burner was out, pilot and main burner ESD was shut with no interlock to show why. Re-lit burner.",user_62,asset_703,48.1470144,-103.6180489
11/9/2017,Chemical System,Pump,Diaphragm Gears,Sunpumper,HBT2,Air Locked,Pump stalled disconnected air and got pump back up and running,user_101,asset_575,48.0614644,-104.8417043
2/27/2018,Fuel Gas/Start Gas,Coalescer/Filter,Mist Pad,,,,Drain desi ,user_111,asset_559,48.03785648,-103.3446681
5/24/2018,Separator Inlet Valve (XV),Pneumatic Control System,Diaphram,,,,Need to replace washed out hi lo body,user_35,asset_1086,48.19432302,-103.5550221
4/12/2018,Gas Scrubber Separator,Dump Line,,,,Erosion,Mon 11-160 checked location drained scrubbers everything looked OK. Dropped flare pilot boom and relit pilot.,user_71,asset_261,48.1470144,-103.6180489
3/6/2017,Instrumentation,Transmitter,Other,Other,Other,Other,fuse,user_65,asset_180,48.224585,-103.8291059
10/14/2018,Tanks/Pits,Tank Level,Probe,,,Calibration Issue,CALLOUT high tank. Verified as false. ,user_31,asset_26,43.252261,-115.0567324
12/6/2016,Instrumentation,Transmitter,,,,Calibration Issue,"While completing LEL testing at #8 found AIT-3001 failed test due to high output. Re calibrated transmitter, verified and tested good. ",user_92,asset_838,48.16022809,-103.6171336
11/7/2019,Separator,PSV,Body,,,Weather,"Arrived on location to RTP well. Did a walk around to make sure the wellhead valves are open and everything looked good. Shut to choke and started opening the bypass on the high low, the high low opened and let 400 psi into the separator, went to go light the burner and the separator PSV went off at 400 psi and blew down the unit. So I stopped the job and called my team lead to see what I could do or some troubleshooting techniques to get the PSV to reseat are and I was able to get the PSV to reseat by thawing on it. Then I went about pressuring up the unit and the PSV is now holding and not leaking. Might need retested to make sure it holds at 1000 psi.",user_76,asset_994,46.2356189,-100.6010498
7/13/2018,Tanks/Pits,Flare/Combuster,,,,,"Found SCC was down. Lit SCC, it was snuffed out by heavy wind and rain yesterday evening. ",user_62,asset_1419,39.6152124,-112.9593123
11/19/2017,Heater Treater,Burner,BMS,,,Freezing,Issue: Bath 39deg Root Cause: the scrubber had fluid build up in it until it bumped the scrubber shut off float Fix: after the scrubber went down all the fuel gas froze off. I was able thaw and get the burner running and have warming up. Long term fix scrubbers need to be checked and drained more,user_136,asset_611,48.1470144,-103.6180489
11/24/2017,Separator,Choke Valve/Loop,,,,Freezing,Found the flow line between the wellhead and the Esd frozen . Took pressure off both side of the freeze and broke freeze and rtp well,user_100,asset_77,48.1470144,-103.6180489
10/10/2017,Gas Scrubber Separator,Pneumatic Dump Valve,Controller,Invalco,,Out Of Adjustment,unit lost pressure and well logged off,user_179,asset_1943,40.5960545,-113.9323891
4/3/2017,Automation,Plunger Arrival Switch,,TripMate,Other,Other,battery in mso is wearing out causing missed arrivals i am submitting a task request to automation,user_11,asset_1275,,
2/11/2019,Surface Location,Lease Road,,,,Weather,"Primary & secondary roads on pipeline RMA in area of pad drifted badly, some blown shut with 4 feet of snow on road. Blades working to plow snow off road, push snow back to build snow fences and reduce future drifting.",user_42,asset_1988,48.1082016,-103.9181984
2/21/2018,Compressor,Compressor (Recip),Dump Valve,,,,"Compressor went down on high suction scrubber level. Found that the water dump line by the desi before it goes under ground was froze. Threw my thaw tube on it. Started compressor, let it warm up. Got it up to temp and loaded compressor. Finally got water dump line from the compressor and desi cleared and drained both. Glycol pumps were going. Glycol temp at both scrubber was at 61, Glycol return temp at the desi was 41. ",user_53,asset_1914,40.5481548,-114.0112915
1/26/2019,Dehy,WFS Issue,,,,, +DEHY FROZEN ** WORKED WITH WILLIAMS TO GET THE DEHY THAWED,user_34,asset_787,43.56424,-91.351691
11/10/2018,Dehy,Fuel Gas Scrubber,Instrumentation,,,,I was asked to go to location and surface plunger I found that the dehy dump had stuck open I shut the valve and let well pressure build over night per team lead request.,user_159,asset_1181,48.1470144,-103.6180489
1/14/2018,Fuel Gas/Start Gas,Coalescer/Filter,Level Controller,,,,Drained liquid from the desi,user_156,asset_1108,48.20778016,-103.628228
2/10/2018,Compressor,Engine,Vibration Switch,Cummins,,Misalignment,JW mechanic asked me to adjust vibration switch. I adjusted sensitivity and is running now.,user_141,asset_1264,48.1470144,-103.6180489
11/16/2017,Heat Medium,Pump,O Ring,Texam,HBC1,Air Locked,Restarted air locked Glycol Pump.,user_138,asset_1820,48.14354499,-103.4127202
11/2/2017,Instrumentation,Transmitter,Tubing Pressure,ABB,1151,Temperature,Tubing transmitter was freezing up and needed insulation and heat trace,user_150,asset_1625,,
12/28/2017,Tanks/Pits,Flare/Combuster,,,,,"Relit SCC's ""A, B, C and D"". Pilots were extinguished after losing fuel gas supply pressure. Location was shut in. ",user_41,asset_1087,48.21234444,-103.639081
12/29/2016,Sand Separator,Manual Drain Valves,Body,,,Freezing,Choke had a freeze in regulator to DVC causing it not to work. Thawed regulator and DVC with thaw tube. Choke is working properly.,user_141,asset_1650,48.3619066,-103.2129855
2/2/2018,Automation,RTU,Board,ABB,Bristol 3310,Loose Connection,"whole pad down on bad transmitter, field bus card locked up needed re initialized. Ran field bit with adam sanchez and i was able to re initialize card",user_87,asset_2169,40.7126799,-114.1193569
12/18/2017,Wellhead,Tubing,,,,,"Vented well to get pressure off, swapped meth down casing. Cycles and plunger out, choke pinched. Casing still at 2000#",user_35,asset_1031,48.31195092,-103.4082502
3/24/2019,Tanks/Pits,Tank Level,Probe,,,Weather,"producing into 2 condo tanks, both over 16'2"", both with bad bottoms, swapped tanks",user_31,asset_1160,43.56424,-91.351691
3/6/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,"Found that sales line had freeze from being down for so long. Shut in at dehy and at separator, relieved psi from both ends. Added methanol and pressured back up, continued to do this until sales line freeze finally broke free. ",user_44,asset_1784,,
3/8/2019,Separator,Dump Line,,,,Freezing,frozen water dump line off the low pressure unit thawed and rtp'd,user_10,asset_2046,39.2506642,-92.4357879
2/3/2018,Wellhead,Tubing,,,,,"Freeze in flow line between well head and separator. Opened to tank and freeze broke. Plenty of methanol, got pump going and made sure all valves open to well head. RTP'd and return to optimizer.",user_141,asset_909,48.1470144,-103.6180489
4/25/2019,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,, +FUEL GAS SCRUBBER FULL OF LIQUIDS AS WELL,user_34,asset_1607,40.5262342,-113.8824849
5/18/2018,Heater Treater,Back Pressure Valve,Body,Kimray,,Improper Calibration,"When doing site walk down, i noticed the Heater treater was at 0 PSI. Oil and some water was being sent to heater treater. Found the back pressure valve was stuck open. Found shipping plug was still installed on the vent that allows the valve to open and close. This plug prevents the oil from draining out during shipping. Removed plug and valve started actuating. Set heater treater pressure to 40 PSI. Root Cause is human error. Plug was not found and removed. ",user_62,asset_796,48.0614644,-104.8417043
9/27/2018,Flare System,Flare Header,Instrumentation,,,,Issue: Arrow dispatch for SCC down Root Cause: found SCC (B) down (INT) no pilot status. when i got here i found the SCC pilot was running Fix: adjusted the thermocouple to get a better status and then relight remotely ,user_170,asset_1187,43.56424,-91.351691
1/23/2018,Instrumentation,Controller,,,,,Kelvin not optimizing to its ability on this well ,user_53,asset_1932,48.1602435,-103.6172092
1/31/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,"Fluid found in pots in front of unit. No fluid present in pots inside of cabinet. Approximately 1’ of fluid found in the desi. Root cause of failure is fuel gas temperature and liquid knock out. See full comments below Arrow dispatch for pad not visited within 8 days P3 and fed gauge P3. IO operations before dispatching as follows. Check bath temperature 84 degrees, Tanks 60 degrees with 48” of glycol. All SCC’s up and burning. All tank levels under 10’. Pull graphs on all wells. 4-30 shut in on 1/30/2018 on consecutive non-arrivals. 4-130 plunger is arriving with good DP’s, 4-150 plunger is arriving despite leaking blowdown cyclonic, Work order in for this repair. 4-100 plunger is also arriving with good DP’s. Plan to vent 4-30 in to unload liquids from consecutive non arrivals as well as to inspect the plunger. Plunger was dropped on 12/19/2017. Dispatch to location. Check pressures on the 4-30. Tbg 358 psi and csg 425 psi. Open to vent and plunger arrives in 7 minutes at 116 psi tbg and 345 psi csg. Flow for clean up. Pull PCS hollow spiral bar plunger for inspection. 1.89 top and 1.88 bottom. Passed. Inspect lubricator cap. Cap is an IPS conversion cap for 8 round lubricators. Cap was not reconfigured correctly from pacemaker operations to conventional plunger operations. Wrong puck and configure was used. Unable to re drop plunger until cap is reconfigured. Pull graphs to see if this was the root cause of the consecutive non arrivals. Graphs indicate plunger hanging in lubricator cap in flowrate and pressure drop on missed arrival cycles. Root cause of non arrivals was plunger hanging cap due to being reconfigured incorrectly. Flag and tag well head. Flag plunger and leave on steps. Notified optimizer of cycle change to optimizing intermitter. Check all scrubbers for fluid. Desi can had less than 1’ of fluid. Scrubbers and regulators in cabinet dry. Check ESD and choke kimray pots. Fluids present. Begin root cause analysis. Check temperatures of heat trace and buy back gas at take off point at dehy. Heat trace 65 degrees and fuel line 34 degrees. Root cause is not maintaining heat back to desi can to allow for fluid knock out before gas enters the separator header inside the cabinet. Gas then is heated and when it exits the front end to supply the ESD and choke the gas cools dropping fluid. Increase bath temperature to 95 degrees. Will continue to monitor performance. May need to add another pump to supply the additional heat trace needs. Choke globe valves to well heads. ",user_75,asset_1899,,
11/4/2019,Gas Scrubber Separator,Dump Line,,,,Freezing,"Drained the Dezi, drained the scrubbers, drained the drip pots, Thumbed the dumps and checked bath temp.",user_76,asset_345,46.0240507,-101.4208674
4/27/2018,Compressor,Intrumentation,,,,,"The gas lift compressor went down. The failure code flagged low oil pressure. This is normally an indication of a power failure of some type. Checked the VFD and it was faulted on over temp. The root cause was the last time the door was closed to the VFD room, it caused the thermostat to come unplugged and wasn't controlling the temperature of the room. Operator plugged the thermostat back in and secured it with tape as well as possible to prevent this from happening again. Ventilated the room by leaving the door open until the cooler turned on to start cooling the room. Operator was able to restart the compressor and return the site to injecting gas.",user_50,asset_634,48.1470144,-103.6180489
6/19/2017,Wellhead,Tubing,,,,,"well lost plunger arrivals, i found the plunger caught in the lubricator and covered in frack sand",user_24,asset_70,36.2541889,-91.2478009
9/16/2018,Automation,RTU,Io,Schneider/Scadapack,Scadapack P4A,Human Error,"Well allowed to free flow up 2 7/8 inch ""casing"" causing well to load. OPS set initial cycles, coded to ENG for review and requested plate up size to allow well to flow hard enough to unload on cycles and reduce risk of upstream cyclonic freezing due to restricting flow to meet DP requirements at beginning of cycle. ",user_54,asset_1231,36.2543776,-91.268112
8/1/2019,Tanks/Pits,Tank,Shell,,,Weather,"Fueled up generator. We now have 2 land sharks that are not running, both on the upper ponds. Work order written. Shut down offload, locked it with purple facility lock. Ponds are full. Will continue to monitor levels.",user_55,asset_1381,,
8/30/2019,Separator,Temp Control System,Thermostat,,,,Found gas supply was not correct for the T-12's. They had the glycol T-12 routed as primary and vessel as secondary. Re-Plumbed the gas supply so the vessel is primary and the glycol bath is secondary. Function tested and they are now working good. ,user_15,asset_760,46.2356189,-100.6010498
10/21/2019,Instrumentation,End Device,Thermocouple,,,End Of Useful Life,Replaced thermocouple and cleaned orifice. Re-lit pilot and verified operations in RTU and with optimizer.,user_44,asset_552,46.2356189,-100.6010498
8/25/2019,Automation,Antenna,,Bluewave,,Loose Connection,"Luman 15-20 called out on high tank, first tank was showing 17-1 on live reads. checked tanks, levels are OK. automation should look at tank levels ",user_37,asset_676,48.2712224,-102.8704416
4/10/2017,Instrumentation,Transmitter,3n1 MVT,ABB,Other,Wiring,,user_13,asset_1432,48.100771,-103.4677667
11/28/2016,Wellhead,,,,,,Tubing freezing on this well every day for the last week and is not a methanol system installed at the well head. Will enter a work request,user_60,asset_438,48.16033218,-103.6172916
4/21/2017,Wellhead,Primary Choke,Other,Other,Other,Other,Flow line froze off due to weather/ burners/pumps.,user_115,asset_1013,48.1470144,-103.6180489
4/17/2017,Instrumentation,Transmitter,3n1 MVT,Other,Other,Recalibrated,,user_113,asset_1049,48.30751194,-103.6409785
3/21/2019,Chemical System,Electrical,Battery,UPC,,Improper Installation, 10. Champlin 452 C 23-85 - Solar Methnanol pump issue • Found batteries at 6 Vdc • Found power system not wired correctly • The pump power is connected directly to the batteries and not to the load side of the prostar which allowed the batteries to be drained down and die instead of shutting off the output when battery voltage gets low • I will have to come back tomorrow to replace batteries and re-wire power system ,user_38,asset_38,46.2356189,-100.6010498
5/25/2018,Gas Scrubber Separator,ESD,,,,,LD 1-20 pad shut in on low unit pressure RTP and started cycles. remotely.,user_71,asset_486,48.1470144,-103.6180489
3/31/2018,Separator,Dump Line,,,,Freezing,Drained scrubber on green complete separator. No fluids present.,user_62,asset_2069,48.1470144,-103.6180489
1/19/2017,Gas Scrubber,Dump Line,Dump Line,Other,Other,Corrosion,Froze dump lines ,user_50,asset_557,47.9386101,-103.5042411
3/25/2018,Wellhead,Wellhead Piping,,,,hydrate,couldnt get downhole freeze to break. equalized flagged all valves used,user_11,asset_817,40.7126799,-114.1193569
10/20/2017,Compressor,Compressor (Recip),Cylinder,,,, Compressor down on Low Suction Pressure. Root cause is too many wells in the off cycle. ,user_41,asset_1761,48.20245665,-103.598746
10/11/2017,Separator Inlet Valve (XV),Pneumatic Control System,Hi/Lo Pressure Controller,,,,Optimizer closed and then opened. Works fine now,user_86,asset_239,,
1/16/2019,Separator,ESD Valve,Gas Sensing Line,,,Freezing,"Found well was froze in flow line at ESD and tubing transmitter. This was due to a flaw in the heat trace system that when it was built, it will flow to dump lines or to the well heads, but not to both. Maintenance is putting together a crew to come out and redo the piping to be able to have heat across location. For now, I used my truck to thaw out ESD and tubing transmitter. ",user_15,asset_1342,48.1499808,-103.6200096
2/22/2018,Fuel Gas/Start Gas,Regulator,,,,,"DVC froze, thawed and RTP well... there is very little to no fluid in these DVC when thawed it is a mild mist. All i can figure is that the relays are old and gummed up",user_88,asset_1642,48.2628861,-102.899611
8/22/2017,Separator,Liquid Dumps,Seat/Ball/Piston,Nalco,,Corrosion,Packing had 5 pieces of packing instead of 6,user_156,asset_45,48.18827363,-103.6596398
1/24/2018,Automation,Cable,Data Cable,SDX 20,,Electrical Short,"LSHH switch water tank 2 False high level shut pad in Faulty switch,not repairable",user_111,asset_56,48.05163348,-103.4445521
8/21/2017,Tanks/Pits,Flare/Combuster,,,,,"Found SCC ""C"" out. Went to light it and found pilot was plugged. Pulled apart pilot and found Teflon tape stuck in pilot orifice. Cleaned tip and re-lit SCC.",user_62,asset_1212,48.3619066,-103.2129855
1/12/2018,Separator,Temp Control System,Pilot,,,,Pilot plugged with trash. Cleaned out and relit burner,user_156,asset_424,48.24292012,-103.6369214
3/18/2017,SWD System,Other,Other,Other,Other,Other,,user_117,asset_2012,40.5481548,-114.0112915
4/9/2019,Automation,Radio,Wiring,Cambium,Force200,Improper Install, 7. WDW #12 - Radio issue • Found radio signal at -76 going to Lost Creek Sec. 2 • Attempted to re-align radio to luman tower • Not able to get radio to get a good enough signal to Luman or North tower • Aligned radio back to Lost Creek Sec. 1 with a -76 signal • Found flakey ethernet connection on the radio cable at the power shot • Replaced ethernet connector • Tested and verified location is no longer missing any pings • Waited onsite for operation to show up because they needed to borrow our ladder to install a gauge ,user_38,asset_523,48.0592597,-104.899174
1/5/2019,Instrumentation,Controller,,,,,I/P and Relay in Fisher DVC6000 fouled with paraffin.,user_12,asset_778,40.5262342,-113.8824849
3/13/2018,Heater Treater,Burner,BMS,,,Corrosion,Issue: found the bath was 101deg on the HMI and wells were flowing 94deg+ Root Cause: the warmer temps are allowing the baths to heat up and not expel as much heat. also can find the pilots running hard enough to heat the bath up on its own without the main burner running. Fix: turned T-12 down ,user_136,asset_1280,48.1470144,-103.6180489
4/3/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,"Casing froze off, well was not able to inject down casing.",user_95,asset_2055,48.12574748,-103.6528699
6/27/2019,Separator Inlet Valve (XV),Sales Valve,Body,Valvcon,,End Of Useful Life,The salesline cyclonic valve was leaking out the stem. It was replaced.,user_68,asset_1990,48.1603509,-103.6188541
3/14/2018,Tanks/Pits,Liquid Level Control,,,,,"False high tank level, triggered a callout.",user_95,asset_2146,48.12370804,-103.6581617
12/5/2017,Compressor,Compressor,Dump Valve,Ariel,,Freezing,"Found dump valve froze, found heat trace not working, swapped valves and heat trace is warming up the dumps ",user_122,asset_2246,48.36239941,-103.8161995
3/7/2017,Instrumentation,Other,,Other,Other,Other,cyclonic actuator,user_65,asset_1930,48.224585,-103.8291059
11/24/2017,Automation,RTU,Display,ABB,Total Flow G4,Wear,"false high tank alarm, shut in well, checked tanks and bypassed alarm RTP.",user_71,asset_1213,48.1470144,-103.6180489
2/6/2018,Fuel Gas/Start Gas,Coalescer/Filter,Level Controller,,,,"Drained desi, about 1/8 full",user_86,asset_1461,,
12/25/2017,Compressor,Engine,Fuel Gas Supply,Cummins,,Weather,"Compressor was down for Low compressor oil pressure due to cold weather. Restarted compressor, it was a rough start, but engine smoothed out. Let it come up to full operating temp and loaded. Compressor was RTP'd and back online",user_141,asset_1264,48.1603927,-103.6171977
11/9/2017,Plunger System,Plunger,Catcher,PCS,,Corrosion,greased plunger catch,user_62,asset_1882,48.1470144,-103.6180489
11/20/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash,Choke seat bad.on both chokes ,user_5,asset_1645,43.252261,-115.0567324
12/16/2017,Wellhead,ESD Valve,Actuator,,,Freezing,ESD actuator would only open about halfway. ,user_134,asset_385,48.1470144,-103.6180489
10/5/2017,Compressor,Compressor,Scrubber Level,Ariel,,Liquid Carryover,"Compressor down on high scrubber liquid level, drain scrubbers and RTP ",user_109,asset_1675,48.392614,-103.8364372
10/26/2018,Chemical System,Pump,Connecting Rod,Texam,HBC1,Air Locked, Opened up bleeder valve on pump and got a bunch of air out of it checked again and it is pumping meth again.,user_15,asset_1284,48.2815048,-102.8554716
10/30/2019,Separator,Choke Valve/Loop,,,,Freezing,"Found all well down and frozen , looks like pad was down overnight . Thawed out front end of the unit and vented wells to unload so that the unit would stay up and run. After getting all the equipment up and run I could flow the well because the automated valve on the dehy would not stay open. Contacted dehy tech to troubleshoot problem. Jumped all unit on and started glycol bath and pumps to prevent the unit from freezing until dehy problem can get fix.",user_10,asset_515,40.5262342,-113.8824849
11/10/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Plunger lost arrivals,user_84,asset_738,48.02047585,-103.5151325
10/9/2018,Wellhead,Tubing,,,,hydrate,"Well had a freeze down hole. Rocked it, on the 4th time it broke the freeze. Started methanol pump, adjusted flow rate. Big joe was also frosted over. Lit burners and observed that it was thawing out with warm gas flowing through it. ",user_55,asset_444,,
7/18/2019,SWD System,Particle Filter,Element,,,,"Walk through, took readings. Changed filter due to high differential pressure. Had some issues getting lid to seal. Had to shut pump down a couple of times to get it done. All good now.",user_55,asset_2012,,
12/12/2016,Automation,Plunger Arrival Switch,,EDI,Other,Other,No damages,user_74,asset_318,48.3241408,-103.6181788
3/10/2018,Compressor - Gas Lift,Engine,Cooler,Ajax,,Controller Failure,Bad T-12. Replaced. ,user_156,asset_1452,48.22029145,-103.5958128
2/12/2018,Compressor,Compressor,Process Gas Supply,Ariel,,Trash,Issue: Called out compressor down alarm Root Cause: all the wells were in off cycles causing the comp to run in recycle. Between the pumps using the fuel gas along with what the compressor is using it went down on low discharge Fix: left a well running ,user_136,asset_932,48.0614644,-104.8417043
2/21/2018,Sales Valve (PV),Sales Valve,Body,Valvcon,,Freezing,Freeze in sales line cyclonic.,user_95,asset_1308,48.1255521,-103.6531323
3/20/2017,Automation,Other,,Other,Other,Other,Esd not opening ,user_58,asset_570,47.9464543,-103.4255328
3/9/2018,Wellhead,Tubing,,,,,Casing freeze,user_95,asset_2055,48.12546128,-103.6530869
5/1/2019,Tanks/Pits,Flare/Combuster,,,,,"2 scc's out, probably due to wind, relit",user_31,asset_793,43.56424,-91.351691
6/8/2019,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_55,asset_523,,
4/3/2018,Compressor,Compressor (Recip),Valves,,,,"Compressor down on low discharge. Compressor recycled for too long while all the wells were on off cycles causing it to go down on low discharge. Kelvin failure. Issue has been brought up Restarted compressor, let it warm up once it was up to temp i loaded compressor. Compressor immediately went down on high suction. Suction controller is reacting slow, found gas froze from sitting down for 6 hours! Temp was also 10 degree Fahrenheit Broke out the thaw tube and thawed the kimray fuel pot. Finally was able to break freeze and blew line out. Restarted compressor again and loaded. RTP'd compressor and well ",user_53,asset_2148,48.2614528,-102.8936593
12/12/2017,Heater Treater,Burner,BMS,,,Pilot Went Out,Issue: called out burner out alarm Root Cause: burner was shut off but everything was turned back on but the burner Fix: relight the bath and got warming back up ,user_136,asset_1556,48.1470144,-103.6180489
3/9/2018,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,"This well has been down for awhile, not saying it’s because of optimization just didn’t know which one to choose. Well was down due to ops. Well had 210 on tubing 950 casing. Vented plunger to surface to unload fluids in tubing.got well cleaned up and handed over to optimizer",user_172,asset_694,,
4/1/2018,Compressor,Compressor (Recip),Valves,,,,"Got to location, whole pad was down all ESD's were shut Had to get pad back up, finally got ESD's opened lit burners Compressor was down on low discharge pressure, compressor sat there recycling for too long while all the wells were on off cycles Kelvin failure. RTP'd compressor and well ",user_53,asset_1193,48.2727581,-102.8682818
4/25/2018,Separator,Temp Control System,Flame Arrestor,,,,Found flame arrestor pounded into housing with hammer and unable to be removed for pilot supply work. Work order in to fix,user_35,asset_1123,48.25424026,-103.4321377
1/5/2017,,,,,,,"Location check, well still producing cycles, still waiting on automation and measurement issues to be taken carenof",user_35,asset_1432,48.10055006,-103.4683357
3/18/2018,Automation,RTU,Onboard Battery,Amocan Cams,Bristol 3310,Electrical Short,ESD solenoid won’t function/open valve,user_111,asset_1564,48.02430726,-103.3640568
6/9/2017,Separator,ESD Valve,Actuator,,,Corrosion,"This is not on an ESD valve, it is on the main valve for an SCC. It uses the same actuator. Internal seals failed.",user_134,asset_419,48.1586562,-103.6172961
8/25/2019,Heater Treater,Back Pressure Valve,Body,Kimray,,Trash,"found well shut in for repair by wyutex , replaced high low bypass valve 8-21-19 rtp'd well and verified by pass valved held ",user_144,asset_1066,40.5262342,-113.8824849
12/10/2018,Heat Medium,Pump,Process Indicator,Sunpumper,HBC1,Power Supply,"inside of cabinet, you can't reach lines to tell if they have flow, no way to adjust flows even if you can reach them",user_31,asset_1349,43.56424,-91.351691
3/21/2019,Tanks/Pits,Valving/Swedges,Body,,,Freezing,There is a cleanout in between the inner and outer loadline valves on the water tank that has froze and broke out.,user_68,asset_865,40.5262342,-113.8824849
12/8/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Wells shut in on low unit pressure choke controller on 100 well was filled with fluid cleared out and brought all wells back online.,user_51,asset_1423,48.1470144,-103.6180489
1/25/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,got plunger to surface. started cycles in an off,user_11,asset_1281,48.1470144,-103.6180489
11/15/2016,Tanks,Valving/Swedges,Seat/Ball/Piston,Other,Other,Corrosion,Leaks through,user_105,asset_248,47.97823877,-103.4972375
1/16/2018,Instrumentation,Transmitter,Tubing Pressure,ABB,1151,Installation Design,"Double block and bleed assembly and piping for methanol injection has Tbg transmitter excessively far from process piping and heat trace causing the transmitter to freeze. Approved remedy is to reconfigure transmitter to be on the process line near the heat trace with a single no shock needle valve. Work order will be input to reconfigure methanol injection and move transmitter. Full resolution comments below. Plunger not arriving causing liquid loading. Pull graphs to troubleshoot. Tbg transmitter appears to be freezing. Plunger appears hung in lubricator. May be a tbg freeze. Dispatch to location. Find double block and bleed assemblies on both tbg and csg transmitters. Excessive exposed piping with out heat trace. WO will be input to remedy down to single no shock set up. Blow out transmitters. Methanol present on both sides. Double check methanol operation. Methanol is pumping. Tank is full as well. Check bath temperature. 80 degrees at bath. Check heat trace at wellhead. Glycol lines at wellhead 75 degrees but process piping only 40 degrees. Find plunger catch set. Shut in master and release catch to check for plunger. Plunger falls to valve. Reset catch. Go to unit to shut high low. Find high low bypass open. Shut high low bypass. Catch plunger again and inspect. Dual pad plunger in good shape. One mark on top from fast arrival. Fish neck good. Passed inspection. Inspect lubricator cap as well. Spring not rattling, anvil in place and not pushed in. Passed inspection. Re drop plunger and wait min off time to vent in plunger to unload and restore cycles. Check pressures before vent. Tbg 350 psi and csg 536 psi. Open to vent and plunger arrives after 20 minutes at 134 psi tbg with csg 501 psi. Flow for clean up. Final flowing pressures tbg 88 psi and csg 498 psi. Unable to get jsams to work in field. Unable to reset shut in. Handover to optimizer to reset shut in and adjust cycles as needed. Also found choke pinched. Opened choke to 64/64”. ",user_75,asset_1933,,
3/24/2019,Tanks/Pits,Flare/Combuster,,,,,"1 scc out, probably due to weather, relit",user_31,asset_1160,43.56424,-91.351691
12/2/2017,Fuel Gas/Start Gas,Regulator,,,,,"while looking through pads found this 4 pack down run out of unit PSI, only 40 & 60 run this modular, so everything must have kicked on at same time& run out of gas in off cycle????? drained desi, checked pumps & heat trace/pressure & RTP wells",user_131,asset_1601,40.5262342,-113.8824849
6/4/2018,Compressor,Compressor,Suction Controller,Ariel,,Trash,Issue: Called out comp down alarm Root Cause: alarm showed hi discharge pressure. restarted and monitored it and the discharge was fine. I am starting to thing that maybe when the valves pinch down or shut the recycle isn't responding fast enough and that's why its going down on hi discharge Fix: restarted and returned to service ,user_136,asset_919,48.259471,-102.9009493
8/13/2019,Separator Inlet Valve (XV),Controller,,,,,"Closed ESD and checked choke operation. Not opening. Found the choke stem metering rod had turned and was out of pivoter on DVC. Loosened bolts and turned rod about 1/8"" and put it back in DVC pivoter. Checked choke operation, working fine. RTP'd well.",user_55,asset_202,,
4/6/2017,Gas Scrubber,Other,,Other,Other,Other,,user_179,asset_1102,47.96432087,-103.5553421
3/28/2019,Compressor - Gas Lift,Compressor,Suction Controller,Ajax,,Freezing,"After starting compressor realized csg psi was not buildimg and could not get a rate. Found that discharge line at well had a freeze, shut in and thawed. Broke freeze and opened valves back up, csg psi began to climb, began getting rates and well started to unload. ",user_44,asset_426,,
2/12/2018,Compressor,Compressor,Panel,Ariel,,Electrical Short,"Compressor went down on high 3rd stage scrubber level, code 30 , inspected all scrubbers and levels were low, opened Manuel dump on all stages an verifided that all dumps work, check heat trace and all glucose lines are hot, No issue found , if it goes down again I will have Archrock come an troubleshoot it, I will follow up with it this evening an tomorrow morning to make sure dumps are working properly before paying to have a 3 party come troubleshoot it ",user_122,asset_793,48.35914225,-103.7767302
11/19/2017,SWD System,SWD Pump,,,,Lubrication,False high shutdown. Transmitter is freezing,user_156,asset_1583,48.16507143,-103.6813544
5/22/2019,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"plunger will not come in, turning over to swab",user_106,asset_317,48.1475232,-103.6191904
1/30/2017,Wellhead,ESD Valve,Actuator,Other,Other,Liquid Plugging,DVC had liquid in it thawed out worked choke several times to drain rtp'd ,user_58,asset_270,47.95051189,-103.4212423
3/3/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_1489,40.5960545,-113.9323891
7/20/2019,Plunger System,Plunger,Catcher,Well Master,,Corrosion,Replaced seized plunger catch,user_18,asset_18,,
2/23/2018,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,Issue: Called out whole pad shut in alarm Root Cause: the whole pad shut in on low unit pressure. That is coming from the drop in temperature and the wind along with the snow is causing the burners to run much more and a lot harder using up way more fuel gas. Fix: turned the pad back on the quick fix for now is to leave one well flowing to keep the pad up and running tell the weather passes. long term fix is to install a buy back meter ,user_136,asset_1516,48.2594311,-102.9010562
1/9/2019,Fuel Gas/Start Gas,Regulator,,,,,Issue: unit (A) shut down Root Cause: found the scrubber ball checked. Drained the scrubber and followed the line back and found the fluid is coming back from Williams buy back line. Fix: really not sure why we have or are using a buy back line here the well is an Horizontal well that is a stable flow. while the well was down it looks like the lateral back filled with fluid and we were buying it back. the units also have cold fingers installed so i started pulling the fuel gas through there and shut the buy back lines at the units ,user_170,asset_2001,43.56424,-91.351691
2/19/2019,Dehy,WFS Issue,,,,,"dehy froze up, manual rodreguez, 307-320-3427, tec. ",user_77,asset_1285,40.5262342,-113.8824849
4/3/2018,Automation,Tower,Master Station,,,Service Outage,Lost comms on location had manually check tanks and cause unnecessary time to drive to location and verify levels. Automation currently working on comms issue. ,user_58,asset_1823,48.41592377,-103.576801
9/6/2018,Separator Inlet Valve (XV),Electric Control System,Actuator,,,,Found that this well had shut in on several different Interlocks. LI-1150D Transmitter Bad. Reset interlocks and opened ESD. Started cycles and lifted well. Safety Temp is showing 0.00 degrees. Well is showing flow. RTP'd well. Will write a work order for safety temp.,user_55,asset_80,,
10/26/2018,Wellhead,Manual Valve,Stem/Seat,,,Erosion,MASTER VALVES BLOWING GAS THROUGH THE STEM AREA.. SUBSTANTIAL LEAK INSTALLED STEM PACKING *** WILL NEED TO BE DONE A FEW MORE TIMES UNTIL PACKING IS SEATED BETTER,user_34,asset_564,48.1470144,-103.6180489
11/8/2016,Compressor,Compressor,,Other,,,Cow shut Williams downstream valve returned to service and valve handle was removed ,user_152,asset_169,,
1/25/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,"Dispatched to location upon arrival walked down location checked wellhead, verified separator was up, glycol bath was up and warm. Both glycol pumps working, noticed methanol pump was off, checked methanol tank and realized it was empty. Will make sure methanol is ordered. Checked dumps and found condo was froze but water was clear, Spoke with optimizer and found that plunger needs to be vented in and inspected but found that blow down valve was froze. Due to snow and deep drifts on location currently unable to get truck close enough to thaw. Will turn in request to have location bladed around surface equipment. Once snow is removed, location will need to be revisited to thaw blow down valve, vent plunger in, inspect and rtp. ",user_44,asset_2144,,
1/16/2017,Gas Scrubber,,,,,,Well shut in on low unit pressure due to bump setting not keeping up with fuel gas usage in colder temperatures. ,user_50,asset_601,47.99325461,-103.4437731
5/20/2018,SWD System,Particle Filter,Element,,,,Filters were at 4 dp. Changed filters ,user_156,asset_2188,48.37857946,-103.8550788
3/21/2018,Chemical System,Pump,O Ring,Texam,HBC1,Freezing,"pump stalled causing plunger to freeze in cap, restart pump",user_87,asset_1219,40.7126799,-114.1193569
12/20/2017,Heat Medium,Pump,Diaphragm Gears,Texam,HBC1,Wear,"Replaced one Graco 1590 1.5"" glycol pump & RTP'd.",user_161,asset_2138,40.7126799,-114.1193569
9/22/2018,Compressor,Compressor,Suction Controller,Ariel,,Trash,"comp down on lo suction found recycle valve shut , opened valve and recycle took over when suction psi got low, human error",user_144,asset_1915,48.224585,-103.8291059
1/16/2018,Heat Medium,Pump,Diaphragm Gears,Texam,HBC1,Wear,Replaced Husky 1040 glycol pump and RTP'd.,user_161,asset_1481,40.7126799,-114.1193569
10/18/2019,Instrumentation,Transmitter,Unit Pressure,Rosemount,266J,Wiring,"Upon arrival walked through location, checked dumps and scrubbers, verified burners were lit. 160 unit bath was only at 65 so turned it up about 30 degrees, bath now around 95 degrees with separator temp at 70. Checked pressures and verified no freezes, did notice that the separator pressure transmitter for the 150 well had no power, turned in WM for repair. Verified psi on separator with analog gauge and hi/lo bumping open, pulled graphs on both wells, found the 160 was doing great but the 150 had been shut in since 10/10/19. Spoke with optimizer had found that the criteria for cycles used separator psi and it shut in because the transmitter does not have power. Optimizer switched from separator transmitter to tbg transmitter and was able to reset cycles and kick well off. Once transmitter is repaired the criteria can be changed back, no further action needed at this time.",user_177,asset_1960,40.5262342,-113.8824849
4/16/2019,Plunger System,Plunger,Plunger,IPS,,Not Optimized,Dispatched to pad due to compressor going down Got to pad and found that the compressor went down on low 2nd stage pressure Got Compressor started and warmed up then got it loaded. This 70 well is loaded and needs a vent TBG had 350 CSG had 605 Vented well for 10 mins and got plunger to come in. After the vent i found that the ESD is bad and needs replaced. WM has been submitted Put well back on cycles,user_56,asset_257,48.1470144,-103.6180489
7/27/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_55,asset_1489,48.1470144,-103.6180489
8/27/2018,Wellhead,Casing,Intermediate Casing Head Valve,,,,"This is an outside KF on the Casing, this is not a Master valve on the casing I had no way to pick another valve.",user_5,asset_1519,48.1601971,-103.6181759
2/2/2017,Instrumentation,Transmitter,Other,Other,Other,Other,Injection pump uses transmitter to auto Start/Stop ,user_65,asset_1696,48.3619066,-103.2129855
1/14/2018,Heater Treater,Burner,BMS,,,Plugging,Issue: found the line heater was 65deg on the HMI Root Cause: the kemRay shut off switch tripped Fix: rest and the burners took off,user_136,asset_457,48.2608782,-102.900126
11/16/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash,unit lost pressure and well logged off,user_179,asset_872,48.1470144,-103.6180489
5/1/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,well was missing plunger arrivals,user_179,asset_2215,48.1470144,-103.6180489
12/15/2017,Wellhead,Tubing,,,,,,user_48,asset_775,48.19819571,-103.7979273
11/16/2017,Separator,ESD Valve,Gate/Seat,,,Corrosion,"Component not listed. Cyclonic blowdown is failure. Valve still needs full tear down. LOTO for roustabouts to replace the 36-70, 80, and 150 well leaking blowdown cyclonics found to be leaking 11/14/2017. Upon completion of repair perform negative test on all three valves. 70 had 59 psi on tbg to test with. 80 had 614 psi on tbg to test with. 150 had 932 psi on tbg to test with. All valves failed negative tests. Negative test ESD and closed choke to unit by shutting all outlets for vessel, blowing vessel down and monitoring pressure on transducer at vessel. All passed aiding in identifying the cyclonic as leak off point. Work cyclonics multiple times. Perform multiple negative tests. All recorded on tbg transmitter at unit that is within the void at test area. Unable to get a passed test. Contact TL, PE, SM, and Optimizer. 20 and 50 wells ready for RTP. Jump 50 well’s ESD. Start and load compressor. Plunger arrives in 53 minutes. Suction pressure 97 psi at plunger arrival. Bypass plunger suspected of losing velocity causing valve rod to fall out and plunger to fall back to bottom. Clutched bypass needed for lower velocity wells. Moved jumper to 20 well and jump ESD. Start cycle after 50 enters afterglow after plunger arrival. Hand over to optimizer to monitor cycles. Develop plan forward for valve failures with engineering for the 70, 80, and 150 wells. ",user_75,asset_6,,
10/13/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Corrosion,Replace choke,user_173,asset_1000,48.1603191,-103.6174056
2/21/2019,Pipeline/Piping,Valves,,,,End Of Design Life,glycol pump was bad and unable to transfer heat to process. crew replace pump,user_28,asset_1249,48.160344,-103.6188275
3/13/2017,Sand Separator,Other,Other,Other,Other,Other,Dump lines freeze.,user_39,asset_1843,48.224585,-103.8291059
12/6/2016,Compressor,Engine,Fuel Gas Supply,,,Freezing,Fuel gas freezing off see comments on f160 well,user_131,asset_1774,47.88297555,-103.5120316
11/4/2016,Automation,,,,,Other,None,user_30,asset_359,47.88138848,-103.595743
3/25/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,couldnt get plunger to come in SIPB,user_11,asset_402,40.7126799,-114.1193569
3/7/2018,Automation,Cable,Data Cable,3M,,Electrical Short,"CG F-pad bath alarm both baths were stuck in pilot running status, master reset and made sure mains opened.",user_71,asset_841,48.1498331,-103.6210837
6/25/2018,Separator,ESD Valve,Gate/Seat,,,Trash,Hilo valve sand cut and leaking bye repaired on site ,user_58,asset_1915,48.37174012,-103.5206297
9/2/2019,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,"Got to site and did a walk around of location. Drained fuel pots, two of them had liquid Drained desi. Found that the 100 choke is leaking. Will submit a WM for it. Left pad as is.",user_56,asset_1914,40.5262342,-113.8824849
12/6/2017,Instrumentation,Controller,,,,,found on end cycle ,user_53,asset_1914,36.2541889,-91.2478009
8/5/2019,Instrumentation,Intrumentation,,,,,Power cycles dvc and was able to reestablish comms to it and then redownloaded the fieldbus information to it,user_16,asset_679,,
7/16/2019,Automation,Transmitter,Tubing Pressure,Rosemount,Ashcroft Pressure,Weather,went to location and was going to start walk down and inspections after well had been shut in all winter. Location has no power and all of the transmitters are dead. Could not go any further. Put a work management in for automation and will code to automation. ,user_106,asset_1879,38.4425988,-95.5406131
11/15/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Corrosion,"Found scrubber full of liquids. Found valving to desi and scrubber not in correct position. Drained desi, scrubber and lined up valves correctly to flow gas to desi then scrubber pot.",user_62,asset_726,48.1470144,-103.6180489
10/5/2018,Separator,Dump Line,,,,Corrosion,"1"" dump line with pin hole leaking, repaired",user_64,asset_960,43.56424,-91.351691
6/6/2018,Amine,Cooler/Condenser,Motor,,,,Not real. Lateral compressor start date,user_4,asset_652,36.2541889,-91.2478009
1/4/2019,Dehy,WFS Issue,,,,,"Shut sales line valves on all wells and blew down sales line from separators to dehy. After blowing down line, opened bleed at dehy and opened sales line valve on a well. Immediately started blowing out of bleed at dehy. Secured sales line valve. Closed bleed and opened sales line valves. Wells still not flowing. Freeze at the dehy. Contacted WFS operator, and advised him of my findings. He made it out there later, and was able to RTP pad. ",user_55,asset_361,,
9/6/2018,Separator,Choke Valve/Loop,,,,Trash,The choke on the front end of a yoko well with a downstream valve on it is getting stuck in manual in the program and is not switching to auto when the cycles turn on. I can force the front end choke to go into auto and cycle but sometime during the day it switches back to manual and will not open the choke. I contacted Mike Edwards about this issue and he has set a few program traps to find the root cause of the problem he thinks this could be a tag issue in the program. If someone runs into this problem again they should contact Mike Edwards to look at the choke page on HMI.,user_10,asset_28,48.1470144,-103.6180489
2/28/2018,Heater Treater,Burner,BMS,,,Pilot Went Out,Issue: found the bath was down on the HMI (INT) bath over temp Root Cause: found the T-12 turned up to hi Fix: relight bath remotely and then turned down the T-12,user_136,asset_1103,40.5481548,-114.0112915
4/4/2018,Fuel Gas/Start Gas,Regulator,,,,,"lower than normal line pressure cased units to go below low set point settings and units went down, adjusted set points and brought pad back on line, drained all location and re lit burners",user_88,asset_365,48.1470144,-103.6180489
4/21/2019,Dehy,Burner,BMS,,,Loss Of Fuel Gas,unit was shut in when i got to location tank was at 14-0x3-0 in a 15-2 tall tank. found dehi dump stuck open and blowing to water tank from lateral isolated dumpline.,user_37,asset_593,48.1470144,-103.6180489
11/16/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,"Low temps causing meter runs to hydrate off, showing high injection rates. Valves close and comp goes down on high discharge. ",user_35,asset_1812,48.19869313,-103.4827618
2/16/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Vented well due to being loaded. Plunger arrived, RTP'd well, started cycles, and return to optimizer.",user_141,asset_1517,48.1470144,-103.6180489
5/16/2019,Pipeline/Piping,Valves,,,,End Of Design Life,The cyclonic blowdown valve was leaking out the stem. The blowdown piping was changed to accept a Balon valve.,user_68,asset_1275,48.224585,-103.8291059
9/25/2017,Separator,Choke Valve/Loop,,,,Trash,New style seats not working went back to original seat and it's holding,user_119,asset_981,48.160251,-103.6173886
1/7/2019,Heat Medium,Pump,Process Indicator,Sunpumper,HBC1,Weather,"no glycol heat trace going to wellhead, made a bunch of adjustments to get it moving",user_31,asset_633,43.56424,-91.351691
12/27/2017,Tanks/Pits,Valving/Swedges,Body,,,Corrosion,"Blow down cyclonic valve is washed out, preventing pressure build, and helping freeze off blowdown piping. Work order in to replace it",user_35,asset_2270,48.19327235,-103.5421398
12/17/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Desi and fuel gas scrubber of liquids daily routine auto dump may be a solution to issue ,user_109,asset_1788,48.3264423,-103.6562598
11/11/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_1489,48.1469003,-103.6177299
4/23/2018,Separator,Liquid Dumps,Controller,Norriseal,,Improper Adjustment,Blew down flow meter and found liquids in the orifice plate assembly. Adjusted seperator dumps. ,user_41,asset_881,48.22028814,-103.6239596
10/5/2019,Separator,Choke Valve/Loop,,,,Freezing,"Dispatched to RTP after tank hauled, found well flowing and reading into Bristol but jsams, submitted work request to automation.",user_18,asset_694,,
10/16/2019,Tanks/Pits,Flare/Combuster,,,,,call out on scc found it out/ re lit and rtp'd scc,user_10,asset_253,40.5262342,-113.8824849
12/31/2016,Gas Scrubber,,,,,,"Fire was out in bath, checked pilot and burner for restrictions found none relit and put back in service ",user_148,asset_1491,48.3063412,-103.6420453
11/20/2018,Separator,Temp Control System,Pilot,,,,"pilot and main burner were shut off, started both",user_31,asset_1820,43.252261,-115.0567324
3/6/2019,Tanks/Pits,Flare/Combuster,,,,,"Scrubbers onsite dry, except for SCC pilot fuel gas scrubber. Drained roughly 1/2 pint",user_54,asset_1383,39.2506642,-92.4357879
12/9/2017,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"Kicked well on due to non arrivals. Paused opened and watched. Plunger came in, restarted cycles.",user_141,asset_515,48.1473689,-103.6174915
12/13/2016,Gas Scrubber,Mechanical Dump Valve,,,,,Freeze between the gate valve and ball valve on the bottom of the desi ,user_39,asset_1148,,
5/17/2017,Wellhead,Manual Valve,Body,,,Trash,"Vented, not much happened. When I was closing blowdown valve noticed handle is messed up. Will try to locate just a handle and return. Until, will pressure build. Plan is to come back to location later today and revent.",user_141,asset_1177,48.1500343,-103.6211481
3/23/2017,Wellhead,Other,Other,Other,Other,Other,Leaking fluids down tree,user_138,asset_1644,48.13828798,-103.4449305
4/11/2018,Chemical System,Tank,Shell,,,Empty - Methanol,"This well has not been receiving injection gas for ~4 days. Operator found the injection pressure equalized with the casing pressure indicating a downhole freeze on the casing side of the well. The methanol pump was turned off waiting for the methanol tank to be filled. The tank was full so the methanol pump was returned to service. Ops shut off the injection gas from the compressor, shut in the tubing, and back blew the casing. This was an unsuccessful attempt to break the freeze due to the amount of time this well was down. Ops tried rocking the freeze with compressed gas which was also unsuccessful. Left the injection gas turned off so the pressures could equalize on the freeze and be broke tomorrow. The well is extremely loaded. Attempted a 2 hour vent to unload but without the assist of casing gas the well did not unload. Will have to attempt the freeze 4/12/18.",user_50,asset_910,48.1470144,-103.6180489
1/15/2018,Wellhead,Cyclonic Valve,Actuator,,,Corrosion, 7. Champlin 345 B-2 - Cyclonic out of sync and not showing a closed a status • Fond cyclonic actuator functioning correctly • Found Closed status switch for actuator functioning correctly • Found common wire for closed status bad between RTU and Separator J-box • Moved to a spare wire • Tested and verified good ,user_92,asset_952,48.1470144,-103.6180489
8/21/2019,Instrumentation,Controller,,,,,"Dispatched to well, got to site and found the compressor online, but no injection to this well Looked on the allen-bradley panel and found that the valve was in auto and showing 30% but physically the valve was closed. Tapped on the DVC and it opened. Possible that the DVC is going out, valve had plenty of pressure will have to keep an eye on it to see if issue happens again.",user_56,asset_1426,40.5262342,-113.8824849
5/29/2017,Wellhead,Tubing,,,,,"Tried venting still froze someone shut off the meth, got it going down tubing and Fmc valves shut in for awhile to force it down tubing, worked on bath and restarted heat trace to these wells on 4pak , done vent log and jsea, come back tomorrow to rtp ",user_131,asset_471,48.01300179,-103.7330017
11/12/2018,Chemical System,Pump,Packing,Goulds,HBC1,Wear," While checking MEOH injection, OPS found Western pump leaking through the packing weep. After attempting to tighten the packing tension collar, the leak did not stop, so OPS notified team lead and tagged out the methanol pump.",user_54,asset_128,48.0831902,-104.8694549
4/5/2017,Gas Scrubber,Other,,Other,Other,Other,Production lost,user_130,asset_1972,48.224585,-103.8291059
1/30/2018,Dehy,Burner,Fire Tube,,,Corrosion,Dehy locked out bt WFS. Fire tube had hole in it.,user_80,asset_1451,48.0713456,-103.3814948
2/18/2019,Separator,Liquid Dumps,Controller,Norriseal,,Improper Adjustment,Adjusted dump so it wouldn't stick anymore.,user_94,asset_140,40.5262342,-113.8824849
3/27/2017,Instrumentation,Transmitter,3n1 MVT,Other,Other,Recalibrated,,user_113,asset_2002,48.22424247,-103.6164158
2/21/2018,Compressor,Compressor,Lubricator,Ariel,,Trash,Possible bad oil pump. Low oil psi. 16,user_156,asset_794,48.22073863,-103.596063
9/14/2017,Fuel Gas/Start Gas,Regulator,,,,,Fisher regulator to burner management valves was plugged. ,user_50,asset_2076,47.99321488,-103.4438922
3/25/2017,SWD System,Other,Other,Other,Other,Other,,user_117,asset_2012,40.5481548,-114.0112915
1/9/2019,Compressor,Intrumentation,,,,,Compressor went down on EICS shut down when I looked at the EICS panel it was cleared and there were no alarms I waited onsite to see if alarm would flag again but it never did I cleared alarm and restarted compressor. I drained all scrubbers on the compressor skid and found the vents to the top of the building were open I slid them shut to help keep heat in the compressor building.,user_159,asset_703,43.56424,-91.351691
1/28/2019,Instrumentation,Switch,,,,,"While attempting to rtp well, I noticed fisher controller was not functioning properly and was way out of wack. Stopped the job and left well shut in until I get a new controller and replace it. ",user_63,asset_1297,48.1898949,-103.4250427
11/12/2017,Compressor,Compressor (Intergral),Process Gas Supply,,,,down on low suction RTP.,user_71,asset_1525,48.1470144,-103.6180489
12/12/2018,Flare System,Flare Header,BMS,,,,Issues: while on location performing my walk around SCC (A) down Root Cause: buy the snow inside the SCC it looks to have been the wind that blew out the pilot Fix: pinched the louvers down more and relight ,user_170,asset_64,43.56424,-91.351691
1/20/2019,Sales Valve (PV),Elec.System,,,,,"OPS attempted to function shut cyclonic valve in JSAMS, no luck. OPS found last attempt to do so 07DEC18 appears to have failed and was left forced open in on hand set well idling since. OPS attempted to function cyclonic via vision/RTU commands and no luck. OPS thawed cyclonic for 30 minutes and tried again with vision, cyclonic went closed. OPS verified functionality via JSAMS using on hand set forcing function both open and closed, then on hand reset utilizing a shut in command. Cyclonic frozen and hit torque limiter. Cyclonic most likely failed and froze due to loss of glycol pumps and ambient temps.",user_54,asset_2016,49.5499678,-102.9290839
12/15/2016,Automation,,,,,,"Tubing transmitter frozen causing well to not flow, thawed transmitter ",user_87,asset_152,47.97948352,-103.4581568
3/10/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Well esd on low mvt psi. Found issues with a dump on the 90. Made minor adjustment. Wells are also extremely loaded from shutting in this compressor. Jumped pad back on and rtp well,user_172,asset_932,,
1/3/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,"Fuel gas buy back installation is complete awaiting commissioning. Verify lateral direction from location. Lateral exits location to the west downhill. Check for fluid at half inch valve downstream of dehy. No fluid present. Request the engineer to give go ahead to Williams to commission buy back meter. Shut in 150 well in preparation to vent. Pull graphs and check pressures. Tbg 145 psi, csg 485 psi. Open to vent. Casing falling fluid to surface in 14 minutes at 17 psi. Extend vent to surface plunger. Plunger to surface at 161 psi after 51 minutes. Allow for cleanup. Final csg pressure 405 psi and tbg pressure 45 psi. Open well back up to supply fuel to pad now that is unloaded. Well has been used for fuel gas supply since 12/21/2017 awaiting decision to proceed with buy back. Three vents in total. ",user_75,asset_385,,
12/28/2017,Fuel Gas/Start Gas,Regulator,,,,,broke well head freeze & thawed reg to esd-rtp well,user_131,asset_350,40.7126799,-114.1193569
9/13/2018,Pumping Unit,Beam Unit,,,,,"Issue: Arrow Dispatch to vent well for deferral Root Cause: Human Error, when i got there i found the rod pump was down and as i performed a walk around i found the well was shut in with the sales cyclonic. upon further investigation i found that an optimizer decided to start shut in cycles and knocked the rod pump down. Fix: got the cycles pulled out and restarted the rod pump ",user_170,asset_588,48.2815848,-102.8554084
8/14/2019,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"Location has been down waiting to have batteries replaced / batteries have been replaced and tested at the PLC. Walked through location and found multiple valves out of position on the water dumps with no tags and the scc's supply line was also shut with no tags. Tested and walked down water dump lines and supply to the scc's before putting them back into service.Jumped units back on and rtp'd contacted optimizer to review and adjust cycles , Kelvin had worked off time down to 25 mins on wells that are running Bar plungers.",user_10,asset_941,48.224585,-103.8291059
11/19/2017,Gas Scrubber Separator,ESD,,,,,Pad shut in on low unit pressure due to cycles lining up on their off time jumped pad back online and staggered out cycles.,user_51,asset_1801,48.1470144,-103.6180489
4/18/2019,Separator,Choke Valve/Loop,,,,Freezing,flow line freeze / broke and rtp'd,user_10,asset_1349,40.5262342,-113.8824849
8/17/2019,Pumping Unit,Sensor,,,,,"Arrived onsite found rod pump down on no rpm signal. Checked sensor to see if it was still lined up with magnet, has not moved. Cleared alarm and restarted rod pump in auto. Engine started, warmed up and engaged clutch. Weights are moving really slowly and wouldn't even turn over on the down stroke. Checked weight on lufkin controller. The amount of weight on the load cell seems normal. Shut down pump and tried again raising rpms slightly. Same thing happened and eventually went down on no rpm signal again. Found that the mechanical arm that engages the clutch is not fully engaging the clutch. Its loose and can still be fully engaged by hand. Not familiar with any procedures on how to adjust this. Shut pump down and tagged out controllers. Coded over to maintenance team. Also put in a work order to have automation relocate the crank sensor. The sensor is currently mounted on the fence. When the wind blows it sways that sensor either close enough to know the magnet of far enough away it doesn't pick it up. Please mount on a stationary part of the unit that will not sway in the wind",user_120,asset_705,,
5/10/2017,Automation,Tower,Antenna,,,Service Outage,tower down. issue was resolved automation tech had to power cycle plc ,user_11,asset_620,,
2/2/2018,Plunger System,Plunger,Lubricator Top,ETC,,Corrosion,"Plunger came in on its own. After pulling the plunger for inspection OPS found the top pads were collapsed and the spring was gone. OPS also found that the wetherford cap springs seems to be broken (rattling around in the cap and the anvil inside is not up against the stop like it should be). After talking to the warehouse we do not have any replacement wetherford caps, SO OPS entered a WR with MAINT to get the lubricator/cap replaced. OPS also found the tubing flow path KF valves leak past internally and asked for those to be replaced as well. The plunger was likely damaged due to the broken spring in the cap and the spring in the cap likely was at it's designed life due to wear. OPS removed the plunger and set cycles for non plunger flow until the well head can be repaired.",user_6,asset_1118,36.2541889,-91.2478009
10/18/2019,Compressor - Gas Lift,Compressor,Suction Controller,Ariel,,Freezing,"Found compressor down on high discharge, broke freeze in the discharge line and rtp'd compressor set rpm at 1400 manual.",user_10,asset_2101,40.5262342,-113.8824849
11/29/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Desi and fuel gas scrubber of liquids daily routine auto dump may be a solution to issue ,user_109,asset_774,48.3272236,-103.6564987
5/5/2018,Separator,ESD Valve,Gas Supply Line,,,Fouling,"Found spring arm off of the Fisher controller. Was able to reinstall it. Then realized block and bleed was bad. Changed it out, and was able to RTP well.",user_141,asset_589,48.1470144,-103.6180489
3/30/2018,Pipeline/Piping,Pipe/Components,,,,End Of Design Life,Replaced bad pressure gauge,user_141,asset_101,48.1470144,-103.6180489
9/13/2017,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,"High tank, turned in as asap",user_84,asset_1467,48.02094746,-103.5251034
9/19/2017,Wellhead,Tubing,,,,,,user_35,asset_1181,48.29651346,-103.4074375
3/21/2017,Tanks,Valving/Swedges,Seat/Ball/Piston,Other,Other,Other,Possibly flooding WFS dehy.,user_141,asset_2136,48.3619066,-103.2129855
4/3/2017,Wellhead,Other,,Other,Other,Other,,user_35,asset_164,48.31750372,-103.5733014
2/22/2017,Tanks,Other,Other,Other,Other,Other,Michigan regulator failure,user_60,asset_2108,48.3631682,-103.7895783
5/5/2019,Separator,Liquid Level Control,,,,,"dumps must have froze, causing liquids to overflow from connections, possibly froze",user_77,asset_1404,48.1470144,-103.6180489
12/5/2017,Gas Scrubber Separator,ESD,,,,,the whole pad went down due to fluids in the fuel supply,user_179,asset_1767,48.1471149,-103.6176793
3/25/2017,Instrumentation,Other,Other,Other,Other,Other,Minimal flow,user_88,asset_495,48.07719271,-103.6669853
3/23/2018,Tanks/Pits,Valving/Swedges,Body,,,Corrosion,All seals on tanks cut or missing ,user_156,asset_1523,48.35479715,-103.7805133
10/9/2017,Compressor,Compressor,Dump Valve,Compressco,,Freezing,High line pressure caused compressor to go down on high discharge PSI so emissions testing was not possible.,user_161,asset_876,40.7126799,-114.1193569
10/20/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_101,,
1/26/2017,Gas Scrubber,Shell,Body,Other,Other,Other,Refurbished glycol pump in stalling out. ,user_41,asset_128,48.27343875,-102.8698842
10/14/2019,Separator,Temp Control System,Heater/Burner,,,," Bath A warm, bath B pilot running but main burner ESD closed. OPS started main burner and no issues were found, possible oversight. ",user_54,asset_1735,43.56424,-91.351691
3/20/2019,Sales Valve (PV),Elec.System,,,,,"sales line cyclonic automated valve out of sync, probable cause is freeze in valve",user_17,asset_2096,,
2/5/2019,Heat Medium,Pump,Housing,Sunpumper,113,Wear,Replaced 1040 glycol pump and returned to service,user_21,asset_1810,46.2356189,-100.6010498
4/11/2017,Gas Scrubber,Other,,Other,Other,Other,"Loss production , got freeze cleared out and flowing ",user_122,asset_1625,48.19815866,-103.790626
8/4/2019,Separator,Liquid Dumps,Seat/Ball/Piston,Norriseal,,Erosion,"Pad was a winter shut in, numerous wellhead valves with no tags and in wrong position or partly open. Pressured up to ESD valve and found leaking flowline blowdown valves on the 100,130 wells, coded to maint. Checked separators and found a split check valve on condo line on east cabinet, replaced. Numerous leaking old leaking packing, replaced packing on the 140 Water, new trim in the 110 condo, new trim in the 130 water. Ran out of time, several more trim sets need packing. Didn't pressure up separator. Found water in 2 of the bonnets and the fuel gas supply, will need to be checked before RTP, All wellheads shut in and tagged, Pre-walk down and SPCC not done. 8/4/2019 Replaced packing and trim sets in 70 well water, 100 well condo. Replaced packing in 70 well condo and 100 well water dump. Pressured up separators and didn't find any other leaks. Started burners and RTP 110 & 140 wells. Started SCC's and burners. Pre walkdown completed and SPCC.",user_31,asset_708,43.56424,-91.351691
5/29/2017,Wellhead,ESD Valve,Actuator,,,Liquid Plugging," 6. Coal Bank 19-90 - ESD venting gas when open, ESD not able to fully opening • Found actuator not opening all the way and gas leaking out of vent • Replaced actuator • Tested and verified new actuator opening correctly ",user_92,asset_1636,48.1470144,-103.6180489
4/6/2017,Automation,Other,,Other,Other,Other,Sales line cyclonic is out of sync and not responding to jsams commands ,user_179,asset_2226,47.95539662,-103.5061956
9/11/2019,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"plunger not making arrivals , vented in plunger for inspection, will replace plunger if needed",user_144,asset_195,48.1470144,-103.6180489
4/22/2018,Tanks/Pits,Flare/Combuster,,,,,Cleaned out pilot orfice. Plugged with soot. Pilot head had been spread out. Put back to original. ,user_156,asset_971,48.27152194,-102.8691722
2/18/2017,Wellhead,Primary Choke,Stem/Seat,Other,Other,Other,Tightened stem 3 turns and stopped leak by ,user_175,asset_1872,47.88158486,-103.5966842
3/3/2019,Fuel Gas/Start Gas,Regulator,,,,,"Got a call out for a high tank. Was at 17', came to location and switched tanks, also have 2 14' condo tanks here that I asked to get hauled, they are filling fast as this pad has been up for a few days and flowing good. Had 3 wells that were ESD'd on valve mis alignment and since I could access location I worked on those and got them open and flowing, also had a bath down that shut on the main burner, got that open and got bath heating back up. Dumps are clear and I emptied scrubbers. Location seems in good shape. Plunger arrivals on the wells that I opened up and the other wells that were already flowing look good.",user_106,asset_1650,48.1470144,-103.6180489
7/22/2017,Flare System,Flare Header,Process Indicator,,,,Scc out probably due to weather ,user_156,asset_1686,48.19131186,-103.6446353
12/13/2017,Compressor,Compressor,Process Gas Supply,Ariel,,Trash,Issue: callout compressor down alarm Root Cause: hi suction pressure. one of the down stream valves on the unit is opening up to hard Fix: optimizer need to check there flow rates and make sure the valves are opening at a controlled enough rate to not hit the compressor so hard,user_136,asset_1401,48.1470144,-103.6180489
11/20/2018,Separator,Dump Line,,,,Freezing,"Well was shut in, assume it had a freeze in the choke. Checked everything over good, started filling separator. Filled separator and shut choke to get burner, pumps, and check dumps. Scrubber was full, drained it. Lit glycol bath and let it start heating up. Turned on glycol pumps, one had the exhaust hose blown. Installed new fitting and reinstalled tube. Check dumps, water was froze. Gave it about 15 minutes, freeze broke. RTP'd well.",user_55,asset_1587,,
1/12/2019,Separator,Dump Line,,,,Freezing,"Found all dumps froze. Got a couple of the open to bleed outside of separator. Still not moving, Steamers showed up, got all the dumps open. I ended up knocking quad pack down. Had to jumper back online. RTP'd all wells ",user_55,asset_1440,,
2/22/2018,Heater Treater,Burner,BMS,,,Pilot Went Out,Issue: found the bath was 52deg on the HMI Root Cause: found with the changing of temp and air density with the last couple of nights been dead calm the burners were set up to run real hard and pull a lot of air causing them to use up all the air in the burner and and then starve for air and blow out. Fix: relight the bath then I readjusted the burners to come on easier and smother to allow time for the burner tube to heat up and start a draft to keep a stable flame and not blow out. ,user_136,asset_1562,48.2629356,-102.8996131
11/5/2017,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,Issue: pad shut in on hi tank alarm Root Cause: recurring problem with this tank. The switch is now out of service but the location had been worked on multiple times. I got with the team lead and it looks like he is working the issue through. Resolution: pad is back on and running. tank transmitter is out of service to keep from a repeat false alarm ,user_136,asset_2247,48.1470144,-103.6180489
11/9/2016,Heater Treater,Firetube,Firetube,,,Corrosion,Unable to I'd the actual damage so we are replacing the fire tube with a salvaged item from a p&a location,user_154,asset_1651,47.95514897,-103.6110178
1/26/2018,Separator,Temp Control System,Fuel Gas Supply,,,,"Found no pressure to all the peripheral fuel gas equipment ( Fisher controller, dumps burner, ect.) but the scrubber pot still had dry gas in it when the scrubber blow down was used. Found freeze in top of fuel gas scrubber pot, where fuel gas is distributed to all support system and there is a pinch point in flow due to piping neck downs into stainless and small 1 inch piping. This rules out a loss of the burner as the cause as the hole system would be flooded and frozen. This leads me to believe a small carry over in the fuel gas due to a high vessel temp that finally caused a drop out during the colder temperature swing and caused the freeze at the top of the scrubber pot where there is the next flow restriction after the fuel gas is taken from the top of the vessel, through the bath, and into the scrubber pot. This would explain why the scrubber pot was dry and thawed at the bottom by the scrubber blow down and frozen at the top where fuel gas is distributed. I thawed the scrubber got dry fuel gas all the way through the rest of the system. Ensured all component parts are functional. Found an over sized gauge for monitoring fuel gas supply PSI (0-2000 psi could not even accurately assess 80 PSI supply pressure) and switched for a 0-200 PSI gauge. Found the regulator supplying the dumps, T-12's, glycol pump and methanol pump set too high and over pressuring the 30 PSI gauges installed on most of that equipment. Turned it down to 28 PSI and checked gauge functionality with known working gauge. I turned down the vessel T-12 to in turn run the vessel a little cooler to target as much drop out in the vessel as possible. I checked both vessel and bath temp probe gauges against my temp gun and found them to be in tolerance (+or- 3 degrees F). I also found two small hole in the cabinet that would have allowed cold temperature into the vessel right next to the scrubber and the vessel. I covered these up with small pieces of insulation tape in an effort to maintain better internal temps with lower temperature swings.",user_6,asset_1475,36.2541889,-91.2478009
4/13/2019,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Attempted to vent plunger to surface to swap but plunger did not come in placed shut in command on well for pressure build,user_18,asset_1901,,
11/18/2017,Fuel Gas/Start Gas,Regulator,,,,,Pilot plugged with liquid ,user_156,asset_1675,48.2715804,-102.8691502
9/7/2017,Chemical System,Pump,Packing,Goulds,375,Wear,"packing on Western pump was worn and wasn't allowing to pump methanol, replaced packing and got pump injecting ",user_53,asset_910,40.5481548,-114.0112915
7/29/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Brought up plunger ,user_94,asset_1019,,
7/21/2017,Flare System,Flare Header,Regulator,,,,Relit SCC. Pilot was extinguished after evening rain fall. ,user_41,asset_1419,48.19683805,-103.5568148
9/14/2019,Automation,Tower,Antenna,,,Loose Connection,Restarted compressor and rtp'd well 130 / emerson system was in and out most of the day / took extra time to rtp'd,user_10,asset_1873,40.5262342,-113.8824849
11/4/2017,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,"Callout: pad called out hi hi tank switch in the blow down tank Root Cause: It was a false alarm the tank only had 3' 3"". was able to rest the alarm and turn the pad back on but this is the second time that i know of this has happened on this locaiton Fix: for now i rest the alarm and turned the location back on. but i will write a work order so automation will come out and look at the switch in order to stop false alarms ",user_136,asset_596,48.1470144,-103.6180489
11/16/2017,Compressor - Gas Lift,Engine,Cooler,Ajax,,Freezing,Issue: compressor called out down alarm Root Cause: found the cooler was freezing off. Fix: blew comp down started warmed back up and returned to service. may need more isolation in the cooler,user_136,asset_1976,48.160299,-103.6174583
8/14/2019,Instrumentation,Meter,Orifice Plate,Control Micro,4203DR,Passed Function Test,"Well flowing but showing deferment, High Clean Found Manifold not in service; but settings in SAMS were not accurate; Corrected and Test Thru SAMS.",user_139,asset_212,,
10/14/2017,Pipeline/Piping,Valves,,,,End Of Design Life,"2” 10,000# Blowdown Cyclonic was passing when closed creating potential freeze issues",user_150,asset_1646,,
2/15/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"just cant get plunger to run, fluid shot done yesterday. not a high liquid level. ",user_84,asset_1225,48.1470144,-103.6180489
2/23/2018,Wellhead,Casing,Intermediate Casing Head Valve,,,,"Arrived on location, found well shut in at line heater. No heat trace pumping. Pressure on well 3676. Hooked up echo-meter, shot 3 fluid shots down annulus of well. Obstruction or fluid level detected at 1059 feet from surface. I suspect it is a freeze. Sent information to TL and engineer, shut well back in and left all valves as found.",user_62,asset_599,40.5481548,-114.0112915
1/13/2018,Heater Treater,Burner,BMS,,,Pilot Went Out,"Issue: found bah was 50deg on the HMI Root Cause: Human Error, regulator got adjusted down Fix: adjusted regulator and relight bath ",user_136,asset_1998,48.1470144,-103.6180489
3/27/2019,Wellhead,Manual Valve,Ball,,,Corrosion,"ball valve on lower tubing wing is stuck in open position, I thawed on valve for 30 minutes until valve was hot to touch but it still would not close.",user_22,asset_161,46.2356189,-100.6010498
11/6/2017,Automation,Cable,Data Cable,3M,,Loose Connection,"Fire eye on bath B lost fire detection with pilot flame, restarted pilot flame and fire eye picked it up ",user_53,asset_559,48.1602263,-103.6172714
11/20/2017,Pumping Unit,Sensor,,,,,Went down on No engine signal. Couldn't find anything wrong with got it restarted and RTP'd.,user_0,asset_588,48.1470144,-103.6180489
12/22/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Kelvin failed to recover plunger ,user_53,asset_73,48.2707208,-102.8879894
1/28/2018,Automation,Plunger Arrival Switch,,EDI,,,MSO is not reading arrivals.,user_0,asset_2024,48.1470144,-103.6180489
5/28/2018,Compressor - Gas Lift,Compressor,Panel,Ariel,,Electrical Short,Compressor down on low oil pressure or esd. ,user_156,asset_521,48.22018479,-103.5963862
2/13/2019,Separator,Dump Line,,,,Freezing,"found unit down thawed out choke and hi/lo pressure up unit and dug out burners on location. Started burner and temped unit bath dumps are frozen had Brett shut well in with a pinched choke to keep unit warm , will we need to check dumps in the morning. Was called back to office because of weather.",user_10,asset_1401,40.5262342,-113.8824849
2/27/2018,Fuel Gas/Start Gas,Coalescer/Filter,Mist Pad,,,,Drain desi ,user_111,asset_1363,48.02420655,-103.3642633
10/2/2019,Separator,Temp Control System,Heater/Burner,,,,"OPS: Found upstream D4 frozen and stuck partially open. Burner was blown out. OPS verified pilot and main burner pressures are correct. Found no liquids in fuel gas to burner main and pilot. Found no freezes in the fuel gas to the burners. Burner likely blown out due to issues with wind. Burner was re-lit and valve thawed, plunger arrival was verified and cycles reset.",user_54,asset_1029,43.56424,-91.351691
3/12/2018,Chemical System,Pump,Plunger,Texam,113,Air Locked,"Western chemical stalled out, fuel gas set to low, would stroke only for 3-5 then stall out, increase fuel gas supply and fixed issue on the 3rd stage injection, 150 well pump diagram bad will not stoke, replaced and RTP'd",user_115,asset_1264,,
1/16/2019,Separator,Dump Line,,,,Freezing,"OPS: Found pad down with no fuel gas. Found windward side cabinet doors open on cabinet B. Wells 20 and 75 share a water dump line and a union was leaking and drained roughly 3""x1'x20' inside the secondary cabinet containment trough. OPS stopped the job, verified with TL permission to proceed with isolation and repair attempt. OPS adjusted JSA to include repair on dump line. OPS was unable to correct the issue and did not have parts on hand. Dump line also seems bound up and possibly too short for connection to function properly. WM and coding completed for MAINT to come replace union, and change'replace/custom fit piping to remove bind on union and ensure good fit and clean vessel and trough. OPS left 20/75 wells shut in and water dump lines tagged out. ",user_54,asset_635,40.5262342,-113.8824849
8/20/2019,Fuel Gas/Start Gas,Pipe/Components,,,,Erosion Corrosion (Internal),"Fuel gas line to ESD was leaking pretty good at pressure regulator, Shut off gas, pulled out fitting and retaped, then put back in service, not leaking now.",user_22,asset_1586,46.2356189,-100.6010498
8/29/2018,Instrumentation,Controller,,,,,"ARROW PLUS ESD was stuck in travel, worked with AUTO and fieldbit to get issue fixed. RTP'd well ",user_56,asset_1224,48.1470144,-103.6180489
1/29/2018,Gas Scrubber Separator,ESD,,,,,call out well shutting in-esd solenoid & scrubber froze-thawed out & rtp boc,user_131,asset_504,40.7126799,-114.1193569
4/19/2019,Separator,Dump Line,,,,Corrosion,"1"" Tulsa check valve corroded externally and leaking, shut and tagged until replaced. Work management entered, using condo only until repaired. ",user_44,asset_541,,
8/22/2019,Separator,Manual Drain Valves,Body,,,Corrosion,The cyclonic blowdown valve was leaking to atmosphere. I t was replaced with a new Balon valve.,user_68,asset_84,48.1470144,-103.6180489
1/6/2018,Tanks/Pits,Flare/Combuster,,,,,B scc pilot out. Relit,user_156,asset_1168,48.20703216,-103.6214101
11/22/2017,Chemical System,Pump,Plunger,Texam,HBC1,Wear,Graco pump,user_156,asset_1460,48.23350179,-103.6425328
8/13/2018,Wellhead,Tubing,,,,,Well is in need of a SIPB Got to location and shut ball valve on header system and tagged out. Can be RTP'd tomorrow or whenever it gets dispatched again ,user_56,asset_970,,
7/22/2017,Compressor,Compressor (Intergral),Oil Level Controller,,,,"Compressor down on low compressor oil level. Verified level and restarted compressor. Verified level again, good. Day tank level is good.",user_141,asset_201,40.5960545,-113.9323891
5/6/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,Vented up plunger and restarted cycles ,user_58,asset_163,48.33972494,-103.6365765
4/10/2019,Separator,Temp Control System,Thermostat,,,, +GLYCHOL BATH T12 THERMOSTAT SET FOR 160 DEGREES- SHUT OFF AND RESET AT 80 DEGREES,user_34,asset_1108,40.5262342,-113.8824849
9/29/2018,Compressor,Compressor,Suction Controller,Ariel,,Trash,"comp and vru going down, found comp down multiple time on lo inter stage and lo discharge , found off skid recycle not opening enough and starving compressor, causing comp to go down this also causes the vru to go down due to being connected on the same inlet line, adjusted recycle to start opening sooner to keep inter stage psi and discharge psi higher, also found stanless line from flair scrubber to pit used for drilling rig, removed line and put up tag saying no fluid can be dumped into this pit. ",user_144,asset_1383,48.1470144,-103.6180489
7/12/2018,Automation,RTU,Fuse,Emerson,Bristol 3310,Corrosion,Found that the emerson had a program issue on this well. I contacted Mike Edwards and with his help I function tested the card in the PLC and Mike is rebooting the program to restore comms.Mike will contact me when the well has restored comm.,user_100,asset_2216,43.252261,-115.0567324
12/1/2018,Pipeline/Piping,Pipe/Components,,,,hydrate,"Well had been down since the 18th. Had no unit pressure. Pressured up unit slowly, listened for leaks. None heard. Lit the burner and checked the dumps. All clear. Found sales line froze. Thawed on it and got it cleared. Contacted optimizer to start cycles. Well is flowing good. RTP'd",user_55,asset_2166,,
10/5/2018,Automation,RTU,Fuse,Schneider/Scadapack,Scadapack P4A,Electrical Short,Tubing pressure transmitter was not working. Found the fuse in the RTU for power to transmitter was blown. Could not identify what caused the fuse to blow. Replaced fuse and transmitter powered back up.,user_108,asset_1926,,
12/15/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_1633,,
6/22/2018,SWD System,Particle Filter,Instrumentation,,,,West side offload pump turbine meter impeller broke as I was removing it.,user_163,asset_523,43.252261,-115.0567324
3/12/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ge Gemini,,Freezing,"compressor went down on high discharge psi, started ,loaded, and psi is normal, will watch it.",user_84,asset_1391,48.1470144,-103.6180489
12/7/2016,Sand Separator,Manual Drain Valves,Body,,,Freezing,"Choke would not close. Worked on thawing the DVC, fuel supply bowl filter, lines and regulator. No luck thawing, must be a different issue with the DVC, can shut off fuel supply and choke closes. Wrote a task to Automation to repair.",user_141,asset_1348,48.3619066,-103.2129855
1/24/2019,Sales Valve (PV),Sales Valve,Body,Valvcon,,Freezing,+SALES LINE CYCLONIC VALVE FROZEN ***ACTUATOR IS IN WORKING CONDITION **THAWED VALVE AND VERIFIED OPERATION,user_34,asset_811,43.56424,-91.351691
11/7/2017,Compressor,Compressor,Scrubber Level,Ajax,,Freezing,Issue: comp went down on hi dischage pressure Root Cause: found lots of fluid in the scrubbers all 3stages means we are carrying fluid over. I also found the cooler doesn't have any isolation in it. Fix: scrubbers need drained frequently and the cooler needs isolated ,user_136,asset_521,48.2594907,-102.9011386
3/19/2018,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,"Knock out pots, to flare, fuel gas to flare, line heater, and line heater scrubber had liquids. Wells flowing over 110deg carries liquids through the gas stream which drop out in these pots and scrubbers. ",user_58,asset_580,48.37264818,-103.5168052
2/12/2018,Heat Medium,Pump,Diaphragm Gears,Texam,HBC1,Wear,"Replaced Graco 1040 1"" glycol pump & RTP'd.",user_161,asset_1262,40.7126799,-114.1193569
3/23/2018,Heater Treater,Burner,BMS,,,Pilot Went Out,"Issue: found bath (B) down. no (INT) Root Cause: Human Error, went to location and walked threw the bath and made sure nothing was tagged out and everything was lined up. looks like the pad had issues and once the work was done no one went back through the pad and made sure everything was in order before leaving Fix: relight bath remotely and returned to service ",user_136,asset_175,48.0614644,-104.8417043
1/15/2017,Chemical System,,,,,,"WFS. Dehy was froze, got contacted thawed and flowing 435 mcf. ",user_84,asset_2096,48.05321393,-103.4831666
9/27/2019,Tanks/Pits,Berm,Gravel,,,Erosion,"Repack bottom of the tank with new gravel, please let us know if the tank keeps moving, to do something different",user_21,asset_2275,46.2356189,-100.6010498
12/7/2017,Pipeline/Piping,Valves,,,,End Of Design Life,Check valve replaced found leaking - due to loose connection,user_150,asset_1841,,
4/7/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,noticed while going through pad well 10 csg psi was up to 11003-went there and knocked the comp down trying to get csg freeze broke-finally got it and rtp comp and well 10 & 20 again,user_131,asset_551,40.7126799,-114.1193569
10/30/2019,Separator Inlet Valve (XV),Electric Control System,Actuator,,,,Thawed ESD. Was able to clear interlock and open ESD. RTP'd well,user_55,asset_1016,,
1/19/2017,Gas Scrubber,Mechanical Dump Valve,Controller,Other,Other,Freezing,Damaged fisher control,user_88,asset_1554,,
6/6/2017,Instrumentation,Transmitter,Unit Pressure,Rosemount,3051,Calibration Issue, 3. North east echo springs 33-2 - unit transmitter spiking and dropping • Found transmitter reading 160 psi but showing 100% output • Verified all wiring connections done correctly and tight • Zeroed transmitter • Power cycled transmitter • Verified transmitter now reading correctly ,user_92,asset_1820,48.14640464,-103.445083
3/7/2017,Gas Scrubber,Back Pressure Valve,Seat/Ball/Piston,Kimray,Other,Trash,,user_171,asset_530,36.4444249,-91.3023088
10/28/2017,Gas Scrubber Separator,Dump Line,,,,Trash,dump stuck open on green complete and overpressured heater treater causing it to ESD the well> rest and RTP/,user_71,asset_1915,48.1470144,-103.6180489
1/10/2017,Instrumentation,Transmitter,3n1 MVT,Rosemount,4088,Weather,Meter had comm issues sent a download to meter working fine.,user_13,asset_853,48.16020867,-103.6172068
9/12/2017,Separator,Temp Control System,Thermostat,,,,Replaced non-functioning T 12 on vessel.,user_80,asset_1544,,
4/14/2019,Separator Inlet Valve (XV),Pneumatic Control System,Vent,,,,"Human error: Found bypass on hi lo open, unit live with pressure, and no tags in place. Defeated safety system.",user_54,asset_1965,48.1470144,-103.6180489
2/7/2017,Wellhead,Cyclonic Valve,Actuator,Other,Other,Freezing,Dvc regulator froze thawed rtp,user_176,asset_776,48.21026406,-103.6492552
10/4/2017,Separator,Liquid Dumps,Controller,Norriseal,,Improper Adjustment,,user_126,asset_1348,,
5/1/2018,Gas Scrubber Separator,ESD,,,,,Scrubber pots were balled off with fluid I cleared scrubber pots and regulators onsite and and brought well back online.,user_51,asset_1203,47.9418861,-103.6976002
3/12/2017,Compressor,Compressor,Other,Other,Other,Freezing,wfs lateral has a freeze in pipeline contacted tyler mortenson with williams he is getting a methanol trailer to break pipeline freeze. compressor will be put back in service as soon as freeze is broken,user_11,asset_265,,
10/19/2017,Tanks/Pits,Liquid Level Control,,,,,"Site glass on scc Sump is broke, shut valves , turned in work order for repair ",user_122,asset_1675,48.34290545,-103.6995883
3/8/2018,Flare System,Flare Header,Instrumentation,,,,Issue: found SCC (A) down on the HMI Root Cause: (INT) valve fault. Trying to run 3 SCC's off of one regulator at the SCC's that's exposed to all the elements Fix: was able relight remotely,user_136,asset_996,48.2594026,-102.9010889
5/23/2018,Separator,Shell,Body,,Steel,Vandalism,Steamed out separator cabinet due to pack rats,user_150,asset_1908,,
9/12/2018,Separator,Choke Valve/Loop,,,,Trash,"well 100% down on production, found inlet valve at manifold shut, opened and worked well on, rtp to cycles and wfs came an got a sample",user_144,asset_277,48.1470144,-103.6180489
10/29/2019,Gas Scrubber Separator,Dump Line,,,,Freezing,"Drained the Dezi took about 5 seconds, drained the scrubbers, drained all the drip pots, and all the pressure regulators, Thumbed the dumps and checked bath temp.",user_76,asset_2076,46.2356189,-100.6010498
4/13/2018,Separator,ESD Valve,Actuator,,,Calibration,"Well was showing a deferral, pulled a graph and looks like the well stopped cycling. Went to location to troubleshoot possible down stream freeze/issue. Had 720 on tubing. 620 unit pressure. Temps looked good 68degrees in unit. Had optimizer force downstream cyclonic open. Found that the cyclonic needed to be downloaded and the cycle criteria had been removed. Optimizer entered criteria and is going to be working on plunger cycles well RTp",user_172,asset_602,,
8/26/2019,Separator,Choke Valve/Loop,,,,Corrosion,Choke replaced and ready for calibration,user_21,asset_708,48.1070894,-104.8939242
4/12/2019,Heat Medium,Pump,Instrumentation,Goulds,HBC1,Electrical Wiring,West side glycol pump skid - Controller and motor were both bad. Replaced them and turned the pump on.,user_108,asset_18,,
11/20/2018,Separator,Dump Line,,,,Freezing,"Well was shut in due to stuck condo dump. Adjusted dump. Checked everything over good, started filling separator. Filled separator and shut choke to get burner, pumps, and check dumps. Lit glycol bath and let it start heating up. Turned on glycol pumps. Check dumps, water was froze. Gave it about 15 minutes, freeze broke. RTP'd well.",user_55,asset_360,,
4/7/2017,Gas Scrubber,Other,Other,Other,Other,Other,"Choke is very stiff, needs replaced SI well until parts are picked up",user_53,asset_403,48.05148445,-103.3692942
12/31/2016,Gas Scrubber,,,,,,Fire went out on bath heater unit is a block of ice installing jumper to warm up unit ,user_148,asset_456,48.31184137,-103.6330664
9/2/2019,Dehy,WFS Issue,,,,,Dispatched to well. Got to site and found well is cycling but its deferring because of WFS Did a walk around of location everything was good. ,user_56,asset_931,40.5262342,-113.8824849
2/19/2019,Wellhead,Tubing,,,,,"Couldn't read or even see the tubing transmitter, approximately 9 ft in the air. Will write a work order to have stairs installed at well head.",user_55,asset_523,,
8/15/2017,Flare System,Flare Header,Regulator,,,,"Relit SCC ""A"". Pilot was extinguished after evening rain fall. ",user_41,asset_1227,48.16519268,-103.6813316
2/14/2017,Gas Scrubber,Mechanical Dump Valve,Supply Line,Other,Other,Freezing,Solenoid/sandprobes and regulators fuel gas froze off,user_131,asset_23,47.8646618,-103.5284358
2/13/2018,Heater Treater,Burner,BMS,,,Corrosion,Issue: called out bath shut in alarm. (INT) low bath (B) glycol level Root Cause: went to location walked through the location and didn't see any glycol anywhere. Acts like the transmitter may have had a bad reads Fix: rest the alarm and relight the bath remotely ,user_136,asset_628,48.1470144,-103.6180489
1/16/2019,Wellhead,Cyclonic Valve,Actuator,,,Freezing, 6. Coal Bank 5-5 - Cyclonic issue • Found cyclonic actuator closed • Tried to open cyclonic and it didn’t respond • I sent cyclonic a closed command and then a open command and cyclonic opened right up • Torque limiter tripped in cyclonic actuator probably due to a hydrate or freeze in the valve at an earlier date • I put actuator back in auto • Coded well back to operations • Notified operations ,user_38,asset_2245,40.5262342,-113.8824849
10/31/2019,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,Replaced NRG tape on condo tank and reset control loop and tested. Verified operations in RTU and with optimizer.,user_44,asset_1419,46.2356189,-100.6010498
10/16/2019,Separator,Water Meter,Turbine,,,Corrosion,"looking through emerson this morning found location down due to a high high tank. all six tanks were showing a high status with live reads reading highest tank was 8.3', contacted automation tech to see if he had been working on the tank transmitters he reported there was contract crew onsite working on tank switches. arrived onsite found water truck driver pulling down tanks and automation crew working on top off tanks. informed them that they need to be wearing respirators while doing any work on tanks.wyotex had green complete shut in and tagged out. they were changing out turbines on both water and oil dumps. switching them from 2ich to one inch. contacted engineer and informed him that we should not be changing the orifice size on the water dump,he agreed. had crew change out turbine on condo only.leak tested dumps after crew completed work. drained ko pots for scc. found the sight glass broken on one of the knock out pots with valves open, small amount of gas was blowing out of broken sight glass. isolated glass and tagged out both valves.took all tanks out of operational bypass or high status and put them back to normal, had to do each tank individually but this allowed me to finally clear the high tank status and reset the interlock on high low.verified all tank levels are low before resetting interlock. crossfire has some piping locked out for compressor install. while doing a walk around of location found a 3/8 stainless line on flowline of green complete open ended with needle valve completely open. the only reason this line wasnt blowing well bore pressure is because of a 3/8 stainless check valve in the line. this line was previously used for an injection point that we used for a de foamer chemical. when they disconnected there pump they left the line open ended and the needle valve open, unacceptable.removed line and installed a plug. put well to sales, well died down very quickly with over 1000psi differential between tubing and casing. vented well to tank for around 45 minutes.tubing psi increased to around 418psi, put well to sales on 64?64 choke. green complete is 110 degrees. changed out one inch balon on on condo dump it was leaking by internally. adjusted oil dump level was getting to high trying to push through one turbine, dumps is now keeping up. well rtp to sales",user_120,asset_796,40.5262342,-113.8824849
1/4/2017,Automation,Battery,Battery,UPC,Other,Weather,No damage ,user_74,asset_1430,48.26579207,-103.4628189
2/8/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,changed out worn dual pad with new dual pad,user_11,asset_1249,48.1470144,-103.6180489
11/20/2018,Flare System,Flare Header,BMS,,,,Issue: while performing my walk around i found SCC #2 down Root Cause: the on board computer shows flame fail Fix: looks like shut down on low pressure but didn't relight. long term fix is to pull setting and just make run all the time,user_170,asset_705,48.2648401,-102.9012874
12/9/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,"Found fuel gas scrubber full, had raised the float and shut fuel supply off to everything in that quad pack. Drained scrubber, shut off fuel supply to scrubber witch allowed float to drop. Repressured unit. Got all back online.",user_141,asset_2209,48.1473689,-103.6174915
11/11/2017,Separator,Choke Valve/Loop,,,,Freezing,Well has no flow for today and yesterday. Got to location noticed dvc was not working. Fuel gas was froze going to dvc. Thawed that out. Had a freeze in inlet on separator. Thawed that out.attempted to rtp well. Water dump frozen. Got it to break. Four pack low on glycol can not light bath needs to be filled ASAP l,user_172,asset_1413,,
5/11/2018,Compressor,Compressor (Intergral),Dump Valve,,,,"Siberia 30 comp down on low interstage pressure, suction scrubber dump stuck open, got dump working and RTP.",user_71,asset_1124,48.1470144,-103.6180489
9/13/2019,SWD System,SWD Pump,,,,Lubrication,"Location was checked no issues. Shut off pond water since level was at 9'. 9/12/2019 replaced thrust chamber on pump #3, it was leaking. 9/13/2109 Removed thrust chamber again and the seal had the wrong O ring and was too small. Put the old O ring in and no leaks. Started pump up.",user_31,asset_308,48.1470144,-103.6180489
1/19/2017,Gas Scrubber,Shell,Nozzle,Other,Other,Erosion,"South glycol pump on center quad pack stopped pumping, reason unknown ",user_148,asset_1525,48.33945684,-103.6364712
7/3/2017,Wellhead,Wellhead Piping,,,,,IPS Lubricator catch has stripped threads,user_105,asset_546,48.09453923,-103.3424324
1/13/2019,Fuel Gas/Start Gas,Regulator,,,,,"Issue: during my walk around i found the diaphragm was blown on the kimray Root Cause: Human Error, the supply pressure to open the valve got turned way up blowing the diaphragm Fix: wrote WM to remove ",user_170,asset_247,43.56424,-91.351691
11/9/2019,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Found plunger missing arrivals, vented plunger to surface and RTPd well, plunger less then two months old so did not inspect. ",user_18,asset_495,,
3/22/2019,Surface Location,Lease Road,,,,Weather,3/22/19 Plowed location access road & turnaround. Well is ready for ops to attempt to RTP.,user_42,asset_137,46.2356189,-100.6010498
1/18/2017,Compressor,Compressor,Suction Controller,,,Freezing,Compressor down on low suction. Process gas to suction control valve froze off thawed and returned to service,user_11,asset_82,,
7/18/2018,Wellhead,Tubing,,,,hydrate,"ARROW Well was dispatched because it is deferring which is accurate, but both TBG and CSG are froze. Need hot oil set up to get freeze broke. ",user_56,asset_1825,48.2591755,-102.9018355
2/13/2018,Compressor,Compressor (Screw),Coupling,,,,replace belts and rtp,user_84,asset_1803,48.1470144,-103.6180489
12/3/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_1633,40.5262342,-113.8824849
5/16/2018,Flare System,Flare Header,Instrumentation,,,,Igniter was arcing to thermocouple and not the pilot tip. Adjusted igniter and thermocouple.,user_65,asset_796,40.7126799,-114.1193569
8/7/2018,Pumping Unit,Sensor,,,,,Rod pump down on remote stop fault. Cleared alarm and RTPd pump,user_147,asset_1644,,
9/14/2017,Recirc Pump,Pump,Housing,Texam,HBC1,Wear,glycol pump stalled just blowing gas not pumping need new one ,user_110,asset_1242,48.1472905,-103.6181064
5/30/2019,Separator,Thermostat,,,,,"Called out for high temp on separator and found the bath at 170 degrees. the T 12 seemed to have stuck but after manipulating it back and forth it began to operate correctly, adjusted it down to approx. 100 degrees",user_22,asset_1484,46.2356189,-100.6010498
3/19/2019,Tanks/Pits,Shell,Body,,Steel,Corrosion,"Bottom of water tank has rust thru and could start leaking, this is the only water tank currently set up to flow.",user_174,asset_1567,38.4425988,-95.5406131
7/5/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,Well was shut in on consecutive non arrivals I surfaced plunger and put back on plunger cycles.,user_51,asset_1993,48.1470144,-103.6180489
11/1/2018,Separator,Liquid Level Control,,,,,"dump trim washed out, replaced",user_64,asset_1389,43.56424,-91.351691
2/2/2018,Automation,Radio,Wiring,3M,,Electrical Short,"BB 19-80 pad, called out on high water tank. False alarm, reset interlock and RTP pad. Went back down an hour after I left, on the same alarm. Went back and restarted. Adam put level switch in operational bypass. Pad stayed up the rest of the night. ",user_71,asset_787,48.1470144,-103.6180489
11/6/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash,HI/LO valve body leaks ,user_179,asset_1908,48.1470144,-103.6180489
6/24/2018,Separator,Choke Valve/Loop,,,,Corrosion,"Choke linkage from DVC is rusty and tight, loosened slightly and lubricated the linkage. Choke opened RTP'd Notified optimizer",user_163,asset_1152,43.252261,-115.0567324
6/26/2019,Separator,Temp Control System,Pilot,,,,"Frozen in flowline at line heater, actuator at 261 D1 isn't working, probably causing some of the freezing issues, only opens about 30%. Attempted to break freeze. Isolated flowline and bleed down to thaw. Pilot was plugged at the D-1 separator, cleaned out and started pilot, left main burner off, glycol pumps were running, shut off.",user_31,asset_154,43.56424,-91.351691
5/1/2018,Fuel Gas/Start Gas,Regulator,,,,,Burner pilot tip was plugged up. Cleaned manually.,user_107,asset_434,,
4/22/2018,Compressor,Compressor,Process Gas Supply,Ariel,,Trash,Issue: compressor down alarm Root Cause: went down on low suction pressure. pulled wells up and the cycles are not cycling very well and the compressor is spending way to long recycling until it runs out of gas Fix: left well running to keep feeding the compressor until the well can be optimized ,user_136,asset_857,48.2594956,-102.9009337
12/22/2017,Gas Scrubber Separator,ESD,,,,,well shut in on high scrubber level. drained scrubbers and restarted,user_71,asset_1675,48.1470144,-103.6180489
4/18/2018,Wellhead,Tubing,,,,,Vented ,user_86,asset_1575,,
4/11/2017,Automation,Radio,Other,Other,Other,Improper Install,radio mast was not strong enough to support the weight of the upgraded radio,user_92,asset_1321,48.224585,-103.8291059
11/10/2016,Wellhead,,,,,Other,"Below ground glycol line corroded and leaked, upon excavating location existing piping 7' deep, replacing all below ground piping to bring up to 42"". ",user_8,asset_439,48.24130023,-103.1298451
6/17/2019,Separator,Controller,,,,,Hi lo block and bleed was bad not controlling pressure to unit. Changed it out with new one and checked pressures. Lo 100 hi 575. Well rtp,user_153,asset_1462,,
6/19/2018,Tanks/Pits,Flare/Combuster,,,,,ARROWPLUS 1 scc out. Everything ok. Out due to heavy rain. ,user_156,asset_2242,48.1961522,-103.619005
1/28/2019,Tanks/Pits,Flare/Combuster,,,,,"all scc's probably due to high winds, relit",user_31,asset_1135,43.56424,-91.351691
7/26/2017,Compressor,Compressor,Process Gas Supply,Ariel,,Liquid Carryover,Compressor down on low discharge pressure. Recycling too much well works needs done to run compressor correctly. ,user_103,asset_617,48.25467825,-103.6529959
7/21/2017,Compressor - Gas Lift,Compressor,Suction Controller,Copeland,,Vibration,"down on low suction, back up 130 and 140 both flowing",user_176,asset_1873,40.5960545,-113.9323891
1/15/2017,Sand Separator,Containment,,Other,Other,Weather,"Need glycol in sepator level is low 11""",user_39,asset_1427,,
1/18/2018,Dehy,WFS Issue,,,,,Dehy down due to burner tube leakes and WFS not fixing it. Froze up down stream of their sep,user_58,asset_1392,48.34744484,-103.6192951
2/24/2018,Separator,ESD Valve,Gas Supply Line,,,Freezing,Scrubbers are ball checked lossy fuel gas. Supply line to esd froze. Baths are cold. Thawed out fuel gas got esd open and well rtp on plunger cycles,user_172,asset_31,,
10/21/2018,Gas Scrubber Separator,Dump Line,,,,Corrosion,"Dispatch to pad. Got to location and found completely down. Jumped pad back on and was getting wells cycling After that pad started shutting back in Upon further review, I found the 1 inch unit dump valve leaking on the 120 well I was able to get valve replaced and got pad RTP'd ",user_56,asset_729,48.1470144,-103.6180489
1/6/2019,Tanks/Pits,Flare/Combuster,,,,,"pilot orifice was plugged, also cleaned a moth out of pilot mixing tube, relit",user_31,asset_148,43.56424,-91.351691
5/22/2018,Tanks/Pits,Liquid Level Control,,,,,"Issue: called out hi tank alarm Root Cause: Human Error/ Dispatch found water tank at 19' 4"" Fix: shut well in called IBEX and they were headed to haul the water ",user_136,asset_1197,40.7126799,-114.1193569
4/27/2017,Compressor,Compressor,Process Gas Supply,Ariel,,Trash,"Compressor down on lo discharge Not enough wells on to feed compressor , restarted compressor , 6 wells shut in on high line set points , set points need raised too 600psi , ",user_122,asset_886,48.30722805,-103.6409565
1/20/2019,Separator,Liquid Dumps,Float,Norriseal,,Freezing,"Well was warm, dumps cleared, RTPed",user_97,asset_295,40.536336,-114.0492448
4/3/2019,Surface Location,Well Pad,,,,Weather,snow covering equipment access ,user_28,asset_2251,48.1511744,-103.6275517
11/10/2016,Gas Scrubber,Pnumatic Dump Valve,Seat/Ball/Piston,,,Erosion,Leaking choke,user_148,asset_1849,48.30903565,-103.6751845
3/20/2017,SWD System,Other,,Other,Other,Other,Down time ,user_141,asset_1489,48.3619066,-103.2129855
7/2/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_1489,48.1470144,-103.6180489
7/14/2019,Plunger System,Plunger,Lubricator Top,IPS,,No Liquid,I was able to vent in plunger. Something is keeping the plunger from entering the lubricator. Plunger is caught above the bottom master. Well is shut in ,user_90,asset_1321,48.30724984,-103.3894658
1/16/2018,Separator,Back Pressure Valve,Body,Kimray,,Freezing,"frozen back psi valve, this valve sits outside the cabinet with no heat. thawed out",user_87,asset_787,40.7126799,-114.1193569
2/24/2018,Heater Treater,Burner,BMS,,,Loss Of Fuel Gas,"Issue: found Bath (C) was down with a bath temp of 55deg. No (INT) Root Cause: Human Error, the remote lighting sequence wasn't started to light the bath Fix: relight remotely using the light sequence ",user_136,asset_1404,48.2594705,-102.9010554
11/5/2019,Separator,Fuel Supply System,Regulator,,,freeze,"OPS: Found unit with no fuel gas pressure, hi lo frozen and big joe frozen. Hot pass for fuel gas is bypassed, sending vessel temp pass to big joe, causing it to hydrate the big joe off, allowing the choke to hydrate off the coils/hi-lo. OPS STJ, contacted TL, could not find any reason this work was done to the fuel gas supply, received permission from TL to pressure test hot pass and if it passed RTS the system with the hot pass in line again. FGHP passed test and piping reconfigured to allow fuel gas to be warmed by bath. RTS unit/burner/glycol pump. RTP'ed well after a vent to unload and bring warm fluid/gas up tubing in an attempt to remove any hydrates.",user_54,asset_1810,46.2356189,-100.6010498
3/22/2018,Chemical System,Piping,Discharge Line,,,Corrosion,"Possible partial restriction/hydrate down hole. Found methanol pump not operating. Removed thumb valve cleaned, and replaced. Adjusted flow to around 9 gallons per day. Will check on it tomorrow and see if it is any better.",user_141,asset_1308,48.1470144,-103.6180489
3/16/2018,Flare System,Flare Header,Regulator,,,,"SCC out, was able to light remotely",user_141,asset_620,48.1470144,-103.6180489
10/20/2018,Separator,ESD Valve,Actuator,,,Freezing,"Cyclonic is stuck open. Causing well to free flow and liquid load.Optimizer sent download to cyclonic, but hasn't moved. I removed top works and cyclonic turns freely. Motor is probably bad due to winterization not being done. Shut in FMC valves at wellhead to pressure build well until automation can repair sales cyclonic",user_120,asset_2016,48.35599645,-103.651869
11/13/2017,Compressor,Intrumentation,,,,,"Meter run was froze off. Heat trace not carrying over any heat, no meth in this part of the system",user_35,asset_1812,48.19854456,-103.4827269
2/16/2017,Instrumentation,Other,,Other,Other,Other,reset over tourque,user_65,asset_450,48.3619066,-103.2129855
4/4/2018,Tanks/Pits,Flare/Combuster,,,,,Scc down on flame fail drained and relit,user_172,asset_1800,,
11/25/2018,Flare System,Flare Header,Regulator,,,,"OPS found pilot fuel gas line hydrated off and leaking pressure through regulator weep, indicating the diaphragm has lost integrity, likely due to liquids in fuel gas line expanding and damaging regulator internals allowing gas too leak off causing JT resulting in hydrates. Fuel gas and main supply lines not insulated/heat traced allowing carry over of liquids into the lines and subsequent freezing/hydrates. OPS replaced regulator, set functional PSI and re-lit SCC. OPS verified no leaks. Pad runs off of fuel gas buy back, OPS found desi-dryer had significant liquids in it. Dehy seems up and functional but not pump strokes could be heard, indicating dehy may not be fully functional as buy back is pulled from post dehydration sales. OPS emptied scrubber dumps and verified valving positions to ensure all gas goes to desi-dryer in an effort drop out as much liquid as possible. Desi-dryer may be too inefficient to completely remove liquids from fuel gas supply to SCC's to keep them dry enough to not freeze/hydrate. No cold finger is installed onsite.",user_54,asset_1988,48.0831411,-104.8694914
2/25/2018,Fuel Gas/Start Gas,Regulator,,,,,well compressor went down on high suction scrubber liquid level. thawed and drained returned to service the found that line heater fuel gas was frozen thawed fuel gas and got burners lit,user_11,asset_1707,40.5481548,-114.0112915
11/21/2017,Compressor,Compressor,Process Gas Supply,Compressco,,Trash,Compressor down on low suction pressure. Cleared alarm restarted compressor ,user_172,asset_1525,,
5/12/2017,Compressor,Compressor,Scrubber Level,Ajax,,Vibration,"While working on recycle valve in compressor. We identified that the 4"" flange going into the first stage scrubber pot had the wrong size bolts on the flange. The bolts installed were 3/4"" x 6"" bolts but the flange requires 7/8"" x 6"" bolts. We stopped the job contacted the OPS TL to determine how they would like us to move forward, after conversation with TL we decided to move forward with replacing the bolts on the flange.",user_8,asset_1339,48.1470144,-103.6180489
3/18/2018,Flare System,Flare Header,BMS,,,,Issue: SCC # 1 down Root Cause: when the location shut in the pilot ran out of fuel gas Fix: once the location was back on i returned it to service ,user_136,asset_1675,48.1470144,-103.6180489
1/25/2017,Tanks,,,Other,Other,Other,,user_179,asset_2,47.92002134,-103.4941064
9/5/2018,Plunger System,Plunger,MSO,Trip Mate,,Wiring Shorts,MSO was removed for well work and never put back on when well head was reconfigured. I installed the MSO so we can start monitoring plunger arrivals. ,user_15,asset_2202,48.1470144,-103.6180489
4/20/2018,Heater Treater,Burner,BMS,,,Loss Of Fuel Gas,Issue: bath (B) down Root Cause: when the pad ran out of fuel gas the burner ESD's shut in on valve fault Fix: once the pad was pressured back on i was able to relight remotely,user_136,asset_932,48.0614644,-104.8417043
2/28/2017,Gas Scrubber,Dump Line,Dump Line,Other,Other,Other,"Pilot plugged fire out, cleaned pilot tip",user_87,asset_1126,47.93859031,-103.4903237
2/15/2017,Automation,Cable,Data Cable,Automation-X,Other,Other,"Flow line froze,",user_84,asset_405,48.09607768,-103.5401769
9/15/2017,Flare System,Flare Header,Process Indicator,,,,Scc out probably due to weather ,user_156,asset_1892,48.20989936,-103.6485718
3/19/2019,Separator,Liquid Dumps,Body,Norriseal,,Freezing,Y strainer split.,user_94,asset_1600,48.113936,-104.12136
5/11/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Drained desi while on location. Took 15 seconds to drain fluids.,user_62,asset_932,48.1470144,-103.6180489
1/22/2018,Fuel Gas/Start Gas,Regulator,,,,,"Fuel gas from hp unit to SCCs froze. Root cause wet fuel gas, construction has a up graded to help the issue if we can get it done. ",user_58,asset_876,48.41632191,-103.5768604
10/27/2017,Compressor,Cooler,,,,,"Compressor went down on high discharge psi, had a cooler freeze, cleared out freeze, root cause is the insulation in cooler is falling out, called Archrock to come make repairs",user_122,asset_1206,48.32698675,-103.6566704
7/29/2018,Automation,Plunger Arrival Switch,,Tripmate,,,Mso switch has moved so it was more on the top flow path and not on tubing. Adjusted and attached ,user_31,asset_2019,48.42242272,-103.604378
5/20/2019,Wellhead,Valves,,,,Corrosion (Internal),"master tubing valves will only move 1/4th turn, didn't force valves open , contacted TL to have maintenance trouble shoot",user_144,asset_1873,40.5262342,-113.8824849
3/8/2017,Wellhead,Other,Other,Other,Other,Other,Higher casing pressures creating JT freezing off the coil near surface. Waiting on Methanol. Swapped to casing flow to warm tubing up until freeze breaks or Methanol is delivered ,user_175,asset_1403,47.96416773,-103.6914716
10/2/2019,Separator,Fuel Supply System,Regulator,,,wear,"Pad went down on low unit pressure,this well will need a downstream valve installed to keep the pad up when running the glycol baths and pumps running. Work order was already turned in but i wrote another work order for the downstream valve. Pressured up units and functioned tested chokes and rtp'd. found that the choke on the 40 well was not responding, removed and cleaned I/P and put well back into service and function tested. Restarted all scc's and baths on location did not start pumps because of fuel gas issue.",user_10,asset_1652,40.5262342,-113.8824849
10/16/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Ajax,,Freezing,"Compressor down on high discharge pressure. Cause of high pressure appears to be hydrate formation through D4, meter or casing annulus entry point. Blowdown compressor to restart for warm up. Start compressor to warm up. Reconfigure methanol injection point with stainless tbg from instrumentation flange to injection point upstream of the D4 and meter. Load compressor and begin injecting. Annulus accepting gas. Will monitor hydrate remediation plan overnight. If no hydrates form will work with optimizer to optimize flow rates for both wells on compressor. ",user_75,asset_521,,
11/6/2017,Separator,Shell,Body,,Steel,Erosion,Inlet to separator frozen. Adjusted burner temps to prevent future issues ,user_107,asset_1932,47.95101213,-103.4209421
10/5/2017,Separator,Temp Control System,Fuel Gas Supply,,,,Pilot for the burner was clogged. It was cleaned and relit. ,user_41,asset_1336,48.22788202,-103.6247321
2/2/2018,Gas Scrubber Separator,ESD,,,,,Champ 263 b #40 & #130 down on valve miss/. Low unit. RTP and started cycles. ,user_71,asset_1788,48.1470144,-103.6180489
11/30/2017,Separator,Choke Valve/Loop,,,,Freezing,"In let has a hydrated in it shut inlet an released pressure off freeze to remove it , d4 was not all the way open an cause hydrate, adjusted tension spring on d4",user_122,asset_1029,48.35285276,-103.7748783
4/1/2018,Fuel Gas/Start Gas,Coalescer/Filter,Regulator,,,,Fluid in red kimray knockout pot at ESD estimate to be 1/8 full. Manually drained.,user_107,asset_1114,,
11/5/2019,Plunger System,Plunger,Plunger,PCS,,Corrosion,"vent well to get plunger in. Well was loaded. Vented in plunger, caught and removed. Inspected and passed. 2 3/8 bar stock. RTP'd well",user_55,asset_515,,
4/5/2017,Gas Scrubber,Other,,Other,Other,Other,Big joe was frozen off which caused the esd to shut in ,user_100,asset_282,48.224585,-103.8291059
12/28/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,"found compressor down going through HMI @ 1st of shift-no call out-down on hi discharge froze up, there is no happy medium with this compressor, trying to keep it from going down on high cyl temp or freezing it off on the discharge trying to get the cooler set up right !!!!!!!!!!!!!!!! blew down, started let thaw out & warm up/rtp don't know how long it will last !!!!!!!!!!!!!!!!!1",user_131,asset_1869,40.7126799,-114.1193569
8/28/2019,Separator,Choke Valve/Loop,,,,Corrosion,"Upon arrival took well to tank right away, tbg psi died with in 5 minutes. Equalized well three more times and finally managed to break freeze, left choke pinched back due to 1500 psi @ tbg, will return later to check pressures and open more. Started glycol pumps, verified bath was at temp and hi/lo was holding once again. Optimizer paused open until pressures normalize then he will return to cycles.",user_177,asset_771,40.5262342,-113.8824849
9/27/2019,Fuel Gas/Start Gas,Regulator,,,,,Found pilot burning on SCC A burning but main was out. While trouble shooting while main wouldn’t open found that fisher regulator was plugged. Removed regulator took apart cleaned and replaced. SCC main now functioning ,user_18,asset_1691,,
1/31/2017,Chemical System,Pump,Packing,Sub pumper,113,Wear,Pump worn out,user_111,asset_1442,48.03781985,-103.3446106
4/23/2017,SWD System,Other,Other,Other,Other,Other,,user_117,asset_2012,36.2541889,-91.2478009
12/4/2017,Gas Scrubber Separator,ESD,,,,,"wells 150,160 were shutting in on valve fault, with colder temps here had to bump regs up, not enough psi to keep them open everyone should know to bump these up when colder temps start coming, reset/rtp wells, done walk through, SCC""s and ht trace baths good",user_131,asset_1304,40.5262342,-113.8824849
7/12/2017,Instrumentation,Tank Level,Probe,,,Weather, 4. High Point 27-60 - Replace tank switch • Replaced bad intrinsic barrier • Replaced bad tank switch • Tested and verified new tank switch working correctly • Removed bypass on HMI • Notified operations that tank is ready to flow into ,user_92,asset_1958,40.5481548,-114.0112915
2/25/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Fuel gas bath heater had pilot line freeze up again. Because our wells are so hot the fuel gas carries a lot of fluid in it. And you go from 120 degrees to ambient temp on this burner and fluids drop out then it freezes and plugs up the pilot.cleared out pilot line and relit bath. I insulated 3/8 pilot line to try and hold some heat. ,user_172,asset_1035,,
2/1/2017,Instrumentation,Transmitter,Flow,Viatram,1151,Weather,ESD actuator was stuck in mid travel. Thawed out esd valve and the actuator went to closed status.,user_65,asset_827,48.3619066,-103.2129855
6/25/2019,Sales Valve (PV),Sales Valve,Body,Valvcon,,End Of Useful Life,Salesline cyclonic valve was leaking to atmosphere and was replaced.,user_68,asset_1683,48.224585,-103.8291059
2/19/2017,Gas Scrubber,Pnumatic Dump Valve,Seat/Ball/Piston,Other,Other,Corrosion,Flow tester said kimray water dump was leaking. Pulled valve apart and found a gasket was bad and allowing it leak. Replaced gasket and returned the valve to proper working condition.,user_107,asset_1754,48.07841203,-104.8723137
4/20/2017,Compressor,Compressor,Panel,Other,Other,Other,Found compressor down on manual shut down. No sign of why it went down. Restarted compressor.,user_62,asset_1913,48.1470144,-103.6180489
11/2/2018,Sales Valve (PV),Sales Valve,Body,Valvcon,,Freezing,"Went to location to investigate well. Found sales line was open. Talked with optimizer, he got cyclonic to close part of the way. Used thaw tube on cyclonic, it finally closed the rest of the way. Talked with engineer, discussed well, and decided we would shut it in for a pressure build. I will check on it tomorrow and see if it is building pressure. If so, I will go vent it.",user_55,asset_1747,,
12/12/2017,Compressor,Intrumentation,,,,,"Off skid recycle not functional and was bursting the diaphragm in the 30 HPG control valve. The valve is regulated to a point below its maximum of 300 PSI by a pressure safety regulator on the suction sensing line, but not on the discharge sensing line. This line should have had a pressure safety regulator installed on it but was missed in the installation phase. OPS ordered the pressure safety valve and a new 30 HPG to install and return the off skid recycle valve to service.",user_6,asset_140,36.2541889,-91.2478009
3/10/2018,Flare System,Flare Header,BMS,,,,"Issue: found SCC (B) down on the HMI Root Cause: Human Error, there wasn't any (INT) it had been cleared buy someone. Then there wasn't any flow up or complete check before moving on and this was missed Fix: was able to relight remotely",user_136,asset_1305,48.2595296,-102.9010832
2/18/2018,Gas Scrubber Separator,ESD,,,,,Burp settings were erased when the PLC had a download on it I reinstated burp settings and brought wells back online.,user_51,asset_1601,48.1470144,-103.6180489
4/24/2018,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,"Issue: called out well shut in alarm (INT) valve fault Root Cause: all the wells being in off cycles so long the glycol pumps, burners, SCC used up all the fuel gas Fix: pressured pad back up turned back on left one well running to keep enough gas to keep pad pressured up ",user_136,asset_1492,48.2595694,-102.9009394
6/16/2019,Chemical System,Pump,Packing,Texam,HBC1,Wear,"packing on pump was leaking, tightened",user_31,asset_1753,43.56424,-91.351691
3/9/2018,Fuel Gas/Start Gas,Regulator,,,,,"Checked Glycol baths and burners, checked Glycol pumps, drained scrubbers and thumbed dumps. Some of the filter pots had excessive fluids in them. Also have 2 SCCs that are flashing blue in temperatures. Will write a work order to have them repaired.",user_141,asset_1921,48.1494873,-103.6217299
4/13/2019,Wellhead,Wellhead Piping,,,,hydrate,"2"" ball valve downstream casing master is not holding and needs replaced master casing is not holding either, try greasing and did not work",user_28,asset_1026,48.1605507,-103.5925275
12/11/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Sullair,,Trash,"Found the suction control manual valve closed with no notes,tags or comments on why it was shut. Compressor down on low compressor oil pressure. Possible that compressor did not see the low suction code before it shut down and threw the wrong code. Verified there is oil is compressor frame and attempted to restart, batteries only showed 8 volts and engine would not crank. Called arch out to troubleshoot.",user_54,asset_1833,48.1470144,-103.6180489
3/29/2019,Separator,Choke Valve/Loop,,,,Freezing,"Dvc sticking not allowing choke to open, tapped on dvc, choke opened and well began flowing. ",user_44,asset_2024,,
9/28/2017,Tanks/Pits,Liquid Level Control,,,,,761466 showing a false high level of 19' actual is 3'6,user_11,asset_1240,48.1470144,-103.6180489
9/25/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash,,user_58,asset_1574,48.40521556,-103.5811397
11/14/2017,Tanks/Pits,Valving/Swedges,Body,,,Trash,"Found heat trace to tanks not pumping. Found heat trace valve at tanks closed, causing pump to stall. Opened valve and pump started working.",user_62,asset_1108,48.1470144,-103.6180489
6/22/2018,SWD System,Particle Filter,Element,,,,Replaced filters and RTP'd pump,user_141,asset_1633,40.5960545,-113.9323891
10/10/2019,Separator,Choke Valve/Loop,,,,Freezing,"Found pad had shut in on low glycol level 44”, contacted team lead and got the go ahead to drop lo lo setting to 42” until glycol is topped off. Jumped pad back on lit burners and SCCs tested all dumps and drained Desi and fuel scrubber. Submitted 3rd request for glycol top off on this location.",user_18,asset_171,,
10/9/2019,Chemical System,Pump,Packing,Goulds,HBT2,Wear,The methanol pump was leaking out the packing. It was replace with a rebuilt pump.,user_68,asset_507,41.474544,-90.6778637
2/3/2019,Surface Location,Lease Road,,,,Weather,Leas road to location is drifted in and caused water haulers to not be able to make it to location which caused pad to go down on HIGH HIGH water tank alarm pad is shut in currently.,user_159,asset_787,48.1508,-103.6191904
3/13/2018,Flare System,Flare Header,Instrumentation,,,,Issue: found # 3 SCC down Root Cause: the pilot gas solenoid isn't working. I made sure the pilot was plugged and the line was open it just isn't enough pressure through the solenoid. Fix: waiting on the work order to be completed ,user_136,asset_2034,48.1470144,-103.6180489
3/30/2019,Separator,Dump Line,,,,Freezing,"Walked down location and found water dump frozen broke freeze and cleared dumps .Found sales line shut in at the dehy contacted William tech to open sales line , rtp'd well after Williams got there sales line open. drained all scrubbers on location and replaced snap dump on the 160 well on this well . ",user_10,asset_1063,46.2356189,-100.6010498
3/22/2018,Plunger System,Plunger,Plunger,IPS,,Corrosion,Well producing about 40 mcf low so I inspected the plunger and replaced it and talked to Brett about adjusting cycles to maximize the production of this well,user_100,asset_28,48.1470144,-103.6180489
2/20/2018,Gas Scrubber Separator,ESD,,,,,"HP 23-40 high unit pressure callout lateral is froze, dehi at 900 PSI. shut in wellhead and blew down separator. ",user_71,asset_2154,48.1470144,-103.6180489
3/23/2018,Flare System,Flare Header,Instrumentation,,,,Looks like there was an automation issue. Had to relight all 4 SCCs and 3 glycol bath heaters,user_141,asset_1240,48.1004963,-103.5858235
10/1/2019,Heat Medium,Pump,Seals,Texam,HBC1,Wear,Diaphram pump for heat trace on the 27 10 well failed. Please replace ... Graco 1040 Completed ,user_5,asset_631,38.4425988,-95.5406131
11/21/2016,Wellhead,,,,,,"2"" tubing KF valves leaking through stem",user_105,asset_1331,48.09116484,-103.6579404
8/23/2017,Plunger System,Plunger,Plunger,IPS,,No Liquid,"Well loaded,vent",user_111,asset_1645,48.03877204,-103.4295565
11/19/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,"comp down on hi discharge again, blew everything down, acted like it was still freezing off in discharge line, pretty cold, 14 ambient and 20 mph, don't help, started up and let warm up and recycle to thaw out for awhile, RTP,. checked baths, wh comp, and drained liquids from controllers, this comp is like clock work when it hits this temp every night ",user_131,asset_1350,40.7126799,-114.1193569
11/2/2018,Compressor,Cooler,,,,,"possible freeze in cooler, checked louvers ",user_144,asset_1623,48.1470144,-103.6180489
10/4/2019,Automation,Antenna,,Bluewave,,Electrical Short,Pad is locked up in hmi cannot bypass or clear interlocks attempted to power cycle with no luck. Spoke with Justin Rodriguez and he did not know what was going on informed me that we would have to wait until mike Edwards returns ,user_18,asset_446,,
2/20/2018,Compressor - Gas Lift,Engine,Cooler,Caterpillar,,Freezing,"Compresor down on High 2nd stage pressure, found hydrate within 2nd stage cooler. Could not get compressor to restart kept going down on low/lost RPM stall. Used heater, put on tube on the engine block/ compressor block and the other to heat the building. on 2-19-18, on 2-20-18 started compressor on 2nd try, warmed up unit, based on cylinder temps hydrate has been cleared out, pad still not flowing due to freeze in WFS dehy, once cleared can RTP the pad",user_115,asset_1264,,
1/11/2019,Surface Location,Well Pad,,,,Weather,"Micro turbine issue caused supply air to fail. Location froze up. Micro turbine issue resolved by automation. Pad brought back on but burners reset to low setting. Reset burners to 110 degrees, restarted down pumps. Vessels in cabinet remain frozen",user_17,asset_1827,48.19846318,-103.4818708
1/1/2018,Pipeline/Piping,Pipe/Components,,,,Human Error,Weekend shift left valves closed on bath heater and forgot to reopen. It is open now and burners are on.,user_0,asset_1841,48.1606624,-103.6173175
1/16/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Replaced bar stock plunger for a dual pad, the plunger had lost arrivals and was under specc when pulled out for this well. Also this well does not have sanding issues and does not flow often enough to put it into the drop rate range of a bar stock and sets is firmly in the dual pad range of off time. This well also carries a fair amount of fluid and a better seal should help it unload as well as require less frequent change outs.",user_6,asset_1473,36.2541889,-91.2478009
8/23/2019,Plunger System,Plunger,Plunger,PCS,,Corrosion,inspect plunger and replaced mic. 1.87 / installed new bar / rtp'd well,user_10,asset_71,40.5262342,-113.8824849
8/24/2019,Plunger System,Plunger,Plunger,PCS,,Corrosion,vented plunger to surface/ inspected and replaced mic. 1.84 . Rtp'd,user_10,asset_1428,40.5262342,-113.8824849
10/5/2018,Separator,Fuel Supply System, Big Joe Regulator,Fisher controls,,freeze,Found big joe was frozen and not allowing pressure to reach the burner valve. Thawed out big joe and restarted burner,user_10,asset_736,43.252261,-115.0567324
2/2/2017,Gas Scrubber,Dump Line,Dump Line,Other,Other,Trash,Produced water dump line froze and needed to be thawed.,user_161,asset_328,40.5481548,-114.0112915
12/15/2017,Automation,Antenna,,Bluewave,,Loose Connection,"radio switch was stuck, power cycle",user_39,asset_1572,48.1603023,-103.6174272
9/29/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,Changed 3 Load line valves and removed Load line,user_173,asset_21,48.1603344,-103.6174373
8/31/2018,Flare System,Flare Header,BMS,,,,Fire out on SCC. Relit and put back in service.,user_55,asset_1873,,
11/9/2017,Separator,Choke Valve/Loop,,,,Freezing,Glycol pump stalled,user_126,asset_858,,
5/1/2018,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,CB 7-pad high tank alarm tank #761360 at 17-1x1-8 already switched ,user_71,asset_1704,48.1470144,-103.6180489
3/8/2019,Separator,Dump Line,,,,Freezing,"Shut well in for winter. Checklist done. Wellhead valves closed. Flowline blown down. Dumps froze, all tanks froze. Lower FMC at separator closed. Cannot close in dehy due to some separators still having pressure on them. ",user_55,asset_993,,
7/2/2019,Instrumentation,Meter,Orifice Plate,Control Micro,4203DR,End Of Useful Life,Found Meter had a Blown Fuse and Lost MVT Configuration; Found Damaged Lighting arrestor; Replaced damaged components and tested thru SAMS.,user_139,asset_2267,,
4/9/2017,Wellhead,Other,,Other,Other,Other,,user_179,asset_1025,48.0108657,-103.5016001
10/30/2017,Wellhead,Choke Valve,Body,,,,check and drained fuel pot going into dvc. there was none. gave dvc a love tap and choke started working,user_11,asset_1228,48.1470144,-103.6180489
2/7/2018,Compressor,Compressor (Recip),Valves,,,,"Found compressor went down on 2nd stage discharge valve temp. Restarted compressor and monitored valve temps. after 20 mins of running, 2nd stage discharge valves were at 119 degrees and 128 degrees After 40 mins of run time, valves were at 151 and 154 Lost the air compressors and had to restart whole pad again Got everything going then got called to go assist MAINT ",user_53,asset_1945,40.7126799,-114.1193569
8/28/2017,Instrument Air,Dryer,Shell,,,,"filter housing broke due to sun damage and pressure, lost 3 esd because of blowing air, replaced housing and rtp wells",user_87,asset_634,40.7126799,-114.1193569
3/7/2017,SWD System,Other,Other,Other,Other,Other,,user_117,asset_101,36.2541889,-91.2478009
8/5/2019,Separator,Liquid Level Control,,,,,"Dispatched to location. Both 80 & 90 had been shut in for high tank, water tank had been hauled. Reset cycles and RTP. Flowing wells out before doing cycles. SCC was out, relit. Removed jumper that was going scrubber to scrubber, scrubber was ball checked on the 80 well. Adjusted to condo dump on the 90 well, level was in top sightglass. Flowed pressure off the 90 well and started cycles",user_31,asset_480,43.56424,-91.351691
1/5/2017,Automation,,,,,Other,Loss of production ,user_163,asset_1205,47.88192295,-103.4771055
2/24/2019,Flare System,Flare Header,Regulator,,,,"Flare down due to wind, pressure are set to appropriate pressures. ENG to work with AUTO to hook igniter cable back up, 30 minutes to manually lower flare pilot boom in order to light flare. ENG to work solution to keep pilot from blowing out in high wind situations.",user_54,asset_1383,46.2356189,-100.6010498
2/20/2019,Surface Location,Lease Road,,,,Weather,"The access road, turnaround and the surface equipment needs snow plowed or removed.",user_68,asset_259,48.1470144,-103.6180489
2/10/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,"call out compressor down-gl down hi discharge, blew everything down, acts like a cooler freeze, left it opened up while I went to bring the tr15-140 back up, came back and started compressor to warm up, had to fight it fow quite awhile to cooler freeze broke and then there were freezes in flow lines also at the 10 & 150 inlet, finally got those broke tried adjusting the auto louver closed a little more but the t-12 won't let it adjust just right it goes all the way closed and then the cyl temps go up, opened back to where it was these temp swings are bad again",user_131,asset_1350,40.7126799,-114.1193569
3/23/2018,Instrumentation,Communication Card,,,,,Issue: found well down on the HMI (INT) watch dog timed out Root Cause: the RTU's keep quit talking to each other Fix: i kept resting it and turning the well back on but i wrote a work order for automation to take a better look at it,user_136,asset_1477,48.0614644,-104.8417043
2/28/2017,Automation,RTU,Relay,Other,Other,Other,,user_138,asset_1175,48.13611606,-103.478048
2/14/2018,Compressor,Compressor,Process Gas Supply,Gemini,,Freezing,Found gas lift compressor went down on high discharge pressure. The recycle had ice on it leaving me to believe we froze off from recycling gas. Verified there were no freezes on the injection side of the well by blowing the casing down. No indication of a freeze. Started the compressor and began injecting. Waited for ~30 minutes to ensure the pressures weren’t climbing on the discharge side of the compressor. ,user_50,asset_247,48.36796026,-103.5269405
3/28/2018,Separator,Temp Control System,Pilot,,,,Debris plug in pilot cleaned out and relit burner system,user_109,asset_1432,48.1007075,-103.468193
2/13/2019,Pipeline/Piping,Valves,,,,End Of Design Life,"valve was hard to operate, so we added a new balon valve ",user_28,asset_2145,48.160305,-103.6188078
4/11/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Vented well due to being loaded. Plunger arrived, RTP'd well, started cycles, and return to optimizer.",user_141,asset_553,48.1470144,-103.6180489
5/11/2018,Flare System,Flare Header,Instrumentation,,,,"CG 5-20 SCC callout, relit SCC C.",user_71,asset_1705,48.1470144,-103.6180489
10/18/2017,Automation,Plunger Arrival Switch,,EDI,,,Cyclops mso was bad. Replaced. ,user_30,asset_1734,47.9426073,-103.6978675
6/8/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,has missed last several arrivals I went to location I tried to surface plunger it did not come in I restarted cycles I will try to make it back tonight,user_51,asset_613,48.1470144,-103.6180489
8/30/2019,Separator,Choke Valve/Loop,,,,Corrosion,"Replaced HI/LO trim set and seat. When I did winterization found it leaking, but didn't have the parts to repair. ",user_55,asset_1896,,
6/20/2019,Separator,Valves,,,,Corrosion (Internal),"RTP checklist performed by Ken Boswell on 20-June-2019. Williams was contacted through Josh Parker to ready the dehy. Well will need to be RTP's onsite as there are outstanding repairs that operations will need to make during RTP. The pilot regulator on the fuel supply line to the B separator needs replaced. The trim set on the dump on 60 well needs rebuilt. It appears the trim is broke off. It will not dump when actuated. The SCC enardo at the SCC's needs the gasket replaced as well as gauges on the SCC regulators on main and piilot. The 60 well needs the 2'"" drain valve replaced. The 110 needs the check valve on the dump line replaced as well. Coding to operations as this work can be completed by operations and the ETA to dehy readiness is 21-JUNE-2019.",user_66,asset_679,,
11/19/2017,Compressor,Compressor (Recip),Process Gas Supply,,,,"comp down on #21 again low 1st stg discharge psi, blew everything down, acted like it was still freezing off in panel tubing lines,and running out of suction, i used to run this compressor with all 4 valves open from 4 packs to keep better suction the way this unit was originally set up and some one had closed the other valves, i opened them and suction PSI got better again and its pretty cold, 14 ambient and 20 mph, don't help, started up and let warm up and recycle to thaw out for awhile, RTP,. checked baths, and drained liquids from controllers, SCC's in service",user_131,asset_1346,40.7126799,-114.1193569
9/2/2019,Dehy,WFS Issue,,,,,High line pressure causing well to defer,user_56,asset_931,40.5262342,-113.8824849
5/24/2018,Wellhead,Manual Valve,Body,,,Erosion,"Well was shut in and tagged during WFS TAR for maintenance to remove compressor and install new one. Contacted Site manager for permission to remove tags. Received permission, removed tags and opened well head valves to begin flow.",user_62,asset_1270,40.7126799,-114.1193569
3/1/2018,Automation,RTU,Wiring,Schneider/Scadapack,Scadapack P4,Human Error,Someone disconnected power wires during wellhead auto and meter install. ,user_30,asset_2157,48.10839359,-103.6114991
11/26/2017,Compressor - Gas Lift,Engine,Vibration Switch,Ajax,,Vibration,,user_156,asset_521,48.22010894,-103.5964779
4/29/2019,Separator,Fuel Supply System, Big Joe Regulator,Fisher controls,,wear,"On location to RTP, pad was shut in on WFS lateral freeze. All separators no pressure and cold. Opened up buy back and got burners going on 90, 100, 140, 160 wells. 160 well pilot was plugged, cleaned out and RTP. 140 well RTP, 100 well rebuilt big joe and and hi low was leaking, replaced trim set, found bonnet to be leaking left shut in until tomorrow. 90 well is frozen or super loaded. The rest of the pad needs lots of attention to RTP",user_31,asset_647,48.257296,-102.863888
3/28/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,fluid,Site visit resulted in draining the desi. The front end filters were all dry to the chokes and the dvc's. Cold fingers seem to be having positive results in keeping the fluid out of the supply gas system or a buy back meter would be beneficial on this site due to a small number of wells with upstream control valves.,user_50,asset_1050,48.1507681,-103.6208284
1/24/2017,Automation,Battery,Battery,Interstate,Other,End of Useful Life,No damage. Generator on site. Batteries are old and no longer charging properly. Causing communication issues. Batteries need replaced,user_30,asset_92,48.09981387,-103.6534773
12/19/2017,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,Issue: pad called out shut in Root Cause: all the wells in off cycles at the same time units ran low on unit pressure and shut in Fix: need to get the buy back line in service. turned pad back on ,user_136,asset_1449,48.1470144,-103.6180489
2/13/2018,Flare System,Flare Header,BMS,,,,"scc out, had to clean one pilot tip. 4 sccs on location",user_84,asset_1423,48.1470144,-103.6180489
11/27/2017,Instrumentation,Controller,,,,,I shut sales valve for a 24hr pressure build per operator request until cyclonic actuator gets fixed,user_51,asset_1163,48.1470144,-103.6180489
4/4/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,fluid,Well called out on con valve alarm I went to location and cleared scrubber there was a little bit of fluid which cause the three way valve to fault.,user_51,asset_1973,48.1470144,-103.6180489
10/23/2018,Wellhead,Casing,Intermediate Casing Head Valve,,,,Arrived on location and walked down all the equipment to ensure everything was in good condition. Identified tags on the wellhead and choke highlighting previous issues. Recived permission to remove the tags and attempt troubleshoot. Casing has 13# on it indicating a freeze down hole. Opened up to the tank to see if we could break it. Jumpered gas from Williams so we could get Methanol pumping down the casing. Will follow up in the morning,user_59,asset_245,43.252261,-115.0567324
11/3/2018,Automation,RTU,,ABB,,Weather,casing transmitter full of ice and water,user_22,asset_2136,43.252261,-115.0567324
2/20/2019,Surface Location,Lease Road,,,,Weather,"Unable to access location due to deep snow drifts in spots, got stuck but was able to get out. Did not want to try and proceed any further. Coded to down weather waiting on maintenance. ",user_44,asset_209,,
11/29/2017,Fuel Gas/Start Gas,Regulator,,,,,Issue: Well shut in on low unit pressure Root Cause: all wells were in off cycles at same time for to long and well shut in on low unit pressure Fix: to relook at the cycles and not have all the wells in off cycles a the same time. long term fix is a buy back meter,user_136,asset_113,48.1602546,-103.6172966
2/1/2019,Heat Medium,Pump,Valves,Sunpumper,113,Weather,the old heat trace at the well head was leaking. Replaced with new heat trace and re insulated the whole well head,user_21,asset_2147,44.2489295,-118.0582155
9/6/2018,Separator,Fuel Supply System,Regulator,,,wear,"plastic filter pot blown apart causing pad to go down on low air supply. Replaced filter pot, rtp",user_64,asset_600,48.1470144,-103.6180489
2/27/2017,SWD System,Other,Other,Other,Other,Other,No damages.,user_117,asset_422,,
3/30/2018,Separator,Fuel Supply System,big joe regulator,,,wear,Found leak at the button/nipple service break. Uneven tightening at last button change out. Replaced button and nipple and reinstalled making sure to tighten evenly. No leaks observed,user_163,asset_1986,48.1470144,-103.6180489
5/27/2018,Wellhead,Wellhead Piping,,,,hydrate,gas lift is running but i did break down hole freeze in casing on 10 well. rtp'd,user_11,asset_2055,40.7126799,-114.1193569
7/21/2018,Automation,RTU,Relay,ABB,Bristol 3310,Wear,"Red wash 3-1 high unit pressure callout, well is shut in and dehi is TD with outlet locked.",user_37,asset_978,48.1499168,-103.6211877
9/23/2019,Heat Medium,Pump,Seals,Texam,HBC1,Wear,Changed out pumps,user_5,asset_946,38.4425988,-95.5406131
4/22/2019,Wellhead,Cyclonic Valve,Actuator,,,Freezing,No issue. Torque limit functioned correctly. Operator apparently did not know how to clear it.,user_12,asset_120,40.5262342,-113.8824849
10/25/2017,Instrumentation,Controller,,,,,"Called Eric, he got it fixed",user_84,asset_2139,48.04926098,-103.4870497
12/7/2018,Separator,Liquid Dumps,Float,Norriseal,,Freezing,condo dump frozen ,user_121,asset_1928,48.3580576,-83.27272
7/17/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized," Vent plunger in. Inspect and replace, bar to bar. RTP well Plunger had a very different wear pattern. Body was worn on one side.",user_141,asset_2201,48.1506685,-103.6208952
2/18/2018,Gas Scrubber Separator,Dump Line,,,,Freezing,CL 29-50 checked site drained scrubbers everything looked OK relit SCCs and flare.,user_71,asset_1800,48.1470144,-103.6180489
4/5/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Plunger missed arrival because of small line bump vented plunger ,user_100,asset_2032,48.1470144,-103.6180489
7/19/2017,Compressor,Compressor (Recip),Process Gas Supply,,,,Down on low interstage 2 psi /rtp'd ,user_131,asset_1350,47.99777862,-103.7121393
5/13/2018,Automation,RTU,Relay,Schneider/Scadapack,Scadapack P4,Weather,"Luman 33-2 SCC callout, site shut in. ",user_71,asset_2243,48.1470144,-103.6180489
12/8/2016,Gas Scrubber,,,,,,"Every dump on location frozen, baths and pumps running ",user_87,asset_396,47.9506634,-103.4211705
11/12/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,"suction line to compressor froze, probably caused by solar glycol pumps being off",user_31,asset_1623,48.2717879,-102.8687171
7/25/2019,Separator Inlet Valve (XV),Controller,,,,,"After arriving on location found unit up but only had 133 psi with hi/lo shut. Spoke with optimizer to verify there were no shut ins on well and to open cyclonic. After cyclonic opened hi/lo opened and well began to flow, optimizer shut cyclonic and once vessel reached 600 psi hi/lo shut but once pressure began to drop never opened back up. Found block & bleed leaking along with dixon fuel gas regulator blowing out. Changed block & bleed and fuel gas regulator, opened supply and hit test on fisher controller, hi/lo then began opening and closing as it should and new regulator did not leak. Optimizer informed me well was flowing good with consistent production but found williams meter was not reading a flowrate, spoke with Mario with williams he is going to get their measurement team to repair it. Our meter is reading accurately and reporting in, it was only showing zero production due to hi/lo not opening.",user_177,asset_2099,39.2506642,-92.4357879
12/7/2017,Separator,ESD Valve,Gas Sensing Line,,,Liquid Plugging,Drained fuel gas to ESD and brought well back online and started plunger cycles.,user_51,asset_1783,48.1470144,-103.6180489
3/6/2018,Separator,Liquid Dumps,Controller,Norriseal,,Improper Adjustment,"Condo dump was leaking, checked and adjusted.",user_48,asset_596,48.22140826,-103.563433
1/19/2019,Tanks/Pits,Liquid Level Control,,,,,+ ROGER VERIFIED HIGH WATER TANK --**SEPARATOR ALREADY SHUT IN SO ROGER SHUT IN THE DEHY LINES TO TANK,user_34,asset_1026,43.56424,-91.351691
3/13/2018,Compressor,Intrumentation,,,,,"Compressor was shut of for production test, Engineering team requested that the compressor be re-started. Arrived on location and found compressor off, inlet shut and tagged and batteries shut off. walked through all piping and made sure all valves were in proper order to start and run compressor. Started and warmed compressor, loaded compressor. As i was kicking wells on and off, I heard compressor decrease in RPM. This is a set point in the electronics to decrease RPM's when suction pressure gets low to avoid the compressor going down. Root cause of low suction, I looked over the off skid recycle and found the jam nut for setting the recycle valve was not locked down and the HPG30 backed out from vibration. I looked at the set points for the compressor and the suction set points were 40 low and 80 high. Suction valve was set for 70 PSI. I set the recycle valve to 55 PSI, tested it and its working good. Set the jam nut to prevent compressor vibration from backing it out.",user_62,asset_1124,48.1470144,-103.6180489
4/17/2019,Pipeline/Piping,Valves,,,,Corrosion (Internal),none,user_157,asset_1965,46.2356189,-100.6010498
10/21/2018,Tanks/Pits,Flare/Combuster,,,,,"pilot out, took apart and cleaned out, relit",user_31,asset_816,43.252261,-115.0567324
3/12/2018,Wellhead,Casing,Lower Casing Head Valve,,,,Blow down casing on #3 injection well,user_141,asset_101,48.1470144,-103.6180489
11/7/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Got a bath heater shut down call out went to location and found the the solenoid for the burner control valve had a freeze in the supply line and would not open. Thawed the solenoid for the burner management system and valve started working . Restarted burner and waited for it to get to temp.,user_100,asset_77,48.1470144,-103.6180489
2/2/2017,Automation,Other,Other,Other,Other,Other,Unknown damages caused RPOC to quit reading rod string weight for rod pump. Replaced motherboard and load cell card. Re-programmed. Fixed,user_30,asset_599,48.16042983,-103.617722
2/2/2018,Separator,Choke Valve/Loop,,,,Freezing,"Thawed DVC and checked operation of choke. Vented well due to being loaded. Plunger arrived, RTP'd well, started cycles, and return to optimizer.",user_141,asset_1348,48.1470144,-103.6180489
3/9/2019,Separator,Choke Valve/Loop,,,,Freezing,Well was shut in for bad dump a few days ago. In between the line heater and high pressure unit was froze due to no heat trace and cold temps. Thawed with heater. ,user_15,asset_787,48.1147552,-104.1197216
2/27/2019,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"Dispatched to pad, I knew that this pad was down and has been down for a few weeks. Pulled into location and saw JW onsite working on the compressor. Spoke with the tech and found out that the batteries were dead. I contacted leadership to have them run me down 2 boostpro's Onsite i found that the line heater was up and warmed up, found only one solar glycol pump working. Notified Travis 90 well, I found that burner was off, unit had pressure in it so i started burner and got bath warming up. After getting burner lit i checked both dumps and found that the condo dump was clear to the tank and that the water was froze. Started to thaw on the water dump line as well as the unit blow down. After thawing for 2.5 hours i got the water line cleared to the tanks. Proceeded to troubleshoot well and found that TBG had 130 and CSG had 800. Decided to vent well, got it cleaned up and put well back on cycles. RTP'd 90 well 85 well, found this unit completely down, TBG has 1244 and CSG has 844. Decided to jump this unit from another unit to eliminate having the TBG opened to the unit. After jumping it i was able to get the burner stared and then i checked the dumps, both dump displacers were froze in the unit. Started thawing on the shell of the vessel. First i did get the water displacer free. 165 well, found this well online with the unit warm but it is loaded and is waiting for the compressor to be stared. Compressor is down on low engine jacketwater level and possibly the batteries but i am charging them right now. This well will be RTP'd once i can get the compressor running. I need to come back to location tomorrow to get gas lift running and get it all back on. ",user_56,asset_546,48.224585,-103.8291059
4/25/2018,Compressor,Cooler,,,,,"hole is cooler leaking gas , contacted arch rock, depressored compressor and tagged out",user_122,asset_1323,48.1470144,-103.6180489
12/13/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Liquid Carryover,"Compressor went down due to low suction, the Williams dehy was not running and we were getting a lot of fluid to the compressor from Williams. After the dehy was up and running, i got the compressor running and verified that it stayed up and going. everything is functioning properly on location and we are not sure why the dehy flooded over. Well RTP'd",user_24,asset_387,48.1470144,-103.6180489
7/18/2018,Wellhead,Tubing,,,,,"Checked lubricator for plunger. Not there. Worked with optimizer to kick well on and off. Plunger coming very quick. Shut well in, listened through master valve. Sounds like plunger is falling 50 to 100 ft. Will give to engineer.",user_55,asset_1572,40.5262342,-113.8824849
11/10/2017,Tanks/Pits,Tank Level,Probe,,,Calibration Issue,Water tank at 15' called in before weekend,user_126,asset_1791,,
1/14/2019,Fuel Gas/Start Gas,Regulator,,,,,Fuel gas frozen,user_153,asset_1634,48.30304367,-103.6608807
5/10/2018,Compressor,Compressor (Intergral),Scrubber Level,,,,"Luman 8-115 SCC callout. SCC C out on thermocouple error, automation will need to check. Comp and flare were down, comp was down on high second stage scrubber level no fluid in scrubber, relit flare with igniter.",user_71,asset_1317,48.1470144,-103.6180489
1/29/2018,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,Load line changed out,user_60,asset_1356,48.1470144,-103.6180489
8/22/2019,Plunger System,Plunger,Plunger,IPS,,Corrosion,Plunger found to be undersized. Replaced with new bar,user_153,asset_1601,48.0407455,-103.5396458
10/30/2017,Plunger System,Plunger,Plunger,PCS,,Not Optimized,this plunger is only 16 days old and bath burners are going cycles need adjusted or at least looked at,user_11,asset_80,48.1470144,-103.6180489
7/12/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,Load valves leaking by,user_165,asset_710,40.5481548,-114.0112915
7/11/2018,Plunger System,Plunger,Lubricator Top,IPS,,Corrosion,ARROW SEPARATOR LOST PRESSURE SUSPECT DUMP MIGHT HAVE STUCK IPS BOWEN LUBRICATOR CAP O-RING LEAKING WHEN I ARRIVED ON LOCATION REPLACED O-RING PLUNGER VENT UNSUCCESSFUL DUE TO LEAKING O-RING THE WELL IS BADLY LOADED. SIPB NEEDS AT LEAST 1000PSI ON CASING TO VENT PLUNGER TO SURFACE,user_163,asset_450,43.252261,-115.0567324
12/12/2017,Pumping Unit,Motor,Bearings,,,,"Access road locked gates had been accidentally preventing access to well site, shortened chains to prevent accidental lockout.",user_161,asset_2170,48.2645815,-102.9262129
10/20/2019,Gas Scrubber Separator,Dump Line,,,,Freezing,"Drained the Dezi took about 3 seconds, drained the scrubbers, drained all the drip pots, all the pressure regulators, Thumbed the dumps and checked bath temp.",user_76,asset_809,46.2356189,-100.6010498
1/14/2019,Instrumentation,Meter,Orifice Plate,Control Micro,4203DR,Recalibrated,Scheduled Calibration,user_139,asset_586,,
12/8/2017,Instrumentation,Controller,,,,,kelvin ,user_53,asset_1924,36.2541889,-91.2478009
7/18/2019,Compressor - Gas Lift,Compressor,Instrument Gas Supply,Ariel,,Trash,Gas lift #1 down on high suction pressure I found that the offskid recycle bleed was cracked open which caused the recycle to open I shut the bleed and brought the gas lift back online.,user_159,asset_1833,43.56424,-91.351691
2/27/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,Use steamer to thaw load lines,user_125,asset_1417,46.2356189,-100.6010498
3/8/2018,Wellhead,Casing,Intermediate Casing Head Valve,,,,well valves are frozen all of the top flow path can not turn valves to equalized we do not have meth going to well head the because the meth pump controlling panel is messed up automation has came out and looked at it needs some different parts to fix then will be able to break freeze in well head and rtp well,user_110,asset_168,36.2541889,-91.2478009
2/11/2018,Wellhead,Tubing,,,,,"Found a freeze in flow line. Closed separator and opened well to tank. Freeze broke, RTP'd well.",user_141,asset_858,48.1470144,-103.6180489
1/30/2018,Flare System,Flare Header,Instrumentation,,,,Issue: found SCC (A) down on the HMI Root Cause: (INT) no pilot flame Fix: relight and returned to service ,user_136,asset_364,48.1470144,-103.6180489
4/30/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,got plunger to come in. i didnt inspect due to donnie telling me he has changed this plunger out last week,user_11,asset_165,40.7126799,-114.1193569
8/31/2017,Instrumentation,Transmitter,Temperature,IPS,1151,End Of Useful Life,,user_113,asset_971,48.18202589,-103.6141701
8/9/2018,Wellhead,Tubing,,,,,"Well is deferring 35mcf, looks like it could is loading up. TBG was at 323 CSG was at 539 Vented well for 15 mis Put back on cycles Comms have been in and out on location, will monitor well RTP'd",user_56,asset_1636,48.1470144,-103.6180489
8/10/2018,Instrumentation,Communication Card,,,,,comm error shut well in on false alarm,user_144,asset_1661,48.1470144,-103.6180489
3/6/2017,Compressor,Compressor,Other,Other,Other,Other,Rtp'd ,user_58,asset_2148,47.95068343,-103.3853789
1/14/2019,Heat Medium,Pump,Process Indicator,Sunpumper,113,Weather,"2 cold glycol flow paths, adjusted valves and got warm glycol moving",user_31,asset_1055,43.56424,-91.351691
5/24/2018,Tanks/Pits,Flare/Combuster,,,,,"Well was shut in and tagged during WFS TAR for maintenance to remove compressor and install new one. Location was brought back on, Lit SCC C",user_62,asset_1352,40.7126799,-114.1193569
11/1/2016,Automation,,,,,Other,,user_92,asset_1489,48.16508753,-103.6812487
4/4/2017,Wellhead,Primary Choke,Stem/Seat,Other,Other,Other,Well shut in and wasn't flowing causing lost production.,user_141,asset_2157,48.0614644,-104.8417043
1/9/2019,Separator Inlet Valve (XV),Pneumatic Control System,Regulator,,,,"worked with engineering , 140 well was not flowing , found cold finger froze and liquid in the dvc controller , worked with automation , thawed out cold finger and dvc , got choke to control ",user_144,asset_2024,48.1470144,-103.6180489
6/15/2017,Pipeline/Piping,Valves,,,,End Of Design Life,"Rebuilt manual choke and replaced (2) 1/2"" needle valves that would no longer open/close",user_150,asset_609,,
2/2/2017,Automation,RTU,Relay,Other,Other,Other,Bad unit pressure transmitter. Well is in interlock and won't clear ,user_175,asset_312,47.90549412,-103.597041
6/24/2018,Automation,Radio,Wiring,Cellular,,End Of Useful Life,This is for SixNet ES-5MS network switch. ,user_134,asset_1225,48.1605156,-103.6206521
12/30/2017,Heater Treater,Burner,BMS,,,Loss Of Fuel Gas,"call out bath temp high alarm, went and adjusted",user_131,asset_1790,40.7126799,-114.1193569
4/18/2018,Separator,ESD Valve,Actuator,,,Liquid Plugging,Drained regulator for the esd and adjusted supply gas / opened esd and rtp'd well,user_100,asset_1938,48.1470144,-103.6180489
1/5/2017,,,,,,,Well vented back to production,user_35,asset_160,48.08573387,-103.5259704
11/17/2017,Automation,RTU,Relay,Vinson,Bristol 3310,Loose Connection,"had Brett reset cyclonic, it worked so was able to air up unit and is now rtp",user_176,asset_397,48.1470144,-103.6180489
12/4/2017,Compressor - Gas Lift,Engine,Water Pump,Cummins,,Controller Failure,"call out compressor down, GL down on high discharge, all froze up, trying to thaw, went to start to warm up & recycle and flagging low jacket level,LB showing 5.5"" RB showing 8.5""-there is not any coolant in any of the compressor buildings, wiil have to try and find some or call vendor to come out.",user_131,asset_1264,40.5262342,-113.8824849
10/26/2018,Separator,Choke Valve/Loop,,,,Trash,"Found well had been missing arrivals since 10/18, looks like plunger is frozen in the cap. Thawed out cap and got plunger to drop, inspected plunger and installed new bar plunger function tested MSO and its working fine. Dropped new plunger and made sure plunger made arrivals. Found all glycol baths on location set at 60 degrees adjusted bath temps up to 85.",user_10,asset_955,43.252261,-115.0567324
1/29/2019,Flare System,Flare Header,Regulator,,,,"Issues: found SCC # 4 down Root Cause: the fuel gas to the SCC's is wet from the wells flowing warm and having liquid carry over. So when people come to sight and see the heat trace is cool because the wells flow so warm they turn up the T-12's to make the heat trace warmer and in turn cause the carry over to get worse. To go along with that they made U in the line that catches fluid with no way to drain it and there is 40' of exposed pipe with no heat trace or insulation to protect it. Fix: i was able to drain the line as best as i could. as for the carry over we should never regulate pressure at the SCC's that far away from any heat source, There should never be a U installed on purpose that doesn't have a drain, insulation, heat trace. As far as the flowing temps are i tried to get the glyocl pumps installed at the line heater so the baths could run cooler but the decision was made not to do the up grade. ",user_170,asset_247,48.264857,-102.9014931
2/15/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Sertco,,Freezing,"Restarted compressor, thawed on discharge meter and attempted to restart injecting. Waiting for methanol to get delivered and also getting a hold of measurement to check meter out",user_58,asset_247,48.36810979,-103.5273201
12/8/2018,Pipeline/Piping,Pipe/Components,,,,hydrate,"Following up with Redi crew to check dumps. They got all the dumps open. While dumping the dezi, heard some water flowing. Turned around and it was coming out of the dump line in front of the 77 water tank. Took a closer look, and found that line had parted from hammer union. Contacted Henry, and advised of what I found. Contacted IBEX to dispatch a truck to start cleaning up water. Shut inlet valves to tanks, leak stopped flowing, mostly. Went and started shutting all dumps. Found 1 dump stuck, on the 80 well. Will write a work order. Found the dump on the 50 well leaking by, will write a work order. Flagged all valves with orange flagging (I'm out of orange tags and so is the warehouse. I closed and flagged 3 sales line valves in an effort to keep pad up and warm. Those are the 90, 40, and 20. IBEX on scene cleaning up water. They will pull all water tanks down below inlet valves to assist with repairs. I will write a work order for that.",user_55,asset_317,,
8/30/2019,SWD System,Particle Filter,Element,,,,"1 duck on west cell. Opened up valve more to pond, level at 14'. Slowed injection pump #4, pinched valve to pit, level at 10.6. IBEX skimming west cell. Leak detection and monitoring wells gauged. 8/29/2019 opened valve on evap tanks to drop level then pinched it at quitting time. Increased flow on #4 injection. Steam cleaner on site to clean out drains in offload buildings. Leak on 5K tank valve, leaking about 1 gallon every 4 hours 8/30/2019 5K tank has about 2' of oil, south evap 5K has about 1' oil. Both condo at south evap are mostly mud, turned in to be emptied. Changed filters at WDW #4 east set",user_31,asset_308,48.1470144,-103.6180489
1/25/2018,Heater Treater,Burner,Flame Arrestor,,,Pilot Went Out,"Found fluids in the fuel gas lines which cause the I2P-100 valves issues. Opened it up and removed the filter, cleared the fluid out of the automation and connecting structure. Filter bottom metal piece fell off during removal, so it needed to be replaced. The D-4 is still not acting appropriately, after a discussion with AUTO tech this was turned to OPT to get with M. Edwards to look at possible criteria issues. Fluids in the fuel gas lines was due to loss of bath burner. After thawing and inspecting all parts of vessel for damage and re-pressurizing, I tested the pressures going to the pilot (5 PSI) and main burner (9PSI) with a new gauge to verify against existing gauges and found them to be accurate. The tip of the pilot appears to be placed correctly to avoid getting snuffed by the main burner during lighting. The motor control valve holds pressure when the t-12 shuts it off and the regulator does not leak past building pressure when the T-12 is not calling for flame. This must have been blown out by a high wind, causing the unit to lose temp, until the dumps froze, the vessel flooded and everything flooded from there. May need to turn to engineering for a better resolution.",user_6,asset_1401,36.2541889,-91.2478009
3/23/2018,Instrumentation,Transmitter,Casing Pressure,Rosemount,266J,Weather,Casing transmitter has not been working since Nov 2017 ,user_163,asset_1817,48.1470144,-103.6180489
1/31/2017,Compressor,Compressor,Hose,Other,Other,Vibration,Both compressors broke belts causing units to go down,user_87,asset_345,47.96757674,-103.4474857
6/3/2019,Separator,Fuel Supply System, Big Joe Regulator,Fisher controls,Type 912,wear,Button worn out and not sealing against orifice.,user_54,asset_1675,46.2356189,-100.6010498
8/12/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Trash,well ran to long with compressor down and casing pressured up causing gas lift to go down on high discharge.,user_71,asset_1452,48.3619066,-103.2129855
10/31/2019,Separator,Temp Control System,Heater/Burner,,,,arrived onsite found BOTH TRIDO GLYCOL PUMPS DOWN. mike and i thawed out water dump. thawed out fuel gas to line heater and re lit line heater. compressor is frozen and down on high liquid stage. all dumps on compressor are frozen. isolated suction and blew down compressor shut off power. location probably wont stay running for long with pumps being down,user_120,asset_1574,40.5262342,-113.8824849
9/14/2017,Compressor,Compressor,Suction Controller,Ajax,,Vibration,Block valve located upstream of the suction control valve is leaking-by. Causing the compressor to pressure up slowly with the valve been closed.,user_130,asset_1346,48.3619066,-103.2129855
10/27/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Whole seperator down due to lack of fuel gas. ,user_41,asset_679,48.20118189,-103.5630752
1/28/2019,Gas Scrubber Separator,Pneumatic Dump Valve,Controller,Norriseal,,Out Of Adjustment,Issue: while leaving location i herd gas blowing at the tanks Root Cause: found water dump stuck open and unit drained Fix: unstuck dump and drained fluid out of the controller and got working again ,user_170,asset_1833,43.56424,-91.351691
11/1/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Trash,"OLD Valve Replaced with new one and also replaced 2"" Drain Valve",user_119,asset_1226,48.1470144,-103.6180489
2/20/2019,Separator,Dump Line,,,,Freezing,"pad was down for a short period of time due to a high oil tank. got tank switched and cleared interlock. oil tank is at 17'3.swapped into middle tank. the A four pack had lost fuel gas due to the scrubber being ball checked. drain line on scrubber was froze.thawed out line and got scrubber drained and ball fell. found solar glycol pump that supplies the a unit was down. replaced fuse and pump started.pump was turned all the way up. lowered both settings on pump.found water dump on the A separator froze. thawed on water lines and they finally broke. took awhile because i can not reach most spots due to snow drifts onsite.dezy drain was also froze. thawed out line and drained dezy.looks like psv on the scrubber pot on the A four pack lifted,spilled a little bit of oil on equipment.reported to team lead. pad is back up and running.",user_120,asset_857,43.56424,-91.351691
10/29/2019,Separator,Temp Control System,Fuel Gas Supply,,,,Team Lead had me come to location to verify fuel gas mains were open to burners. All the automated mains were open on all three units but the manual block valve outside the unit just before the burner was shut on the B-140. I opened it up.,user_22,asset_1139,46.2356189,-100.6010498
10/22/2019,Separator,Temp Control System,Fuel Gas Supply,,,,bad regulator on pilot ,user_121,asset_764,46.2356189,-100.6010498
4/13/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"plunger will not come to surface, vented 3hr, will try again tomorrow and if wont come around turn to slickline",user_88,asset_1819,48.1470144,-103.6180489
1/16/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Fuel gas scruber balled out/frz. Blew unit down. Shut in at wellhead. Left open to atmosphere to thaw.,user_80,asset_1315,48.04220522,-103.4207529
12/5/2017,Compressor,Compressor,Dump Valve,Ariel,,Freezing,"Found dump valve froze, found heat trace not working, swapped valves and heat trace is warming up the dumps ",user_122,asset_2247,48.36110365,-103.8164644
4/15/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,"Pilot blew out due to wind causing hydrate in choke and hi-lo. Manually broke, thawed and RTPd unit",user_107,asset_2090,,
2/7/2019,Fuel Gas/Start Gas,Regulator,,,,,"attempted to get to location to get pad back on, could not access road due to drifted snow and high winds, poor visibility, work order turned in for plow",user_106,asset_483,40.5262342,-113.8824849
7/19/2017,Pipeline/Piping,Valves,,,,End Of Design Life,Replaced choke that was leaking,user_150,asset_2132,48.1602676,-103.6173103
4/17/2019,Pipeline/Piping,Valves,,,,human error,"1"" line for the buy-back line needed extra supports",user_28,asset_809,48.1511744,-103.6275517
10/3/2018,Flare System,Flare Header,Instrumentation,,,,Found that the SCC was lit. Adjusted thermocoupler 90 degrees. Looks like the flame with the wind is mostly staying on back side of rosebud. Will know if it is repaired when I don't get a callout on it.,user_55,asset_2173,,
1/23/2017,Sand Separator,,,Other,Other,Other,Bath is low on glycol need a refilled ,user_39,asset_2212,,
7/12/2018,Tanks/Pits,Tank Level,Sonar,,,Weather,confirmed tanks were hauled pressured up whole pad cycles started.,user_11,asset_647,43.252261,-115.0567324
9/6/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,Inner and outer load line valves are leaking. ,user_41,asset_48,48.19408095,-103.7558924
1/7/2017,Automation,RTU,Relay,,,Loose Connection,Cyclonic not responding to commands,user_175,asset_198,47.89261767,-103.6119752
3/4/2019,Separator,Temp Control System,Electrical,,,,Verified all dumps and scrubber clear. Well is flowing and making arrivals. Had to light glycol bath on separator A. Ignitor and fire eye not working. Found the Ignitor Power Disconnect off on Jbox. Everything working now. ,user_55,asset_2032,,
4/25/2019,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,," +1/2 "" BALL VALVE AT VESSEL UPSTREAM OF BATH AND BIG JOE REGUALTOR NOT HOLDING, NEEDS REPLACED. **WM ENTERED",user_34,asset_1607,40.5262342,-113.8824849
12/8/2016,Gas Scrubber,,,,,,DVC and filter to DVC frozen thawed ,user_100,asset_28,48.06521216,-103.5977837
1/17/2019,Compressor,Engine (Gas),,,,, I went to location to work on compressor I could not get the engine to turn over I found the heater had run out of fuel I shut the suction on compressor and bled down and tagged out suction valve. I hooked up to the trailer and went back to town and fueled it up and returned to location and put it on engine block and tarped up as much as I could.,user_159,asset_1417,43.56424,-91.351691
2/21/2018,Sales Valve (PV),Pneumatic Control System (3Pgra),,,,,"Regulator froze, thaw with truck and blow lines free of liquids. Liquids dropping out of stainless when it exits cabinet and settling in regulator ",user_109,asset_1135,48.1695832,-103.4458746
6/20/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,Load lines leaking by,user_165,asset_1063,48.1602534,-103.6174576
4/4/2018,Heater Treater,Vessel,Fuel Gas Scrubber,,,Corrosion,"Well esd on high psi on the low pressure unit. Went and shut choke mainifold before troubleshooting. All equipment looked good and was working properly. Went to clear interlock on LP and it was saying that the LP only had 4psi while onsite it was at 54psi. Somehow all the high and low set points on the LP in Emerson got set to zero’s, and that’s what triggered the alarm. Spoke with mike Edwards and he reset all the set points. He is working on figuring out why this happend. Rtp well on 24/64 choke. Flowing3.2 with 550 psi on casing",user_172,asset_1213,,
12/21/2017,Plunger System,Plunger,Plunger,IPS,,Not Optimized,plunger came on its own after pausing it on,user_11,asset_2161,48.2593664,-102.9009552
3/19/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,vented plunger in. I let it blow do lower casing pressure. Looks better now.,user_141,asset_105,48.1494387,-103.6217593
3/11/2019,Tanks/Pits,Shell,Body,,Steel,Corrosion,"Tank on location 770019w was previously patched, and patch failed tank is leaking again. Shut and tagged out inlet valve so tank is currently out of service. ",user_63,asset_1220,48.40505739,-103.5810111
8/28/2017,Automation,RTU,Board,Control Wave,FB 107,Vandalism,Jumpers were not set correctly on I/O card,user_65,asset_1675,48.3619066,-103.2129855
1/13/2018,Fuel Gas/Start Gas,Regulator,,,,,Issue: found the flare was out on the HMI Root Cause: fuel gas regulator froze off at the SCC Fix: regulator is out in the open exposed and the piping is raised right at the flare and also exposed. This all combined is a great freeze point. pressure drop should be taken at the separator never at the flare and the line should slant back with no exposed piping ,user_136,asset_2034,48.1470144,-103.6180489
2/14/2018,Tanks/Pits,Valving/Swedges,Apollo Valve,,,Freezing,"Dispatched to location for frozen load line on oil tank 770042C. Arrived on location and found load line full of water and frozen. Called fluid management coordinator to check recent haul records. Found water hauling company had recently transferred oil from water tanks to oil tank 042C using the 4"" load lines. The water haulers pull all fluids from water tanks and push into oil tanks, let fluid settle and pull water out of tanks. Root cause, water driver did not pull water out of load line and it froze. Tested load line valve at tank to make sure its not leaking, it is good. This location has heat trace going around load lines, but we do not always run it due to heat loss in the system, heat trace is cold by the time it exits the last tank and can cause other freezing issues. Adjusted heat trace and forced flow through load line heat trace to thaw load line. Will check tomorrow to see if load line is thawed.",user_62,asset_793,48.1470144,-103.6180489
10/26/2019,Gas Scrubber Separator,Dump Line,,,,Trash,Dump scrubbers Desi 5 seconds scrubber inside unit 1 seconds,user_128,asset_855,48.169451,-103.4457722
4/4/2018,Pumping Unit,Electrical,Surface Cable,Interstate,,Wiring Shorts,Had Brad come out and shoot a fluid shot on the 50 well. I did a site walk down on location before rod pump start up. Opened fuel gas up to motor. Found that wires had been chewed through on pumping unit and spark plug wires are showing bare pipe. Shut fuel gas down. Contacted maintenance team. Tagged out pump.filled out task request for maintenance to fix,user_172,asset_1197,,
6/29/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_1633,48.1002122,-103.5869184
4/5/2019,Wellhead,Wellhead Piping,,,,, +ANALOG GAUGE AT WELL HEAD WAS NOT WORKING. THE DIAL HAD BECOME UNPINNED. REPLACED,user_34,asset_8,48.1470144,-103.6180489
4/20/2017,Gas Scrubber,Other,,Other,Other,Other,turned up reg. pressure to the esd and it started working,user_100,asset_329,48.224585,-103.8291059
12/25/2016,Automation,,,,,Other,,user_134,asset_811,48.158196,-103.6169055
6/1/2018,Compressor,Compressor,Suction Controller,Ajax,,Trash,"Issue: found compressor down on the HMI Root Cause: down on low suction pressure. found the suction controller is out of adjustment. Fix: restarted the compressor but it doesn't sound real healthy, adjusted the controller and returned to service ",user_136,asset_1800,48.1470144,-103.6180489
8/24/2019,Plunger System,Plunger,Plunger,PCS,,Corrosion,inspected and replaced plunger rtp'd well,user_10,asset_1155,40.5262342,-113.8824849
12/15/2018,Automation,Solar Panel,Wiring,BP Solar,,Electrical Short,"Conduit run has unnecessary 90° fittings. Wire had been yanked through them, stripping insulation along its length and causing intermittent shorts to the conduit.",user_12,asset_2048,46.2356189,-100.6010498
9/26/2019,SWD System,Particle Filter,Element,,,,changed both sets of filters. Location looks good,user_31,asset_1847,48.2715555,-102.8684979
12/29/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"well not building psi because of winter conditions keep losing pad on low psi because of everything running while shut in on cycles to long/need to vent up plunger,tried venting up /no go , ended up equalizing and let day ops know-",user_131,asset_1245,40.7126799,-114.1193569
1/10/2018,Tanks/Pits,Flare/Combuster,,,,,Pad went down on low unit pressure due to all wells being off at the same time. Burners and pumps used up all the gas and the location shut in. This pad needs buyback meter to keep it up and running. Lit SCC b,user_62,asset_1087,48.1470144,-103.6180489
9/10/2019,Separator,rupture disk,,,,premature rupture,Rupture disc popped at 650,user_145,asset_156,48.0557637,-103.6356549
1/4/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,"Insulation is almost non existent, work order in",user_77,asset_915,47.93789273,-103.504669
12/8/2018,Separator,Dump Line,,,,Freezing,Found water dumps frozen and big joe on two of the three unit frozen. Thawed out big joes and got burner going. Thawed out all water dumps on location at the tanks and just as the dump went into the ground near the units. Rtp'd wells,user_10,asset_322,43.252261,-115.0567324
8/22/2019,Instrumentation,Meter,Turbine,Halliburton,1,Recalibrated,"8/20/2019 Changed west filters, then swapped. Location checked, cut off rebar that was by unloading on east side. 8/22/2019 High condo tank 19.8' 761936C, was keeping drivers from unloading, equalized tank and dropped level to 18'. Cleaned transfer pump turbine meter on south side, had a nut stuck on the inside. ",user_31,asset_1847,48.2712224,-102.8704416
3/23/2019,Separator,Choke Valve/Loop,,,,Freezing,"location down and unit frozen/ jumped unit and temped up flow well to thaw out dis-placers on the dumps. Thawed out choke,dvc and function tested . Rtp'd well but well died off / vented to unload and rtp'd well contacted optimizer to adjusted cycles. Vented well to unload fluid and rtp'd.",user_10,asset_686,40.5262342,-113.8824849
12/17/2017,Pipeline/Piping,Pipe/Components,,,,CO2 Corrosion (Internal),Issue: day crew found a leak on the hi pressure flow back iron Root Cause: the gasket went bad and they couldn't get it fix so i was asked to drain the units Fix: I got all the water drained out of the equipment ,user_136,asset_876,48.2609773,-102.899974
2/26/2018,Separator,Dump Line,,,,Freezing,Found unit down and frozen broke freeze in choke and got burner going thawed out unitand dumps -rtp well,user_100,asset_1873,40.5481548,-114.0112915
4/25/2019,Pumping Unit,Engine,Battery,Cummins,,Wear,Pumping unit engine battery is dead and needs to be replaced.,user_42,asset_298,46.2356189,-100.6010498
12/11/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Vented plunger to surface and put back on plunger cycles optimization may need to look at cycles.,user_51,asset_2225,48.1497816,-103.6213838
2/19/2018,Heat Medium,Furnace,Tube,,,,Heaters down Air intake covered in snow,user_111,asset_1654,48.02590829,-103.4436681
1/5/2019,Separator,Dump Line,,,,Freezing,"Found all wells down on the pad, had to thawed out the front end needle valves on the units to jump gas into the units. Thawed out fuel gas lines and the big joe to get the burners and pumps going on the pad. Thawed out the condo dumps and chokes on all three wells on this pad. I got unit up and warming but couldnt get the water dumps thawed out and they are still frozen. We should check this pad in the morning to see if the gylcol pumps have thawed out the water dumps overnight. I function tested all chokes and the unit should be good to go when the water dumps get thawed.",user_10,asset_1191,,
4/11/2018,Compressor,Compressor,Instrument Gas Supply,Ariel,,Trash,Issue: called out compressor down alarm Root Cause: the compressor has been removed all that is left is the building Fix: will get with the programmer and get the false ghost callout removed ,user_136,asset_2270,48.2591345,-102.9020474
3/26/2017,Heater Treater,Firetube,Other,Other,Other,Other,Emissions ,user_156,asset_2051,48.2321526,-103.6238584
9/16/2018,Separator,Temp Control System,Fuel Gas Supply,,,,"While doing winterization check list, I pulled the burner appart to inspect tips and flame arrest device and found the air mixture plate for the main burner melted into a puddle and obvious burn marks all the way back to the flame arrest device. I contacted team lead and was given permission to investigate further and document with pictures. I pressurized the internal fuel gas fittings and leak checked with snoop and found the fitting that connects the internal fuel gas supply line to the main burner was leaking as well as the internal fuel gas supply line for the pilot leaking. This is likely where the fire was being sustained from the back of the burner near the flame arrest device, melting the air mixture plate. I removed the fitting for the main supply line and found the fitting itself and the threads for the housing where stripped allowing it to leak. The leaking stainless for the pilot were simply loose. The burner has been tagged out as unsafe to use until the burner/flame arrest housing is repaired and all internal fuel gas lines leak checked. WM created to repair burner.",user_54,asset_1231,36.2543776,-91.268112
7/14/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Drained desi while on location working on well 160. Took over 2 minutes to drain desi. Location has WFS buy back meter but location is running off of gas from top of units. Burners are shut off, i suspect it has just been a long time since it has been drained. ",user_62,asset_1404,43.252261,-115.0567324
3/4/2019,Wellhead,Cyclonic Valve,Actuator,,,Freezing, 5. Latham Draw 5-1 - Comm failure • John and I worked on this issue together • Found fuse for scada blown • Found sales line cyclonic valve frozen • Found old style (no torque limiter) actuator installed on cyclonic valve • Determined that cyclonic actuator had blown fuse due to freeze in the valve • Replaced cyclonic actuator with new style • Moved power for cyclonic actuator and relays to their own independent power • Tested and verified new actuator functions correctly • Left actuator off of valve tagged out because of freeze in valve • Coded well back to operations ,user_38,asset_1274,46.2355104,-100.6413984
1/30/2018,Flare System,Flare Header,Instrumentation,,,,Issue: found SCC (A) down on the HMI Root Cause: (INT) no pilot flame Fix: relight remotely,user_136,asset_463,48.0614644,-104.8417043
12/16/2017,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Well was down for non arrivals. Kicked well on and paused it open. Plunger arrived, returned well to production.",user_141,asset_310,48.1470144,-103.6180489
1/29/2017,Compressor,Compressor,Instrument Gas Supply,Other,Other,Freezing,Pressure lines to instrument panel had freezes in them. Put heater on lines and panel. Got everything thawed and RTP'd compressor.,user_141,asset_265,48.3619066,-103.2129855
12/14/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Desi and fuel gas scrubber of liquids daily routine auto dump may be a solution to issue ,user_109,asset_1364,48.3271913,-103.6564863
9/12/2018,Tanks/Pits,Flare/Combuster,,,,,SCC OUT DUE TO HIGH WINDS,user_34,asset_1419,48.224585,-103.8291059
4/17/2017,Wellhead,Primary Choke,Casing Valve,Other,Other,Other,"Well down, not flowing",user_141,asset_1707,48.224585,-103.8291059
12/27/2016,Heater Treater,Firetube,,,,,"The A bath called out last night on high bath temp,day operator will look at it",user_84,asset_809,48.18248924,-103.5378109
11/3/2017,Separator,Choke Valve/Loop,,,,Corrosion,choke is sticking when opening and closing it may need change out soon,user_110,asset_809,36.2541889,-91.2478009
3/1/2017,Wellhead,ESD Valve,Gas Supply Line,Other,Other,Freezing,Thawed dvc rtp,user_176,asset_1152,48.17189564,-103.5952228
12/1/2016,Automation,RTU,Relay,,,Loose Connection,Solenoid to esd needs checked or fuse in rtu the esd to this well won't open,user_131,asset_1,47.89381381,-103.4999359
7/10/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,well lost plunger arrivals after Williams shut pad in for dehy removal,user_179,asset_1141,48.1470144,-103.6180489
12/5/2017,Gas Scrubber Separator,ESD,,,,,Freeze in fuel gas system which caused the esd to shut and unit to go down .Broke freeze and rtp well,user_100,asset_534,40.5262342,-113.8824849
2/3/2017,Compressor,Engine,Fuel Gas Supply,Other,Other,Other,Compressor was bypassed and went into recycle causing it to go down on low second stage pressure. I realigned the valves restarted the compressor and rtpd. ,user_175,asset_2073,47.88299059,-103.5120458
12/26/2017,Sales Valve (PV),Elec.System,,,,,There was an alarm on the cyclonic stoping the valve to open. (WCPS Alarm) False alarm.,user_130,asset_1734,48.1470144,-103.6180489
11/12/2017,Chemical System,Pump,Cam,Goulds,HBC1,Wear,Graco pump ,user_156,asset_1934,48.208111,-103.7667079
9/7/2018,Compressor - Gas Lift,Engine,Fuel Gas Supply,GM,,Weather,"Compressor was down on high AFR temps. Compressor building panels were removed earlier in the summer to keep temps down, they were installed again a few weeks ago. With day time temps in the high 70's low 80's, temps in the compressor building are to high and cause compressors to go down on high AFR temps. We will continue to have to start the compressor each day until panels are removed again or day time temps start to cool off more. Restarted and loaded compressor. ",user_15,asset_521,48.2817029,-102.855422
12/5/2017,Separator,Temp Control System,Heater/Burner,,,,Root cause not listed. Burner was not responding to call for fire from T12. Checked fuel supply. Good. Tore down burner assembly and find the nuts on the main burner at the fuel/gas mixture point all back off causing leaking preventing a good mixture and combustion causing the weak burner performance. Retighten assembly and function test. All is well in the world. Root cause - Inadequate fuel gas mixture caused by vibration backing off assembly at main burner. ,user_75,asset_203,,
9/7/2018,Compressor - Gas Lift,Compressor,Panel,Ariel,,Vibration,Compressor down on eics restarted compressor without a problem rtp'd set rpm's at 980 injecting 720 down the 10 well.,user_10,asset_2055,48.1470144,-103.6180489
2/15/2018,Gas Scrubber Separator,Dump Line,,,,Erosion,stopped to check that green complete unit water dump had an interface level . everything looked good ,user_71,asset_2069,48.1470144,-103.6180489
3/4/2019,Fuel Gas/Start Gas,Regulator,,,,,"line sat with 1000lb on it and froze off the blow down and the ESD valve, tried thawing and depressurizing, left line closed and need to woork on further tomorrow",user_106,asset_1801,48.1470144,-103.6180489
4/3/2019,Pipeline/Piping,Valves,,,,End Of Design Life,"trim set/packing was leaking, crew was able to replace trim set and packing cage",user_28,asset_1600,48.1511744,-103.6275517
12/18/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_2012,48.1470144,-103.6180489
4/11/2018,Wellhead,Tubing,,,,,"Found needle valve on tubing side of well head was packed with grease. I isolated, pulled needle valve off and cleaned out grease. Put needle valve back on well head. ",user_62,asset_1881,48.1508659,-103.6206981
6/15/2017,Compressor,Cooler,,,,,compressor went down on high suction pressure due to a cooler freeze,user_130,asset_23,40.5960545,-113.9323891
9/13/2018,Instrumentation,End Device,Asco,,,Installation Design,"Solenoid appeared to be plugged off with thread tape, not allowing gas to pass through to the hi-lo controller. Replaced.",user_38,asset_819,36.256016,-91.2697504
1/16/2019,Heater Treater,Burner,BMS,,,Corrosion,Issue: while talking to Williams found there dehy had a lot of fluid Root Cause: found bath (A) temp running 114deg. these wells are not big enough to be running the bath temp that hot. These wells have died down enough and with being on plungers when bring up the fluid they do the contact time in the bath brings the wells up to the flow temp of the bath causing the fluids to not drop out and carry to Williams dehy where we have a buy back fuel gas line. Then to compound the problem more we are buying our fluid right back and it gets back into our fuel gas freezing all the fuel gas back up. Fix: drained desi multiple times to get as much fluid out as i could and lowered the bath temp,user_170,asset_1574,43.56424,-91.351691
4/4/2018,Separator,Liquid Dumps,Diaphragm,Kimray,,Freezing,dumps are frozen well was shut in and the below freezing temps caused the dumps to freeze ,user_110,asset_2171,,
4/16/2018,Separator,Liquid Level Control,,,,,Supply gas was shut off of the water dump. Not sure why. No tag. Opened supply. ,user_156,asset_857,48.32446891,-103.6013837
1/30/2018,Separator,Choke Valve/Loop,,,,Freezing,,user_126,asset_561,,
11/4/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Relit bath on four pack unit A. Drain scrubbers,user_172,asset_1936,,
4/24/2018,Heater Treater,Burner,BMS,,,Loss Of Fuel Gas,Issue: bath alarm Root Cause: (INT) bath (A) low low glycol level alarm. went to location performed a walk around and didn't see any glycol leaking any where and checked the bath looks to be more like evaporation. but i did shut the glycol pumps in this cabinet to help the level from bouncing Fix: lowered the bath level two tenths of an inch and relight remotely ,user_136,asset_1328,48.2595694,-102.9009394
3/25/2018,Instrument Air,Compressor (Screw),Panel,,,,"call out 1st of shift whole pad going down-lost main air comp-tripped out breaker, reset keeps tripping out-brought up spare new comp it has a hard time keeping up not enough volume-had to shut pumps down & by pass dryer to get some wells going, only maintains 66 psi but was able to rtp all but two wells, try to rtp them later hopefully?",user_131,asset_1640,40.7126799,-114.1193569
4/11/2018,Fuel Gas/Start Gas,Regulator,,,,,Went to rtp well found big joe not holding back pressure and vibrating bad. Repair and back to service. Well also rtp’d ,user_58,asset_2034,48.36650914,-103.5605698
8/20/2017,Tanks/Pits,Liquid Level Control,,,,,Pad shut in on a False high tank alarm all wells on pad will not let me reset wells are all currently down onsite waiting on automation.,user_51,asset_1637,48.2736791,-102.8725298
11/11/2017,Compressor,Compressor,Suction Controller,Ariel,,Liquid Carryover,Compressor down on hi suction pressure. ,user_48,asset_140,,
3/9/2018,Tanks/Pits,Liquid Level Control,,,,,multiple false high tank alarms,user_163,asset_26,48.1470144,-103.6180489
5/29/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Gardner Denver,,Freezing,"Comp down on high discharge, possible freeze down hole again, I will watch for awhile, but will need to blow tubing for awhile, psi has already came up to over 1000 psi, I'm sure we have down hole issues, need engineering help,",user_84,asset_943,48.09703674,-103.5408339
1/18/2019,Separator,Dump Line,,,,Corrosion,Found the unit esd interlock on low unit pressure started troubleshooting and found that the dump bonnet on the water dump was not shutting the dump all the way and was bringing unit pressure down which shut the esd. Isolated fuel gas to the dump and replaced dump bonnet rtp'd plunger making arrivals and dump holding and in operation.Cleaned off snow on all the solar panels on the pad.,user_10,asset_2091,40.5262342,-113.8824849
4/5/2017,Gas Scrubber,Pnumatic Dump Valve,Body,Other,Other,Other,None,user_24,asset_4,47.97285474,-103.6368638
3/27/2017,Instrumentation,Transmitter,3n1 MVT,Other,Other,Recalibrated,,user_113,asset_602,48.32667063,-103.5844265
11/7/2019,Surface Location,Lease Road,,,,Weather," Blade is repairing road damaged from excessive traffic & wet weather, entered surface failure in Safety 3.0.",user_42,asset_705,39.2506642,-92.4357879
8/27/2019,SWD System,Particle Filter,Element,,,,"Filter DP at 20, changed filters. Thiefied condo tanks, both 12"" bottoms, turned in for bottom pull.",user_31,asset_569,48.2712224,-102.8704416
7/26/2017,Pumping Unit,Engine,Control Panel,Ford,,Controller Failure,"Started with ""high pipe pressure"" code, Ran engine & pumping unit in manual until warmed up, switched to auto, cleared controller malfunctions and RTP'd.",user_161,asset_1644,40.7126799,-114.1193569
10/12/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_2012,48.1003755,-103.5856957
4/27/2019,Wellhead,ESD Valve,Actuator,,,Corrosion,Actuator internal seals failed. Leaking from lower vent.,user_12,asset_1135,40.5262342,-113.8824849
10/17/2019,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Freezing,"Removed cracked load line and capped, valve is ready for hauler ",user_21,asset_2179,46.2356189,-100.6010498
2/9/2018,Tanks/Pits,Piping,Load Line,,,Vibration,"Possible vibration and float backed off and fell in tank, driver pulled tank level down and sucked float into valve.",user_119,asset_2169,48.1604343,-103.6185014
3/21/2019,Separator,Dump Line,,,,Corrosion,"well had flown out for to long and loaded up the night previous. went to location and vented well for around two hours. casing would drop to around 690 and climb back up to around 710. this happened multiple times. well kicked fluid the entire vent.i shut well in for pressure build while i got the other well online.well was shut in for around five hours. tubing and casing had almost equalized at around 730psi.put well back on cycles and started a cycle. spoke with optimizer and PTL. optimizer is going to watch closley and adjust criteria if necessary. while flowing the other well this well struggled flowing to sales. the 45 is flowing around 4mil and is pushing this well out causing it to liquid load. first cycle did not look very good and will more then likely require another vent. while walking through equipment and checking dumps, i found the insulated hammer union for the dump turbine on the oil dump leaking.isolated and blew down well. attempted to hit hammer union to get a tighter seal but was unsuccessful, eventually took union apart and found casket and insulated washer were both missing from union. contacted team lead and he got a crew to bring me out the parts needed. eneded up replacing the entire union. leak tested my work, no leaks found. rtp well",user_120,asset_793,46.2356189,-100.6010498
3/13/2017,Sand Separator,Other,,Other,Other,Other,"Freezes in fuel supply lines to pumps, hi/lo, dump controllers.",user_141,asset_2157,48.224585,-103.8291059
2/12/2018,Plunger System,Plunger,Plunger,PCS,,No Liquid,Tbg was perforated in an attempt to remedy a cross flow condition on 1/22/2018. Tbg was perforated at the depth of the Lewis perforated interval. Plunger arrivals have been inconsistent since. Suspect intake is below fluid level. Dispatch to perform fluid shot surveillance to confirm. Pull graphs for more information. When plunger is arriving it is arriving in 7-8 minutes with very little fluid. All condensate per dump meters. Intake (perfs) at 9128’ bumper spring at 9118’. Estimated arrival speed 1300 FPM and mostly dry. Rig up to perform fluid shot surveillance. Shoot tbg first utilizing gas gradient to calculate acoustic velocity. Repeatable shots show 0’ of fluid over intake or 9190’ from surface. Shoot annulus utilizing gas gradient to calculate acoustic velocity. Repeatable shots show 0’ of fluid over intake or 9204’ from surface. Inform PE of findings. Remove cycles from well and shut ESD to prevent dry fast arrivals. Worked a plan forward with PE and PTL about surfacing plunger to catch and removal. Also met to discuss production plan forward. Met with PTL verbally on phone to discuss JSA for surfacing the plunger to sales. Top risk is a dry fast arrival causing lubricator spring damage. Controls in place to inspect lubricator cap before surfacing to ensure spring is intact. Attempted to surface to sales. Plunger stalls and needed vent to finish surfacing. Pull plunger and tag well head about removal. Switch HMI to optimizing intermitter. Update enbase and deferral coding. ,user_75,asset_6,,
8/20/2018,Compressor - Gas Lift,Compressor,Valves,Ariel,,Freezing,"Well lost injection, got to location and found that the gas lift compressor was down and it went down at 0540, even before the compressor went down the well wasn't injecting Found that the back side was hydrated off, broke hydrate and restarted injection, Methanol was good. RTP'd ",user_56,asset_910,48.1470144,-103.6180489
8/12/2018,Compressor - Gas Lift,Engine,Temp Switches,Ajax,,Overheat,CALLOUT compressor down on code 45 again. Probably high manifold temp. Reset and restarted. Talked with Archrock. They thought they had it fixed. ,user_31,asset_794,48.2715351,-102.8691406
4/12/2019,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Plunger old and worn ordered new 2” bar will replace on 4/13,user_18,asset_1901,,
11/12/2018,Pipeline/Piping,Valves,,,,Corrosion (External),"Valve and nipple leaking, replaced with new valve and nipple.",user_5,asset_1927,43.252261,-115.0567324
11/2/2019,Separator,Temp Control System,Pilot Valve,,,,"Found that the bath heater was out. Also found valve to pilot closed. Opened valve and lit bath heater remotely. Dumps froze, separator flooded and froze. ",user_55,asset_1103,,
11/3/2016,Wellhead,ESD Valve,Actuator,Other,Other,Fouling,,user_126,asset_241,,
2/24/2018,Separator,ESD Valve,Gas Supply Line,,,Freezing,Scrubbers are ball checked lossy fuel gas. Supply line to esd froze. Baths are cold. Thawed out fuel gas got esd open and well rtp on plunger cycles,user_172,asset_592,,
3/30/2017,Gas Scrubber,Other,,Other,Other,Other,None,user_35,asset_192,48.35096143,-103.6159284
5/20/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,"Compressor down on High Discharge pressure, guessing had a freeze/hydrate somewhere and shut it in. Restarted compressor with no issues.",user_141,asset_551,48.1470144,-103.6180489
3/27/2019,Wellhead,Wellhead Piping,,,,hydrate,"wellhead master valves may be leaking due to partial hydrate, can't depressure wellhead to verify if gauges are accurate due to hydrates in needle valves. will start burners and pumps to attempt to thaw overnight and reassess on followup",user_17,asset_934,,
10/24/2018,Tanks/Pits,Flare/Combuster,,,,,"all 3 scc's out, took apart and cleaned. 2 of the pilot heads had the fins opened up, put back to about original design, relit",user_31,asset_767,48.2717607,-102.868775
1/29/2019,Gas Scrubber Separator,Mechanical Dump Valve,Controller,Kimray,,Liquid,Issue: Found the flare scrubber had 1/4 fluid and had not been drained or dug out Root Cause: no one had dug out the valve and drained it and the fluid level was building. Fix: dug out the drain thawed out and drained the flare scrubber ,user_170,asset_247,48.264857,-102.9014931
4/14/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,"choke was pinched and froze off, opened up and broke freeze",user_88,asset_819,48.262923,-102.8997623
4/13/2017,Gas Scrubber,Other,,Other,Other,Other,,user_35,asset_549,48.3270067,-103.6236855
1/3/2017,Automation,,,,,,DVC on Auto Choke frozen and not allowing to vent off pressure on OFF cycle. Had to hand thaw.,user_138,asset_768,48.17915471,-103.4307914
8/28/2017,Automation,Charging System,,,,,"Gas measurment is not working on our meter, please have automation or measurement check and fix, thank you",user_84,asset_2020,47.95853111,-103.5098417
5/25/2018,Tanks/Pits,Flare/Combuster,,,,,Found SCC A out when I arrived on location. Found piece of Teflon tape stuck in pilot orifice. Cleaned out pilot and Re-lit SCC.,user_62,asset_1352,40.7126799,-114.1193569
12/27/2017,Instrumentation,micro turbine,,,, G4 breaker trip,#2 turbine will not start due to Speed Sig Mismatch. Will write a work order to have FlexEnergy come out and troubleshoot,user_141,asset_1489,47.942078,-103.6975344
6/28/2019,Tanks/Pits,Well Pad,,,,Livestock,Arrived onsite to followup on flare it backfill request. Discovered 2 Angus cows inside fence and in pit. Bottom of pit was muddy and cows exhibited no signs of sickness (I've spent 39 years around cattle and can recognize abnormal behavior with ease). I opened fence and pushed cows out to pad reclamation area. I contacted field environmental adviser of what I found and that I would have pit closed within a week. I contacted a roustabout crew working 2 miles away to assist me in repairing the pit fencing to keep the cows out. Entered surface failure & observation in Safety 3.0. Also added pit to reclamation list and contacted vendor to place one call to close pit ASAP.,user_42,asset_1768,46.2356189,-100.6010498
2/9/2017,Automation,Cable,Other,Other,Other,Electrical Short,Wire is shorted and needs replaced ,user_74,asset_1628,48.16084977,-103.6189009
2/18/2018,Gas Scrubber Separator,Dump Line,,,,Freezing,Mon 11-160 H checked site drained scrubbers everything looked OK,user_71,asset_261,48.1470144,-103.6180489
12/9/2018,Separator,Liquid Dumps,Seat/Ball/Piston,Norriseal,,Corrosion,"leaking condo dump trim set, replaced",user_31,asset_1652,43.56424,-91.351691
8/1/2017,Flare System,Flare Header,Regulator,,,,Replaced Plugged Flame Arrestor with a new one.,user_119,asset_708,40.5960545,-113.9323891
2/23/2018,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,Issue: called out well shut in alarm Root Cause: well shut in on low unit pressure from all the wells being in off cycles for so long units ran out of unit pressure Fix: ESD is in valve fault and cant get to open will let an automation tech know ,user_136,asset_1849,48.2629356,-102.8996131
9/16/2019,Instrumentation,Controller,,,,,replaced IP and relay,user_16,asset_146,48.1461662,-103.6695491
4/17/2018,Fuel Gas/Start Gas,Regulator,,,,,Pilot to A scc was full of liquid. Drained liquid. Also drained liquid from line supplying scc,user_156,asset_793,48.3657189,-103.8133109
8/22/2018,Compressor - Gas Lift,Engine,Temp Switches,Ajax,,Overheat,CALLOUT compressor down on code 45. Temperature sensor from engine. Not sure which one. Building tin just put on. Adjusted doors a little. Restarted compressor. ,user_31,asset_794,48.16894463,-103.6200631
6/11/2019,Separator,ESD,,,,,Pad only had a few wells flowing onsite I jumped pad back online and found that the ESD on #20 well keeps getting stuck in travel automation will need to work on this but I brought three wells that were flowing back online.,user_159,asset_1961,43.56424,-91.351691
10/23/2019,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"well is loaded, attempted to surface plunger and unload but the plunger would not come in, pressures dropped good but no plunger. the plunger data is showing that it is over a year old. leaving shut in over night and we need to try again tomorrow",user_106,asset_1084,40.5262342,-113.8824849
3/23/2018,Separator,Choke Valve/Loop,,,,Corrosion,"Packing on choke leaking, will get new packing and Install hope to RTP tomorrow ",user_109,asset_2009,48.1144306,-103.4781102
4/6/2017,Pumping Unit,Electrical,Other,Other,Other,Other,None,user_158,asset_761,48.00661998,-103.6880558
2/7/2019,Separator,Choke Valve/Loop,,,,Freezing,Blowing and drifting snow preventing access to location coded to maintenance ,user_18,asset_2199,,
1/18/2017,,,,,,,Stuck water dump approximately 50 minutes ,user_163,asset_1521,47.91200514,-103.4956741
1/10/2019,Automation,Radio,,Cambium,Force200,Unknown, 7. While I was driving back to office Luman 8-115 went into comm fail • Leadership sent John and I out to troubleshoot • While we were heading to location I had Mike power cycle radio • Radio signal was -72 before power cycle and he could not ping the RTU • After power cycle signal was -64 and he was able to ping RTU • When john and I got to location we power cycled everything and redid all ethernet connections • I started a continuous ping on RTU when we left location • When I got back to the office the RTU had missed 2% ,user_38,asset_1383,46.2355104,-100.6413984
10/12/2018,Compressor,Engine (Gas),,,,,Gas Lift went down on low oil pressure I was unable to find an issue I cleared alarm and brought it back online ,user_159,asset_600,43.56424,-91.351691
1/10/2018,Separator,ESD Valve,Gas Supply Line,,,Liquid Plugging,Pad went down on low unit pressure due to all wells being off at the same time. Burners and pumps used up all the gas and the location shut in. This pad needs buyback meter to keep it up and running. jumped pad back on and RTP well.,user_62,asset_1899,48.1470144,-103.6180489
1/28/2019,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"Dispatched to well, due to its deferment Got to location and pulled well up on PI and HMI, found that well was down on SICONNA Pulled up plunger history and found the last time it was inspected was 31OCT18. Started a cycle and plunger came in once i knew plunger was up I caught it then i submitted a SBA to OSM and TL Once that was approved i pulled plunger and replaced it with a new bar Put the well back on cycles. I will remain onsite to monitor plunger for the first few cycles RTP'd well",user_56,asset_1090,48.1470144,-103.6180489
8/19/2017,Compressor,Engine (Gas),,,,,High post catalyst temp ,user_156,asset_1087,48.21136074,-103.6387488
6/30/2019,Wellhead,Plunger,Plunger,Well Master,,Corrosion,"Well had lots of off time probably from too much kelvin, 800 minutes. Started cycles and plunger came in, wasn't dropping. Last plunger inspection was Jan 2018, replaced wore out bar plunger with another bar plunger. Tried to drop plunger and it's hanging up just below surface. Methanol tank is empty, ordered methanol. Put methanol down wellhead to break freeze.",user_31,asset_2262,43.56424,-91.351691
7/17/2018,Gas Scrubber Separator,ESD,,,,,Issue: called out shut in alarm Root Cause: found the buyback gas is shut off and the compressor is using up all the pad gas recycling. Fix: i opened up the buyback gas and watched it for a while to make sure it wasn't just gonna flood out the fuel gas. was doing good so i turned the well back on and returned to service ,user_170,asset_1328,48.1470144,-103.6180489
2/16/2017,Gas Scrubber,Dump Line,Dump Line,Other,Other,Other,Thawed out water dump line,user_62,asset_2002,48.3619066,-103.2129855
4/30/2018,Gas Scrubber Separator,Dump Line,,,,Trash,MC 3-40 shut in on low unit tried to RTP remotely but went right back down went to location and water dump pilot had fluid in it blew out fuel gas RTP and started cycles. ,user_71,asset_178,48.1470144,-103.6180489
3/3/2018,Gas Scrubber Separator,ESD,,,,,"LD 17-30 shut in low unit pressure, RTP started cycles remotely. ",user_71,asset_1605,40.5960545,-113.9323891
11/21/2017,Instrumentation,Controller,,,,,not letting me start cycle on HMI ,user_53,asset_1924,48.2670106,-102.879021
2/5/2018,Pipeline/Piping,Pipe/Components,,,,Overpressure,"Well not flowing. Went to check bath temp and found temp thermometer face to be broken and numbers weathered out almost too much to read(see attached picture, unknown source of damage to the thermometer). Replaced with new thermometer and verified temp with temp gun and found bath temp to be @ 100 F. Checked choke functionality and did not find a freeze. Glycol is circulating hot and flow lines/sales lines not frozen. Checked well head gauges and verified well is frozen in coil or loaded. Opened up well to vent and no sign of hydrate is present. Methanol tank full but pump not running. Well unloading to the tank. Looked at graph and coil well free flows, but was loaded when line PSI spiked up by 32 PSI on 1/15/2018 (unknown reason for line PSI bump on that date). OPS set shut in criteria if the well ever loses flow rate below critical, casing raises beyond a 30 psi, and line PSI shut in set point set in an attempt to save the well from the next line PSI spike so that no vent is required.",user_6,asset_1934,36.2541889,-91.2478009
6/7/2018,Tanks/Pits,Flare/Combuster,,,,,found pilot line was shut at one inch ball valve. no tags or flagging. opened line. no issues found relit flare,user_172,asset_876,48.1470144,-103.6180489
5/2/2017,Wellhead,Tubing,,,,,"freeze down hole, shut in well head",user_39,asset_877,48.1470144,-103.6180489
2/6/2017,Gas Scrubber,Shell,Body,Other,Other,Other,Relit pilot on scc,user_100,asset_1686,48.1965283,-103.6327709
2/19/2019,Separator,Dump Line,,,,Freezing,"Dispatched to well, got to location and walked surface equipment down found the FMC on the flowline shut with no tag. Unit was warm but had no unit pressure, buy back was open. Pressured up unit and attempted to dump both condo and water, both were froze. Heater is out of fuel, so I started thawing on the dump inside the cabinet, as well as the unit dump outside of the cabinet. Got the unit dump freed and got it dumping, water dump was still froze. Finally got both dumps free and started flowing the well. Unit transmitter froze thawing on that now RTP'd well Choke is pinched to allow well to flow out. OPS will need to come back and open choke back up. ",user_56,asset_341,48.1470144,-103.6180489
12/10/2018,Separator,Temp Control System,Pilot,,,,Pilot was plugged ,user_94,asset_355,,
2/16/2018,Heat Medium,Surge Tank,Regulator,,,,"Line heater was done found fuel gas supply froze at inlet to scrubber, line heater needs a building to cover all fuel gas lines an regulators ",user_122,asset_1675,48.38750187,-103.8416664
2/26/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Dumped scrubbers on both 4 packs and the T-pack and heard minimal liquid going through. Dumped the Desi scrubber but had to thaw the above ground piping on the drain before it would open up to allow flow through. OPS attempted fixing small holes in the insulation but this may require heat trace as well as insulation to ensure these lines can not freeze.,user_6,asset_1394,36.2541889,-91.2478009
2/25/2018,Tanks/Pits,Flare/Combuster,,,,,Unit lost pressure. Rtp SCC ,user_153,asset_245,48.20341068,-103.6281125
10/18/2018,Separator,Choke Valve/Loop,,,,Freezing,Found that the DVC was opening on the on cycle . Thawed out supply gas and DVC and got choke to open. Function tested choke and rtp'd well plunger making arrivals.,user_10,asset_455,43.252261,-115.0567324
2/19/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Drained scrubber while on location working on burner. No fluids present.,user_62,asset_1556,48.1470144,-103.6180489
5/24/2018,Tanks/Pits,Flare/Combuster,,,,,"Well was shut in and tagged during WFS TAR for maintenance to remove compressor and install new one. Location was brought back on, Lit SCC B",user_62,asset_1092,40.7126799,-114.1193569
7/16/2018,Flare System,Flare Header,BMS,,,,Issue: found SCC # 4 down on the HMI Root Cause: looks like the rain storm from this morning flooded the pilot out Fix: relight and returned to service. may want to look into putting the pilot horizontally instead of vertically. may help from it getting snuffed or flooded out when it rains ,user_170,asset_57,48.2610458,-102.89989
5/11/2018,Compressor,Intrumentation,,,,,Compressor went down on high suction pressure I cleared alarm and restarted. Compressor went back down on high suction I went to location and made a slight adjustment to suction controller restarted and put back online.,user_51,asset_1774,48.1470144,-103.6180489
10/12/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,With all wells in off cycle units do not carry enough volume for offtime duration to maintain above ESD set point due to SCC pilot gas usage. Relight SCC's. ,user_75,asset_638,,
3/25/2017,SWD System,Other,Other,Other,Other,Other,,user_117,asset_1633,40.5481548,-114.0112915
8/22/2017,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"well was loaded and deferring, vented plunger and put back on cycles 22AUG17",user_53,asset_354,48.0614644,-104.8417043
4/25/2019,Separator,ESD Valve,Actuator,,,Corrosion, +ESD ACTUATOR IS BAD CANNOT OPEN- WM ENTERED FOR REPLACEMENT- NONE ON THE SHELF CURRENTLY,user_34,asset_1135,40.5262342,-113.8824849
12/11/2017,Heat Medium,Pump,Seals,Texam,HBC1,Weather,Re-it pilot on line heater. Scrubber filled full of fluids and caused burner to run out of gas. ,user_62,asset_1212,48.1470144,-103.6180489
2/5/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,Cyclonic blow down valve froze due to internal leak. Thawed blow down valve and turned in work management to have cyclonic blow down valve replaced. ,user_44,asset_138,,
12/12/2017,Wellhead,Wellhead Piping,,,,,Had a freeze after high low. It's been brought up to engineering that we need to take the riser out going into the separator. ,user_101,asset_1441,47.9780275,-103.4243334
9/14/2019,Separator Inlet Valve (XV),Pneumatic Control System,Diaphram,,,,"Upon arrival found 10 well shut in and tagged out for psi build. Opened master valves and fount tbg psi @ 385 and csg psi @ 326, spoke to optimizer and found well had been vented and was flowing as of 9/13/19 but no reason as to why well was shut back in because the plunger was running. Optimizer kicked well off and plunger made an arrival, pulled and inspected plunger, found a 2 3/8 dual pad worn with the pads sticking. Installed new 2 3/8 dual pad and let optimizer know so cycles could be reset. Also while well was flowing found that the fuel supply from the dvc to the choke was leaking out the back of the choke. Entered WM to maintenance for repairs, spoke with optimizer to verify we wanted to keep the well flowing, its not leaking enough to load off the well or interfere with the choke operation so left well flowing, it only leaks while choke is open and not in offtime.",user_177,asset_2045,40.5262342,-113.8824849
1/5/2018,Separator,Choke Valve/Loop,,,,Freezing,"Pumps and burners had not been started yet, the well has been down for over a month. Had to thaw out high water dump line.",user_62,asset_1497,48.1470144,-103.6180489
7/17/2018,Wellhead,Tubing,,,,,well has a hole is tubing but we do not own this well just operate it ,user_11,asset_653,43.252261,-115.0567324
3/2/2017,Chemical System,Pump,Other,Other,Other,Other,,user_50,asset_1732,47.98598,-103.4255624
1/2/2018,Fuel Gas/Start Gas,Regulator,,,,,"DVC to sales valve (D4) was frozen, very little fluid in regulator, would like to see electronic valves on the 3 wells on this location, talking to previous operator this is a problem every winter",user_88,asset_1793,48.1470144,-103.6180489
11/16/2017,Flare System,Flare Header,Process Indicator,,,,,user_48,asset_274,,
2/25/2018,Tanks/Pits,Flare/Combuster,,,,,Pilot plugged. Regulator frosen. Cleaned pilot broke freeze. Rtp,user_153,asset_1212,48.32981769,-103.7004847
9/15/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Ajax,,Freezing,Cat compressor went down on high discharge,user_24,asset_1350,48.3619066,-103.2129855
4/12/2019,Wellhead,ESD Valve,Actuator,,,Liquid Plugging,Solenoid was fine for the ESD. Gas was blowing out of the vent when trying to open. The diaphragm in the ESD was bad due to possible fluids or freezing in the fuel gas line. Replaced ESD actuator and opened ESD.,user_108,asset_18,,
4/28/2018,Compressor,Compressor (Intergral),Process Gas Supply,,,,"Sibera 30-comp, found recycle open at 70psi should be opening at 45psi, isolated recycle until archrock can come back and reprogram controller. Went down a few hours later on low suction RTP.",user_71,asset_2241,48.1470144,-103.6180489
4/21/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Vented well due to non arrivals. Plunger arrived, RTP'd well, started cycles, and return to optimizer.",user_141,asset_1570,48.1470144,-103.6180489
6/13/2017,Plunger System,Plunger,Plunger,IPS,,No Liquid,Plunger came in on vent rtp'd ,user_131,asset_2042,47.99744108,-103.7155299
10/26/2019,Plunger System,Plunger,Plunger,PCS,,Not Optimized,This well has the downstream valve on it and with the pumps and burners running it can get the well loaded up . Vented well to unload and contacted optimizer to add off time to the cycles because of the fuel gas consumption. ,user_10,asset_269,40.5262342,-113.8824849
1/3/2017,Compressor,Compressor,,,,,Compressor went down on low suction; this compressor is oversized for this pad if we lose a well or production is down on key wells the the compressor will go down. This location needs to be reevaluated for a possible smaller compressor ,user_148,asset_1124,48.32424159,-103.6004735
10/16/2019,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"walked through well 140 with contractor and put well into cycles, plunger did not make arrivals and well was vented / after contractor was set up on vent I left location.",user_10,asset_477,40.5262342,-113.8824849
12/12/2016,Compressor,Compressor,,,,Freezing,Comp went down on low suction this is due to the whole pad shutting in. I looks like that all the cycling well were in a off cycle and the free flowing well loaded up. Brought pad back on stage ring well cycles and equalized the free flowing well.,user_11,asset_835,,
4/8/2017,Heater Treater,Firetube,Other,Other,Other,Other,Emissions ,user_156,asset_1087,48.21228803,-103.6391832
10/27/2019,Separator,Temp Control System,Fuel Gas Supply,,,,"Both burners were down on this location, the pilots we were lit but the Mains were shut in, last time I was here they were open. I got the quad pak farthest from the turnaround on first with Bretts help. The quad closest to the turn around's main would not open, I verified the pilot was on and checked fuel gas pressure to the solenoid but nothing. Next I warmed up the solenoid and this still did nothing, as a last resort I heated up the valve body then had Tate send the command and she came open, must have been a little moisture in the valve that froze. ",user_22,asset_193,46.2356189,-100.6010498
3/18/2018,Flare System,Flare Header,Regulator,,,,"SCC would not light remotely, relit scc",user_141,asset_1894,48.1470144,-103.6180489
6/12/2019,Automation,ESD,,,,,"esd will not actuate, attempted to reset trip plate. work management submitted",user_17,asset_606,,
11/25/2018,Flare System,Flare Header,Instrumentation,,,,Issue: Arrow Dispatched for SCC down Root Cause: SCC # 3 down on thermocouple error Fix: relight using the on board system. everything look good ,user_170,asset_1417,,
3/1/2017,Instrumentation,Transmitter,3n1 MVT,Rosemount,4088,Passed Function Test,,user_113,asset_793,48.35939991,-103.7781782
12/29/2017,Fuel Gas/Start Gas,Regulator,,,,,Big joe needed adjust to get main valves on bath heater to stay open.,user_0,asset_1841,48.1470144,-103.6180489
7/11/2017,Gas Scrubber Separator,Dump Line,,,,Erosion,Replaced with new 5000# Baylon Valve,user_119,asset_180,48.1602414,-103.6172565
12/17/2016,Compressor,Compressor,Scrubber Level,,,Freezing,Dump lines from compressor froze off near desi dryer ,user_148,asset_1124,48.32437948,-103.6009647
11/9/2016,Gas Scrubber,Dump Line,Dump Line,,,,Meter on water dump stuck from sand,user_152,asset_1374,,
12/30/2018,Separator,PSV,Body,,,Incorrect Set Point,Hi lo failed and let the unit pressure get up to 844 psi.,user_121,asset_734,48.1494775,-103.6215165
7/12/2018,Separator,Fuel Supply System,Regulator,,,debris,"Well had lost unit pressure. Cleared alarms, opened ESD and started cycles.",user_141,asset_1642,48.1470144,-103.6180489
4/24/2018,Flare System,Flare Header,BMS,,,,Issue: found SCC (D) down Root Cause: (INT) valve not in auto. never seen that one before Fix: relight remotely ,user_136,asset_548,48.2595694,-102.9009394
2/26/2018,Heater Treater,Burner,BMS,,,Pilot Went Out,Issue: found the bath temp was 39deg on the HMI Root Cause: looks like the bath went out and then the fuel gas froze in the coils somewhere in the bath Fix: will need a jumper installed to get fuel gas to the scrubber. then heat the bath up and the freeze should break,user_136,asset_1160,48.2594584,-102.9010654
12/27/2018,Separator,ESD Valve,Gas Supply Line,,,Freezing,"hi low controller was frozen and got damaged, replaced",user_31,asset_1212,48.257296,-102.8606112
1/18/2018,Automation,Cable,Data Cable,Automation-X,,Electrical Short,CG 4-150 callout on valve fault. ESD showing in travel on HMI but is fully open. Automation needs to check out.,user_71,asset_385,48.1470144,-103.6180489
6/3/2019,Instrumentation,Meter,Orifice Plate,Nuflo,1,Passed Function Test,"Complete Scheduled Calibration and Plate Inspection, Call Travis Morgan to have Control By-Pass Set & Removed. ",user_139,asset_638,,
9/13/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Pilot was plugged was not able to light glycol bath. Shut in fuel gas and removed pilot tip and cleaned and put back in. Relit and got bath going ,user_52,asset_785,48.20060345,-103.5384135
7/30/2019,Separator,Burner,Fire Tube,,,Pilot Went Out,Pumping Unit was down on high pressure. It acted like there was a flowline freeze or the back pressure valve plugged off. I shut casing and popped it to the tank and that fixed whatever it was. Opened back up casing and started unit. Also cleaned out pilot. ,user_94,asset_2011,46.2356189,-100.6010498
4/30/2019,Instrumentation,Meter,Orifice Plate,Control Micro,4203DR,Passed Function Test,"Checked Meter and Called Brett K. and discussed Meter issue, Brett said that he would watch this meter for the next few days. Looks like that Meter was Over-Ranged for a brief time. ",user_139,asset_1910,,
9/27/2017,Separator,Temp Control System,Pilot,,,,"Found pilot woofs out when burner kicks on. Found pilot light was 6-8"" away from main burner. Moved pilot light right next to burner and returned to service. Kicked burner off and on several times to make sure the issue had been resolved. Issue corrected. ",user_62,asset_1212,,
6/6/2017,Separator Inlet Valve (XV),Pneumatic Control System,Diaphram,,,,"Dispatched to site to check out no flow, found the fuel gas to hi low broke, brittle from age, replaced line and rtpd , 600 mcf day well",user_84,asset_1467,48.02116074,-103.5252144
2/1/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,Plunger worn,user_126,asset_1368,,
4/5/2018,Heat Medium,Pump,Diaphragm Gears,Texam,113,Freezing,"while doing location walk through, noticed heat trace was cold around 3 well heads. Checked pump and it was turned on and stroking once every 10 seconds. Walked through piping and found the return line from the heat trace around well heads were it goes back into the bath in the separator was closed. Only thing the the pump was heating was the desi dryer. No tags found, opened valve and pump took off stroking. Walked through all well heads and validated no leaks and heat trace was warm. Root cause is human error. The valve was closed for an unknown reason and never opened back up when the pump was started.",user_62,asset_1413,48.1470144,-103.6180489
1/9/2019,Separator,Dump Line,,,,Freezing,dump lines frozen williams also shut there sales line valve and was the root cause of hup,user_121,asset_994,48.3572384,-83.27272
12/13/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Found that the burner was out and the big joe was frozen thawed and restarted burner.,user_100,asset_36,48.1470144,-103.6180489
3/19/2018,Separator,Choke Valve/Loop,,,,Freezing,unit had an inlet freeze,user_179,asset_2099,48.1470144,-103.6180489
6/24/2019,Plunger System,Wellhead,Integrity Failure,,,,Set Screw for the plunger catch backed out of the lubricator and caused gas release. Plunger catch was rebuilt and well is ready to RTP.,user_68,asset_1463,48.1511744,-103.6275517
11/9/2018,Flare System,Flare Header,Regulator,,,,"ESD closed for Valve misalignment. No apparent cause determined. ESD opened up, and was able to RTP well. Relit SCC while on location",user_55,asset_2225,,
12/7/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Freezing in fuel gas system,user_126,asset_1662,,
8/24/2018,Wellhead,Manual Valve,Body,,,Erosion,"When doing location walk down, noticed upper master valve was leaking out stem packing. Installed 2 sticks of packing and got leak sealed. ",user_15,asset_1992,48.3085045,-103.6755158
11/25/2017,Tanks/Pits,Tank Level,Probe,,,Weather,Got a callout for high tank. Investigated and found Condo tank at 17ft 1in. Texted gauge data to team lead and shut well in.,user_141,asset_1952,48.1470144,-103.6180489
11/14/2017,Compressor - Gas Lift,Compressor,Valves,Compressco,,Electrical Short,Did the start up on this gas lift. Went down several times when trying to set kills and recycles. Rtp gas lift currently injecting into the 20. 50 has WOR installing man,user_172,asset_1276,,
8/18/2017,Separator,ESD Valve,Gate/Seat,,,Corrosion,Hi lo wasn't holding. Shut in well did lock out changed out trim and seat rtp well,user_172,asset_994,,
7/10/2019,Wellhead,Plunger,Lubricator Top,ETC,,No Liquid,"50 well RTP well and it's frozen, started methanol pump, replaced the PRV, ended cycles and pumping methanol down tubing. 130 well is frozen, tightened packing, pump already on, ended cycles to break freeze. 60 well attempted to RTP, well is frozen, tightened packing on pump and ended cycles to work on breaking freeze, has a bad lubricator cap that needs replaced. 120 well is frozen, replaced regulator and packing on pump and started methanol down tubing, ended cycles. Also has a bad lubricator cap. 70 well has a bad methanol pump, cycles don't look great. 10 well is frozen, started methanol pump. 160 well doesn't look great, has a bad methanol pump, replaced packing but the bottom check valves are bad. 7/10/2019 leak tested surface equipment leaking chokes on 70, 160, 20, 60, 130, 50 wells, leaking blowdown valves on the 20, 130 & 50 wells causing wells to freeze and load up. 50 well plunger is hitting top master valve and isn't coming in, top master is damaged and doesn't open or close, shut well in. Replaced methanol pump on 70 &160 wells. Methanol working on all wells except the 150 well and going down tubing. 60 well is still frozen. Lubricator caps replaced on the 20 and 60 wells",user_31,asset_386,48.2515616,-102.8696224
10/3/2017,Separator,Temp Control System,Electrical,,,,"Automatic valve on main burner doesn't open, separator flowing at 35'F and temperature drops down In the night to freezing temperatures, could cause a Hydrate on separator or dump valves. ",user_60,asset_1783,47.96441345,-103.5553083
3/31/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"line pressure bump, loaded, vented and RTP",user_88,asset_167,48.2630325,-102.8997889
2/27/2019,Separator,Choke Valve/Loop,,,,Freezing,"flow line was frozen in the flow line, this is a satellite well frozen underground and in the upright at the unit. ",user_10,asset_38,39.2506642,-92.4357879
2/23/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,Issue: well called out (Keep alive alarm) from hi MVT pressure Root Cause: shut in cycles are trying to build the well pressure up to hi and come on to hard for the ambient temp and is freezing off in the meter run. don't want to turn bath temp up to prevent carry over Fix: flowed the well out slower and got some of the pressure off of it and restarted the cycles ,user_136,asset_729,48.2629356,-102.8996131
7/21/2018,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,well shut in on false high tank. verified all tank levels are low. rtp well,user_120,asset_1083,43.252261,-115.0567324
4/13/2019,Separator,Choke Valve/Loop,,,,Freezing,"There was a freeze in the inlet by the Hi Lo valve, I cut open the insulation and used thaw tube to clear it, I then retaped everything back up ",user_22,asset_476,46.2356189,-100.6010498
11/8/2017,Compressor,Compressor,Suction Controller,Ariel,,Freezing,found two wells in end cycle restarted and blew out suction control valve. compressor back in service,user_11,asset_940,48.1470144,-103.6180489
8/28/2017,Compressor - Gas Lift,Engine,Cooler,Cummins,,Overheat,"water jacket temp got high, when I was here earlier I should have opened the doors up all the way to keep temp down it is 90 degrees now",user_176,asset_1873,48.3619066,-103.2129855
1/18/2017,Compressor,Engine,Water Pump,Other,Other,,Engine down on high coolant temperatures ,user_131,asset_2073,47.88298133,-103.5121436
3/7/2017,Instrumentation,Transmitter,3n1 MVT,Other,Other,Passed Function Test,None found ,user_113,asset_26,48.35415698,-103.8105456
4/17/2017,Compressor,Engine,Other,Other,Other,Other,,user_35,asset_602,48.32660039,-103.5839343
5/29/2018,SWD System,Particle Filter,Element,,,,Filters plugged. Replaced filters ,user_156,asset_523,48.37798623,-103.8548492
1/15/2018,Compressor,Compressor (Recip),Lubricator,,,,"Compressor went down on low compressor oil pressure, everything looked good restarted compressor let it run and it ran good. RTP'd well ",user_53,asset_1945,48.1602349,-103.6171353
5/14/2019,Pipeline/Piping,Tank,Load Line,,,Weather,"water dump valve and fittings leaking, due to wear, , possible freezing during the winter, ",user_77,asset_2268,46.2356189,-100.6010498
8/5/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,"ARROW Well was dispatched because of its deferral. Looked at the graph and notice it was cycling but not producing any volumes Got to location and found TBG at 449 CSG at 1073 Shut ESD and then opened to AGT and found that the flow line was froze, broke freeze and put back to sales TL was notified about well being out of methanol and he was getting it ordered. ROOT CAUSE, out of methanol RTP'd well",user_56,asset_1305,48.2649267,-102.8790454
5/13/2018,Separator,Choke Valve/Loop,,,,Freezing,Well had its burners shut off for summer OPs. Hydrate found in choke. Warmed bath back up and broke freeze and turned off bath again.,user_107,asset_507,,
3/11/2019,Compressor - Gas Lift,Compressor,Scrubber Level,Leroi,,Trash,Trash in check valve for scrubber dump on second stage.,user_54,asset_1452,40.5262342,-113.8824849
3/4/2019,Surface Location,Well Pad,,,,Weather,Still have a lot of snow on location. I do have salt in the buildings for truck drivers to use at their discretion. ,user_55,asset_101,,
3/17/2019,Separator,Liquid Dumps,Controller,Norriseal,,Corrosion,"Norriseal controller door was seized shut, once opened the control arms and displacer arm would not function due to extreme build up also the snap was leaking very badly, new snap had to be installed.. ",user_174,asset_961,39.2506642,-92.4357879
7/16/2019,SWD System,Piping,Discharge Line,,,Debris,Remove and clean all nozzle. Clogged with stuff from ponds. RTP'd pump,user_55,asset_1571,,
12/10/2016,Gas Scrubber,Dump Line,Dump Line,Other,Other,Corrosion,Hydrate in condensate line caused threads on hammer union to strip causing leak in the line ,user_103,asset_63,48.19647792,-103.619345
9/4/2017,Compressor - Gas Lift,Compressor,Suction Controller,Compressco,,Freezing,methanal sstopped pumping replaced fuse RTP flowing,user_176,asset_1359,48.3619066,-103.2129855
9/28/2018,Generator,Engine,Battery,PSI,,Human Error,Battery failed due to multiple re-start attempts. Replaced battery.,user_108,asset_92,,
12/12/2018,Tanks/Pits,Flare/Combuster,,,,fuel gas freeze,"Found SCC A was out, fuel gas header was froze from liquid drop out from cold temps. Thawed line, blew out liquids and lit SCC.",user_15,asset_793,43.56424,-91.351691
11/13/2017,Separator,Temp Control System,Heater/Burner,,,,Burner was off turned back on and got glycol pumps going to prevent another flowline freeze.,user_51,asset_968,48.1470144,-103.6180489
5/24/2018,Automation,Radio,Wiring,3M,,Unknown,"CB 19-pad high tank callout 2 tanks showing 19-0ft, false alarm.",user_71,asset_464,48.1470144,-103.6180489
10/7/2017,Compressor,Compressor (Recip),Scrubber Level,,,,VRU compressor. Down on high scrubber levels. Several times a day. Drained and rtpd,user_163,asset_1675,48.38713089,-103.8414582
11/29/2018,Separator,Liquid Level Control,,,,,"Unit was down, lost pressure. Pressured unit up. Lit glycol bath and checked dumps. Water dump was a little tight, adjusted it where it feels better. Adjusted condo dump. ",user_55,asset_1054,,
3/16/2017,Wellhead,Fixed Orifice Choke,Stem/Seat,Other,Other,Erosion,"Hi/Lo trim and seat leaking by due to erosion, cutting seat",user_141,asset_444,48.3619066,-103.2129855
6/5/2018,Separator,Choke Valve/Loop,,,,Corrosion,None,user_173,asset_1352,48.1470144,-103.6180489
8/16/2017,Wellhead,Manual Valve,Casing Valve,,,Corrosion,Replaced KF Vavle with new 5000lb Balon Valve,user_119,asset_1576,48.1604246,-103.6171287
3/1/2017,Instrumentation,Transmitter,3n1 MVT,Rosemount,4088,Passed Function Test,None found ,user_113,asset_1600,48.36110009,-103.6353116
9/25/2019,Plunger System,Plunger,Plunger,PCS,,Corrosion,"plunger old, longer cycles, surfaced in cycle and changed out dual pad for dual pad, RTP in cycles...very worn one side",user_106,asset_1570,40.5262342,-113.8824849
9/18/2019,Separator Inlet Valve (XV),Pneumatic Control System,Hi/Lo Pressure Controller,,,,Found hi-lo valve(Safety device) not working properly. It was staying closed. The relay or block and bleed was bad causing the valve not to close. Block and bleed was replaced and well returned to production.,user_83,asset_672,40.5262342,-113.8824849
1/16/2019,Gas Scrubber Separator,Dump Line,,,,Freezing,"arrow dispatch. left location at around 13:00, hot oil has not been on location. spoke with team lead and they should have water tanks hot oiled by the end of today 1/16.dumps on high pressure unit are free,drained scrubbers on both 20&50 not much fluid. LP scrubber was nearly half full. oil dump is open on LP. water line has a partial freeze on LP to tanks.you can get water to dump but its very slow. hot oil will fix this issue. burner was out on line heater, pilot tip was plugged with a little fluid,cleaned out and relit.all heat trace is running tank temps are starting to increase.shot outside water tank 23 degrees. oil was around 40.removed jumper from sales line and logged it in enbase. pilot fuel gas to abutecs is froze back at tank lines.attempted to thaw out but couldn't get to break. someone with a long thaw tube will need to try again.opened the 20 choke 100%, 50 is around 45/64th. will open fully after tanks get hot oiled. separators are keeping up with fluids and looks good (besides water dump on LP).need operator to return tomorrow 1/17",user_120,asset_1760,43.56424,-91.351691
2/22/2019,Separator,Dump Line,,,,Freezing,Water dumps froze due to inadequate heat trace ,user_18,asset_44,,
4/10/2019,Flare System,Flare Header,Instrumentation,,,, +TWO SCC'S OUT DUE TO WIND AND SNOW- *RELIGHTED,user_34,asset_1108,40.5262342,-113.8824849
4/25/2018,Dehy,Pump,Diaphragm Gears,Texsteam,375,Wear,Found Williams glycol pump dry stroking. Shut pump down and contacted Williams tech,user_172,asset_876,,
8/8/2018,Gas Scrubber Separator,ESD,,,,,"Champ CALLOUT 263 B-10 pad went down on valve fault, maintenance has #10 & #140 shut in for cyclonic valve replace, jumped pad on, open shared fuel gas to keep units up. with loss of 2 wells 4 out 9 wells are shut onsite. RTP and started cycles.",user_37,asset_1280,48.1470144,-103.6180489
12/29/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"No plunger in hole, I dropped a new viper",user_84,asset_2130,48.06806524,-103.531723
2/2/2018,Flare System,Flare Header,Process Indicator,,,,Scc was out because the weather ,user_48,asset_277,48.22220223,-103.7528641
3/24/2017,SWD System,Other,Other,Other,Other,Other,,user_117,asset_2012,40.5481548,-114.0112915
9/21/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Trash,"found compressor down , lo suction, found no on skid or off skid recycles, contacted TL and PE is working on fix, contacted Archrock to see if low set points could be lowered, but that was as low as was allowed. was able to pinch back discharge injection to well to get suction pressure and 1st inter-stage to stay above low kill set points and open enough not to high psi the discharge",user_144,asset_2165,48.224585,-103.8291059
9/1/2018,Flare System,Flare Header,BMS,,,,Location had 1 SCC out. Was not able to light remotely. Relit SCC and returned it to service,user_55,asset_41,,
12/1/2017,Wellhead,Manual Valve,Ball,,,End Of Useful Life,"Ball valve on casing is leaking, showing pressure on tubing and casing as equalized. Flowing like normal, nothing wrong with production ",user_1,asset_1214,47.88257498,-103.4114279
1/28/2018,Tanks/Pits,Flare/Combuster,,,,,Scc down due to depressured unit. Re lit rtp scc,user_153,asset_617,48.30741424,-103.6408827
8/24/2017,Separator,Choke Valve/Loop,,,,Corrosion,Choke packing leak,user_111,asset_747,48.02822299,-103.3719033
2/1/2017,Automation,RTU,IO,Amocan Cams,GFC,Human Error,"Run status signal was wired into incorrect scada, it was not landed into the host scada. It is working correctly now ",user_74,asset_602,48.2159539,-103.651452
7/27/2018,Compressor - Gas Lift,Engine,Control Panel,Waukesha,,Human Error,"Found compressor was started and put into manual. This sets the compressor to run at 1275 RPM, this is not high enough to make the compressor inject the desired rates. Turned compressor to manual and ran RPM up to 1500. Root cause is human error. It is wrote in big bold black letters to run the compressor in manual at 1500 RPM on the control panel. ",user_15,asset_1452,48.1470144,-103.6180489
5/1/2018,Flare System,Flare Header,BMS,,,,"Flare out apparently wind blew pilot out. Relit flare and returned to service. Root cause flares pilot blows out at 15 to 20mph wind, and we still need to figure out a wind block to keep flares running. ",user_58,asset_580,48.37298362,-103.5176964
12/6/2017,Compressor,Compressor,Scrubber Level,Ariel,,Vibration,"the line coming out of the 1rs stage scrubber has a crack, and is leaking gas inside of the compressor building.",user_130,asset_1346,48.1470144,-103.6180489
11/5/2019,Automation,Cable,Data Cable,Automation-X,,Electrical Short,Found choke was not openeing. Tapped DVC and it opened up. Drained fluid from Kimray pot. OPs to write WM for DVC is problem continues,user_147,asset_51,,
1/5/2019,Heater Treater,Burner,Flame Arrestor,,,Freezing,"Arrived on location and found all burners on 3 t packs up and running, but heater treater was down and froze. Configuration of heater treater is that it pulls gas from vessel to keep burner up and running. With location down we could not get any pressure in unit to run burner. Talked to Area Manager and engineering and got approval to run stainless line from separator scrubber to scrubber on heater treater. Engineering working on a permanent installation. Got heater treater burner running to warm it up and thaw it out. ",user_15,asset_1574,48.1603431,-103.6187683
4/27/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Drained desi while on location. Took 10 seconds for fluids to drain.,user_62,asset_1677,48.1470144,-103.6180489
2/28/2019,Pipeline/Piping,Pipe/Components,,,,Human Error,"Well shut in for rig work, found equipment blocked with snow. put gas to vessels check to make sure dumps were clear, all where except water on lp. got burners going flowed well on pinched choke until snow removal and water dump can be thawed. Also needs wellhead insulated and heat traced.",user_63,asset_2069,,
4/20/2017,Wellhead,Other,,Other,Other,Other,no sales,user_39,asset_1723,48.1470144,-103.6180489
1/28/2018,Tanks/Pits,Flare/Combuster,,,,,Scc out due to pad being down. Re lit rtp scc. ,user_153,asset_886,48.3073971,-103.6408626
3/2/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,"able to thaw flow line inlet and tubing transmitter. jumped well back on, lit burner and temped up unit. water dump freeze, condo clear. started cycles in off cycle",user_17,asset_1135,,
4/20/2018,Tanks/Pits,Flare/Combuster,,,,,"SCC B, one of the air vents on the side of the combustor was closed. I opened it back up, with these closed the combustor can starve for air and possibly smoke. Root cause is human error. Unknown reason why it was closed. ",user_62,asset_1675,48.1470144,-103.6180489
3/13/2018,Separator,Liquid Dumps,Controller,Fisher,,Improper Adjustment,"40 well had no issues on levels, flowing temp at 80 degrees turned down burner 10 same as 40 60, adjusted both water and condo dump levels down along with burner temp, well takes massive slugs prior to plunger arriving 30, adjusted burner temp no issue with levels",user_115,asset_1662,,
3/14/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,tried venting plunger didnt come in sipb,user_11,asset_98,40.7126799,-114.1193569
4/20/2018,Separator,Liquid Level Control,,,,,Found condo dump controller door in the open position. Root cause is human error. Some one did not close it last time they opened the dump controller door. Closed door.,user_62,asset_2066,48.1470144,-103.6180489
4/16/2018,Heater Treater,Vessel,Fuel Gas Scrubber,,,Corrosion,.Heater treater burner shut in manually at the fuel gas supply valves with no tags. Confirmed with Off shift OPS that it should be on and RTP'ed.,user_6,asset_1383,36.2541889,-91.2478009
1/23/2018,Separator,Dump Line,,,,Freezing,Condo dump line was frozen due to glycol pump being shut off with no tag as to reason why. Started pump and thawed oil dump.,user_62,asset_333,48.1470144,-103.6180489
4/16/2018,Gas Scrubber Separator,Dump Line,,,,Erosion,at 2:00am checked site drained scrubbers equipment working good. ,user_71,asset_1035,48.1470144,-103.6180489
2/21/2019,Tanks/Pits,Tank Level,Sensing Cable,,,Weather,"high tank, waiting on hot oil and turn around plow. ",user_17,asset_1030,,
9/18/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_1633,,
5/14/2019,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,High tank alarm I went to location 28706w 2ft 10in x 0ft 2in 28706c 0ft 11in x 0ft 0in 28705c 7ft 9in x 0ft 2in FALSE ALARM I cleared alarm and brought wells back online. ,user_159,asset_1729,48.3619066,-103.2129855
11/1/2017,Compressor,Compressor,Suction Controller,Ariel,,Freezing,compressor down on low suction pressure. 10/31 i shut the 70 well in for a pressure build so i could change out pacemaker sleeve 11/1 and there was quite a bit of fluid that i drained out of the suction control valve. i drained suction control valve and ensure proper function and changed out worn pacemaker sleeve. returned compressor back into service.,user_11,asset_605,48.1470144,-103.6180489
2/27/2018,Instrumentation,Meter,Orifice Plate,Nuflo,Wonder Card RS232,Freeze,Issue: called out non stop every 5minutes for no flow. Root Cause: well is down for a Williams freeze but the meter doesn't have any cover so its freezing in the meter causing a false flow to go in and out Fix: heated meter up and blew out but really needs to be heat traced and a hood installed on it to keep this from happening. The callout also needs to be looked at line putting in a timer before it reactivates or a time delay to keep this nuisance callout from happening ,user_136,asset_1212,40.5481548,-114.0112915
3/26/2019,Surface Location,Well Pad,,,,Weather,Lot of snow and mud on location,user_55,asset_1927,,
12/11/2017,Separator,Temp Control System,Pilot,,,,Pilot out,user_50,asset_38,48.32413221,-103.6176797
10/17/2018,Compressor - Gas Lift,Compressor,Panel,Sertco,,Freezing,"Arrived on location and checked compressor, it was down on low discharge pressure. Set point is 300 PSI for low pressure. Pulled graphs on well and saw casing pressure dropped to 294, causing compressor to shut down. Well was flowing good, unsure if when we are at orifice valve in well if that will drop casing below 300. Emailed engineering to get some answers, waiting to hear back. Started and warmed up compressor. Loaded and watched injection, injecting at 750 MCFD, well starting to unload. ",user_15,asset_2138,48.2814835,-102.8554247
5/6/2018,Separator,Fuel Supply System,Regulator,,,fluid,"Found and drained approximately 6 OZ of fluid in first scrubber on line heater. This is due to warm temperatures of fuel gas upstream (well flows at 120F) and the end devices (line heater scrubber) sitting at ambient temp (58 F). ENG to further trouble shoot and supply plan forward. There is a shut in sivals unit onsite that does not appear to be doing anything, we could utilize it as a fuel gas scrubber.",user_6,asset_1675,36.2541889,-91.2478009
3/18/2019,Surface Location,Lease Road,,,,Weather,Location drifted shut. 3-18-19 Plowed location access road & turnaround. ,user_42,asset_1251,46.2356189,-100.6010498
5/14/2019,Separator,Dump Line,,,,Erosion,Kimray packing leaking causing it to appear that the D4 was venting gas.,user_63,asset_2034,,
11/4/2018,Separator,Fuel Supply System,Regulator,,,freeze,"Gauge for fuel gas supply to main burner and pilot not reading correctly, likely due to a freeze in the past, stretching the bourdon tube out.",user_54,asset_820,48.3580576,-83.27272
12/1/2017,Plunger System,Plunger,Plunger,Trip Mate,,Not Optimized,"Issue: found whole pad shut in Root Cause: pad shut in on low unit pressure from all the wells being in off cycles at the same time. when there is no gas moving the 4glyocl pumps, 2burners, 4 SCC's 6meth pumps are using up the unit pressure unit it gets to low and shuts in Fix: the optimizer needs to get the cycles so all the wells are not in the off cycles at the same time. long term fix buy back meter",user_136,asset_2126,48.2594193,-102.9011364
11/29/2016,Tanks,Shell,Body,,,,On Monument 11-50 the heat trace is not hot enough to keep the sump thaw up after going in and out on all the tanks on site. The valve to empty the sump and the bottom/ water on the sump was frozen and can't get it empty. This pod goes to SCCs,user_60,asset_1276,48.36871048,-103.5264996
1/9/2019,Separator,Choke Valve/Loop,,,,Freezing,"Inlet freeze in choke loop, unable to open or close choke. Thawed and broke freeze, verified choke would open and close. ",user_44,asset_522,,
1/21/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,I vented plunger to surface and put back on plunger cycles.,user_51,asset_2035,48.1470144,-103.6180489
1/2/2018,Flare System,Flare Header,Regulator,,,,Issue: Called out SCC alarm. SCC (A) down Root Cause: found the fuel gas line was froze underground. The fuel gas line to the SCC's should periodically be blown down to clean the line out from residual build up Fix: broke freeze and got relight. ,user_136,asset_844,48.1470144,-103.6180489
10/16/2017,Compressor,Cooler,,,,,It had a cooler freeze due to temp change,user_51,asset_1366,40.5262342,-113.8824849
8/22/2018,Instrumentation,Controller,,,,,"ARROW PLUS Well is deferring, and DVC is not opening choke and allowing well to flow Got to location verified that the fuel supply to the DVC was dry, then checked the pressure to DVC. Adjusted pressure and then tapped on DVC then sent a 50% command open to the DVC Finally got it to open, baby sat choke and flow RTP'd well ",user_56,asset_1564,48.2629926,-102.8866903
5/1/2017,Wellhead,Manual Valve,Needle,,,End Of Useful Life,"Needle valve was old and had seized, was no longer operable.",user_95,asset_909,,
12/14/2017,Instrumentation,Controller,,,,,"Kelvin did not operator pad properly, had all wells on an off cycle at the same time. ",user_53,asset_1193,40.7126799,-114.1193569
4/13/2019,Pipeline/Piping,Pipe/Components,,,,Human Error,Found a nut off of the flange between ESD and 3 way valve. Contacted TL and we discussed issue. Shut well in at the ESD and Sales line. Tagged everything.,user_55,asset_336,,
3/21/2017,SWD System,SWD Pump,Other,Other,Other,Other,"Pump down due to plugged filters causing high tank, trucks can't unload",user_141,asset_1918,48.3619066,-103.2129855
7/8/2019,Separator,Choke Valve,Seat,,,,The automated choke was leaking by and was loading up the well. It was repaired and will need to be calibrated before well is RTP'd.,user_68,asset_18,38.4425988,-95.5406131
10/13/2019,Separator,Fuel Supply System,Regulator,,,fluid,"OPS: Found 5 gallons in scrubber and through buy back line, liquids coming from buy back line, which is needed as wells cycle off of a front end ESD and require buy back gas for fuel gas. ENG to review some combination of T-pack with functional dumps/cold fingers in line with the buy back line to ensure dry gas to sight, or leave upstream DG4's in place and hooked up to the fisher controllers and re-install downstream flow rate controls on all units and install cold fingers and switch back to wells for fuel gas supply to each unit/entire site.",user_54,asset_2184,40.5262342,-113.8824849
2/24/2018,Compressor - Gas Lift,Compressor,Scrubber Level,Ariel,,Liquid Carryover,"down on High Second Stage Scrubber Level. Not sure why, dumps where clear. Put Allmond heater on compressor to heat up. Will try to make it back to restart.",user_141,asset_1264,40.5481548,-114.0112915
3/27/2017,Compressor,Compressor,Other,Other,Other,Other,compressor down high 2nd interstage pressure caused by wfs. dehy running in proper operating condition. compressor bakc in service,user_11,asset_1350,,
9/20/2018,Wellhead,Tubing,,,,hydrate,Issue: Arrow Dispatch for Deferral Root Cause: found the well is froze tubing and casing with all the methanol disconnected Fix: equalized well and left as is ,user_170,asset_367,48.160353,-103.6187826
1/16/2018,Compressor - Gas Lift,Compressor,Valves,Ajax,,Vibration,"down on high discharge from valves swinging, restarted",user_87,asset_345,40.7126799,-114.1193569
7/6/2019,Instrumentation,Transmitter,Unit Pressure,Rosemount,3051,Weather,Actual failure cause unknown,user_12,asset_1727,38.4425988,-95.5406131
2/2/2017,Automation,Plunger Arrival Switch,,EDI,Other,Other,6. Coal Bank 23-100 - MSO issue (Task request) • Tested Cyclops plunger arrival switch • Cyclops tested and verified good • No automation issue,user_92,asset_661,48.3619066,-103.2129855
4/6/2018,Compressor,Compressor,Process Gas Supply,Compressco,,Liquid Carryover,Compressor was down on high suction pressure. Drained compressor. Blew down compressor cleared alarm and restarted ,user_172,asset_109,,
1/12/2019,Chemical System,Piping,Discharge Line,,,Freezing, Found heat trace to well heads was ice cold but warm to tanks. Pinched down return line from tanks to force heat trace to well head. Got glycol to well heads up to 60 degrees. ,user_15,asset_2186,48.1475232,-103.6224672
4/3/2017,Gas Scrubber,Other,,Other,Other,Other,Thawed choke and RTP well,user_62,asset_1576,48.224585,-103.8291059
8/9/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,, Drained desi while on location. Desi took 5 seconds to drain all fluids. ,user_15,asset_102,48.1470144,-103.6180489
11/16/2017,Separator,ESD Valve,Gate/Seat,,,Corrosion,"Component not listed. Cyclonic blowdown valve is the failure. Valve stills needs full tear down. LOTO for roustabouts to replace the 36-70, 80, and 150 well leaking blowdown cyclonics found to be leaking 11/14/2017. Upon completion of repair perform negative test on all three valves. 70 had 59 psi on tbg to test with. 80 had 614 psi on tbg to test with. 150 had 932 psi on tbg to test with. All valves failed negative tests. Negative test ESD and closed choke to unit by shutting all outlets for vessel, blowing vessel down and monitoring pressure on transducer at vessel. All passed aiding in identifying the cyclonic as leak off point. Work cyclonics multiple times. Perform multiple negative tests. All recorded on tbg transmitter at unit that is within the void at test area. Unable to get a passed test. Contact TL, PE, SM, and Optimizer. 20 and 50 wells ready for RTP. Jump 50 well’s ESD. Start and load compressor. Plunger arrives in 53 minutes. Suction pressure 97 psi at plunger arrival. Bypass plunger suspected of losing velocity causing valve rod to fall out and plunger to fall back to bottom. Clutched bypass needed for lower velocity wells. Moved jumper to 20 well and jump ESD. Start cycle after 50 enters afterglow after plunger arrival. Hand over to optimizer to monitor cycles. Develop plan forward for valve failures with engineering for the 70, 80, and 150 wells",user_75,asset_425,,
8/31/2017,Instrumentation,Communication Card,,,,,Check and test data movements to SCADA PLC. Confirm meter data in PLC ,user_113,asset_2105,48.1819064,-103.6141885
5/23/2017,Separator Inlet Valve (XV),Pneumatic Control System,Hi/Lo Pressure Controller,,,,replace HI/LO trim and packing,user_39,asset_761,48.1470144,-103.6180489
3/2/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,"Well kept going down on valve fault (ESD would not show open status so computer system shuts well in on valve fault). Arrived on location, found scrubber pot set for 80 PSI, ESD requires 90 PSI to fully open. Checked PSV setpoint on scrubber pot, it is set for 150. Adjusted big Joe up to 100 PSI. Via HMI, opened ESD and started well on plunger cycles. ",user_62,asset_118,40.5960545,-113.9323891
11/1/2019,Separator,Fuel Supply System,Regulator,,,hydrate,"found pad down because all the fuel gas to the esd's and dvc's were frozen, had to remove all the line and thaw to break freezes and drain all the line . Scrubber pot was not full . Regulators for the esd's and dvc's are mounted outside of the unit causing all regulators to freeze. After thawed alll fuel gas in the system rtp'd wells .",user_10,asset_167,40.5262342,-113.8824849
4/22/2017,Wellhead,Other,,Other,Other,Other,,user_179,asset_895,48.0109587,-103.5426513
5/6/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,"Froze between well and tpak, currently have well isolated and blow down open to tank to clear hydrate",user_22,asset_1308,46.2356189,-100.6010498
7/10/2018,Wellhead,Casing,Lower Casing Head Valve,,,,"Blew casing down, had 146 psi on it.",user_141,asset_2012,40.7126799,-114.1193569
5/27/2018,Automation,RTU,Display,ABB,Scadapack P4A,Electrical Short,"Cg 5-20 shut in on bad transmitter, reset interlock RTP and started cycle.",user_71,asset_1892,48.1470144,-103.6180489
12/20/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Desi and fuel gas scrubber of liquids daily routine auto dump may be a solution to issue ,user_48,asset_1677,48.32663169,-103.6563524
9/21/2018,Separator,Liquid Level Control,,,,,"Arrived on location and was met by oil hauler leaving location. He informed me that there was a lot of water in the oil tank, i told him i would check it out and get it fixed. Checked dumps in green complete, found water dump was not actuating, all fluids were going into oil bucket and then being dumped to heater treater, then water going to tanks. Looked over green complete dumps, looks to me like they just fell out of adjustment from constantly dumping water. Adjusted dump and verified it was dumping at desired set point and would shut off when water level dropped low.",user_15,asset_1383,48.2816758,-102.8553532
7/12/2017,Pumping Unit,Sensor,,,,,Down on Position Fault- Happens about every fifth day - Root cause unknown - Restarted ,user_138,asset_1644,48.16504759,-103.4492315
4/16/2019,Instrumentation,Liquid Turbine,,,,,"LOTO, single block score of 9 due to butterfly valves, and removed flow meter. Had a rock locking the impeller. Removed rock, cleaned meter, and checked impeller operation. All good. Reinstalled and removed LOTO.",user_55,asset_2012,,
12/2/2018,Heat Medium,Pump,Process Indicator,Texam,HBC1,Air Locked,"fuel gas buy back meter doesn't work, too much back pressure",user_31,asset_1559,43.252261,-115.0567324
2/3/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,"Fuel gas scrubber filled up with fluids. Dumped scrubber, checked operation and fuel supply to sales line valve and hi/lo. All good, RTP'd well.",user_141,asset_524,48.1470144,-103.6180489
8/11/2019,Compressor - Gas Lift,Compressor (Recip),Process Gas Supply,,,,"Gas lift compressor down on a power bump, Restarted compressor ",user_31,asset_606,48.0582304,-104.9028768
9/27/2017,Compressor,Compressor (Recip),Packing,,,,Packing was leaking into crank case and venting from the top near turbo. This would be unsafe to run. ,user_123,asset_1143,26.202611,-151.6204667
6/18/2018,Flare System,Flare Header,Instrumentation,,,,3 SCCs out relit a put back in service ,user_58,asset_1915,48.37136763,-103.5203253
11/30/2017,Plunger System,Plunger,Plunger,PCS,,Not Optimized,lost arrivals ,user_53,asset_1689,40.5262342,-113.8824849
8/16/2018,Separator,Choke Valve/Loop,,,,Corrosion,Found choke packing was bad causing a leak. Pulled apart choke and replaced packing. ,user_15,asset_2243,48.1470144,-103.6180489
1/25/2018,Separator,Choke Valve/Loop,,,,Freezing,DVC drip pot had about 1 ounce of fluid in it and had the thawed the DVC to get the choke to close,user_100,asset_2032,48.1470144,-103.6180489
2/8/2019,Fuel Gas/Start Gas,Regulator,,,,,Fuel gas line to the choke got plugged. Carry over liquid from when the unit was down for frozen dumps. ,user_83,asset_1570,40.5262342,-113.8824849
1/6/2019,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,"Got to location and found that well was down. Line heater was also down, choke on the line heater was frosted over. Line heater still had fuel supply, lit burner and got heat going. Ran over to the host site and checked tanks and checked separator . Everything was good, while i was going through the separator the 80 well was flowing. Ran back down to the satellite well and line heater had thawed out the choke. Sat with well while it flowed out. RTP'd well ",user_56,asset_314,48.1470144,-103.6180489
12/9/2016,Gas Scrubber,,,,,,"Found Scc pilots had no fuel gas, inspected system and found hydrate in line after scrubber pot, where it transitions from 3/8 brake hose to 1"" poly pipe, thawed and cleared freeze. ",user_115,asset_667,48.08479195,-103.6478609
2/23/2018,Instrumentation,End Device,Topworks,,,Weather,"D4 was in closed position preventing injection. Opened valve, begin to inject gas downhole",user_35,asset_1812,48.19893914,-103.4822391
2/5/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,"Opened well up to tanks, found line heater at sat. well only at 90 degrees. increased to 120, WM entered to remove temporary piping from well and install permanent sweep. Also heat trace and insulate.",user_63,asset_599,,
10/8/2019,Tanks/Pits,Shell,Body,,Steel,Corrosion," Crew on site task to clean out tank for replacement. The crew was getting all tools to remove the main hatch/ man way door on the tank so they can start cleaning it, I asked if they were going to shave to be able to wear they respirator, and they asked me if they have to wear respirators to clean the tank. We stopped the job and we have a conversation about respirators and the fumes from the tank. FYI, this crew is new on replacing tanks and I probably spaced out to talk to them about it in the past. Contractor called their safety man, he came out and performed fit test on all 3 members of the crew, issued them respirators and they went back to work in a couple hours.",user_21,asset_315,46.2356189,-100.6010498
8/5/2017,Tanks/Pits,Shell,Body,,Steel,Corrosion,Blowdown tank was found leaking due to hole in floor at plum bob impingement area caused by internal corrosion,user_150,asset_70,,
12/15/2016,Wellhead,,,,,,"Well not getting plunger arrivals, found plunger stuck between upper and lower master valves on tubing, caught plunger and vented well toClear obstruction, partial hydrate was cleared and plunger dropped ",user_115,asset_1572,48.04144482,-103.6622644
4/30/2018,Wellhead,Cyclonic Valve,Actuator,,,Corrosion,"Cyclonic actuator badly corroded inside, motor failed.",user_134,asset_1358,48.1470144,-103.6180489
2/20/2018,Separator,Liquid Dumps,Controller,Norriseal,,Improper Adjustment,Found water dump on green complete had been adjusted to low and would not shut off. This caused gas to blow by and the water rate via turbine meter to show and increase and gas rate to decrease. Correctly adjusted water dump and validated it would shut off if water level got lower than set point.,user_62,asset_1383,48.1470144,-103.6180489
12/6/2018,Pipeline/Piping,Pipe/Components,,,,hydrate,hi/lo and choke were frozen on wells 1 and 4,user_28,asset_466,48.1511744,-103.6275517
9/5/2018,Tanks/Pits,Liquid Level Control,,,,,High water tank ,user_94,asset_417,,
4/16/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,fluid,"Found and drained approximately 2 OZ of fluid in first scrubber on line heater. This is due to warm temperatures of fuel gas upstream (well flows at 120F) and the end devices (line heater scrubber) sitting at ambient temp (68 F). ENG to further trouble shoot and supply plan forward. There is a shut in sivals unit onsite that does not appear to be doing anything, we could utilize it as a fuel gas scrubber.",user_6,asset_1675,36.2541889,-91.2478009
6/14/2018,Separator,Choke Valve/Loop,,,,Corrosion,"Looking through graphs, I found the suspected PSV release. Upon arriving at the location, I found the PSV and the rupture disc had both released. The Inlet valve shut in on the low side rapidly, as designed. The release was minimal.",user_163,asset_1986,48.1470144,-103.6180489
1/24/2017,Chemical System,Tank,,Other,Other,Weather,Out of methanol. Suspect plunger is hydrated in lubricator. ,user_50,asset_807,47.97255383,-103.439848
11/17/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_2012,48.1470144,-103.6180489
12/29/2017,Automation,Cable,Data Cable,Automation-X,,Loose Connection,call out for hi condo psi-upon arriving looks like its been disconnected and these are false call outs-will write a work order for auto to check,user_131,asset_2004,40.7126799,-114.1193569
11/26/2018,Instrumentation,Transmitter,Tubing Pressure,Ashcroft,1151,Installation Design,"Tubing transmitter freezing due to un-heat traced/insulated instrumentation piping that faces down, not allowing liquids to drain and allowing it to freeze. Instrumentation piping input is also in between upper and lower flow paths, right were the plunger arrives causing JT effects during after flow and forcing hydrates into piping. OPS entered WM for MAINT to arrange instrumentation piping so that the transmitter is oriented above the inlet so that liquids may drain away and not freeze, to shorten the transmitter piping to only the no-shock valve and the railroad union/1"" nipple to eliminate un-needed piping and less piping to hydrate and heat trace and insulate all three tubing transmitters onsite. If this does not work we may have to relocate the instrumentation piping to away from where the plunger arrives, which may require a needle valve install on the flow line just downstream of the upper and lower flow paths. ",user_54,asset_1484,48.0831219,-104.8694232
1/23/2019,Tanks/Pits,Flare/Combuster,,,,,"1 scc out, probably due to high wind, relit",user_31,asset_2135,40.5262342,-113.8824849
12/2/2016,Automation,,,,Other,Other,Asco solenoid got destroyed due to wet fuel gas freezing,user_92,asset_1059,48.16028305,-103.6172149
6/8/2019,Instrumentation,Controller,,,,,Fisher DVC6000. Unknown failure.,user_12,asset_993,40.5262342,-113.8824849
1/16/2019,Surface Location,Lease Road,,,,Weather,CANNOT ACCESS SITE DUE TO SNOW.,user_34,asset_73,43.56424,-91.351691
4/15/2019,Gas Scrubber Separator,PSV,Spring,,,Corrosion,wore out,user_157,asset_1123,46.2356189,-100.6010498
11/17/2017,Gas Scrubber Separator,Dump Line,,,,Trash,Unit was full of sand and a clean out was down. Brought unit back on line and returned the equipment to service ,user_136,asset_1323,48.0614644,-104.8417043
11/4/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ajax,,Trash,"well went down on low bath levelA, checked location for leaks and could not find any, lowered low kill on bath 1/10th of an inch and RTP gas lift comp was down so RTP comp.cmp was down on low suction pressure looks like it went down when the bath took out the 70 &80",user_37,asset_1284,48.1497667,-103.6210377
12/14/2017,Compressor,Intrumentation,,,,,"Compressor went down on high suction pressure. Blew liquids out of suction controller. As soon as it got started again, went down again on high suction. I saw that the wells were kicking on harder and faster that the suction controller could respond. Contacted optimization to slow down the speed that the D-4 opens for the well to flow. Started and loaded compressor.",user_62,asset_1495,48.1470144,-103.6180489
8/11/2017,Instrumentation,Controller,,,,,Block and bleed failed in hi-Lo controller,user_126,asset_1948,,
7/30/2019,Separator,Choke Valve,Seat,,,,The choke was washed out. The internal parts were replaced on and is ready to be calibrated by Automation. A WM has been submitted to Automation for the task.,user_68,asset_661,48.1470144,-103.6180489
7/27/2019,Fuel Gas/Start Gas,Compressor,Process Gas Supply,Gemini,,Trash,"pad is esd with no interlock again. arrived onsite and found both air compressors down due to overheating. contacted team lead and got bob fox number. contacted bob and he helped me troubleshoot air compressors over the phone. found both fans turned off in compressor and generator rooms, started fans to help cool rooms. checked oil levels on both air compressors. both of the were ran completely out of oil. filled them both, cleared alarms and restarted both units. dryer is having issues, its not switching bottles properly. bob said its been over 6months since hes performed a PM on this equipment. my recommendation is that our leadership schedules a PM with bob fox ASAP. this equipment will continue to fail if not maintained.the instrument air is carrying fluids because dryer is not fully working. please leave door open to air compressor room to help keep cool.drained dezy and scrubbers on four packs.drained regulators to esd's and DVC's. drained filters inside cabinets to dump controllers.restarted the 60,80,100,120 and the 40 on plunger cycles. put the 130 and 10 in auto to flow out high pressure so we can eventually restart gas lift. if air compressors fail again, please leave pad down and contact PTL. tanks are low and restarted scc's. contacted fluid management to let them know pad has been rtp",user_120,asset_516,39.0112008,-92.3881993
2/28/2019,Wellhead,Manual Valve,Body,,,Freezing,Location had been shut in earlier in the winter due to surface freezes. Opened well head valves to start thawing location and getting well flowing.,user_15,asset_2019,48.2816346,-102.8553762
8/14/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,ARROW PLUS I was already on location working on 5-150 Vented this well for 67 mins with no success of getting plunger to surface Put back on cycles ENG might want to get slickline to pull plunger out ,user_56,asset_1442,,
12/11/2016,Sand Separator,Manual Drain Valves,,,,Freezing,"Choke had a freeze in regulator to DVC causing it not to work, and it didn't close loading well. Thawed regulator and DVC with thaw tube. Choke is working properly",user_141,asset_1493,48.3619066,-103.2129855
7/25/2017,Instrumentation,Transmitter,Temperature,Rosemount,4088,Temperature,Found temp locked. Cycled meter to return to normal operation. ,user_99,asset_1014,40.5960545,-113.9323891
6/22/2018,Separator Inlet Valve (XV),Pneumatic Control System,Diaphram,,,,"hi/lo bonnet is leaking gas, when actuated , wont open to flow unit, needs replaced, going to pick up bonnet at wear house",user_122,asset_1323,43.252261,-115.0567324
2/8/2019,Surface Location,Lease Road,,,,Livestock,No access to location due the drifted snow.,user_83,asset_470,,
12/20/2017,Wellhead,Tubing,,,,,Tubing transmitter frozen. It was thawed and RTP'd. ,user_41,asset_392,48.20718668,-103.5433359
12/6/2016,Chemical System,Electrical,Fuse,Other,,Weather,"No damage, the system was just frozen due to cold weather.",user_162,asset_1974,48.1602732,-103.6174178
1/12/2019,Separator,Liquid Dumps,Float,Norriseal,,Freezing,"vessels frozen, no fuel gas to start burners",user_31,asset_1055,43.56424,-91.351691
3/11/2018,Fuel Gas/Start Gas,Coalescer/Filter,Level Controller,,,,Lots of liquid in desi. Acts like it still has ice inside. ,user_156,asset_1892,48.21080561,-103.6486573
8/24/2017,Tanks/Pits,Flare/Combuster,,,,,SCC out due to rain,user_50,asset_1857,47.97889805,-103.4586935
4/5/2019,Wellhead,Manual Valve,Master Valve,,,Erosion,both tubing master valves are leaking crew greased them and still not getting a good seal. upper tubing master leak thru and out of pee hole,user_28,asset_836,48.1482751,-103.6450538
10/3/2017,Instrumentation,Transmitter,3N1 MVT,Viatram,4088,Calibration Issue,Complete calibration ,user_113,asset_5,48.15433304,-103.5408981
8/16/2018,Wellhead,Tubing,,,,,"well will not unload, shut in for psi build, then attempt to vent",user_144,asset_1088,48.1470144,-103.6180489
6/22/2018,Gas Scrubber Separator,ESD,,,,,Luman 15-pad RTP and staggered cycles after new lateral tie in. wells look good all made an arrival.,user_71,asset_701,43.252261,-115.0567324
8/3/2018,Pipeline/Piping,Valves,,,,Corrosion (Internal),"2” blowdown valve seized closed, task request in to replace",user_35,asset_571,48.05394119,-103.3725283
4/8/2019,Sales Valve (PV),Sales Valve,Pie Disks,Valvcon,,End Of Useful Life,Sales line cyclonic leaking past.,user_54,asset_1419,40.5262342,-113.8824849
1/20/2017,Tanks,Valving/Swedges,Seat/Ball/Piston,Other,Other,Corrosion,"2"" valve is broken and needs replaced not able to open valve -no leaks currently 761730W",user_23,asset_1108,48.05404101,-104.8581624
9/4/2019,Separator,Liquid Dumps,Body,Mallory,,Freezing,The Y Strainer on the condo dump line apparently froze and split. It was replaced with a new assembly.,user_68,asset_2216,48.1470144,-103.6180489
6/25/2019,Instrumentation,Meter (BP Check),,,,,WyoElectric Repaired Conduit and secured wiring,user_139,asset_1549,,
1/10/2017,Gas Scrubber,Shell,,,,,1/10/17 Operator found Cyclonic sales line frozen. Valve was thawed and well was RTP'd. ,user_41,asset_1291,48.2216041,-103.6301605
5/5/2019,Pipeline/Piping,Valves,,,,Corrosion (Internal),replace valve,user_28,asset_738,48.1511744,-103.6275517
4/27/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Did walk through of location, found location has buy back meter from WFS. Walking through the system, i found that the valves from WFS meter were open but the gas from top of vessels to Desi was open as well. This causes the fuel gas system to continue to pull its fuel gas from the wells and not buy back meter. I shut off the gas from the vessels to Desi and checked WFS buy back meter and it was showing a flow rate now. Root cause is human error. It appears that some one does not fully understand the configuration of fuel gas across location.",user_62,asset_1103,48.1470144,-103.6180489
12/25/2016,,,,,,,"SCC ""A"" burner went out.",user_138,asset_1187,48.18390963,-103.4265234
5/30/2018,SWD System,SWD Pump,,,,Erosion,I got pump reprimed and everything working.,user_141,asset_1571,48.1001879,-103.5870438
1/22/2018,Fuel Gas/Start Gas,Regulator,,,,,Fuel gas to ESD froze,user_126,asset_1662,,
2/9/2018,Gas Scrubber Separator,Mechanical Dump Valve,Controller,Kimray,,Out Of Adjustment,Issue: I found the dehy was flooded out. Root Cause: First I checked our hi pressure unit and found the unit was flooded and carrying over. I adjusted the dump and got set. But there inst suppose to be any fluid in the hi pressure unit so i went to the Green Complete and found it was flooded out as well. Fix: found the dumps were not opening soon enough and far enough. i adjusted the dumps to acute sooner and open further as to not get over ran so easy ,user_136,asset_1105,48.1603196,-103.6176623
5/23/2018,Automation,RTU,Fuse,Schneider/Scadapack,Scadapack P4A,Electrical Short,Cause due to lightning,user_162,asset_710,48.1470144,-103.6180489
3/22/2017,Automation,Battery,Battery,Other,Other,Other,RTU has no power. ,user_41,asset_2080,48.20708908,-103.6211694
12/10/2017,Fuel Gas/Start Gas,Coalescer/Filter,Regulator,,,,dezi was full of liquids ,user_53,asset_505,48.2631932,-102.8852154
3/24/2017,Recirc Pump,Pump,Other,Other,Other,Other,,user_149,asset_2052,48.3619066,-103.2129855
6/1/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_101,48.1470144,-103.6180489
3/12/2018,Dehy,WFS Issue,,,,,"No freezes, valve shut at dehy by williams for froze dumps, dumps are clear just need Williams to remove tag and open valve. ",user_141,asset_593,48.1470144,-103.6180489
4/7/2018,Wellhead,Tubing,,,,hydrate,"broke freeze by equalizing well. started methanol injection, flowing well",user_122,asset_2005,48.0614644,-104.8417043
3/19/2018,Instrumentation,Meter,Orifice Plate,Control Micro,4203DR,Calibration Issue,Dp zero was high. Reset zero ,user_166,asset_783,47.98410388,-103.6513114
3/11/2019,Dehy,WFS Issue,,,,,Check valve on williams water dump line is broken at dehy.,user_108,asset_1163,,
9/8/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,Cleaned out the I/P on the dvc and got choke to close return well to cycles plunger making arrivals,user_100,asset_478,48.3619066,-103.2129855
5/20/2017,Wellhead,Wellhead Piping,,,,,"Freeze/hydrate in flow line on the 140 well. The 140 has a sales line valve, so it is used to keep fuel supply to pad. Broke freeze/hydrate by opening blowdown valve to tank. Took approx 2 minutes for it to break. Put well back to production and notified optimizer. ",user_141,asset_174,48.1470144,-103.6180489
1/3/2019,Separator,Fuel Supply System,Regulator,,,freeze,"regulators were rerun from valves (esd and choke) to header system, this header is outside the cabinet in the elements. the same configuration was done on other pads and was inside the cabinets, this helps keep the regulators and drain pot from freezing",user_64,asset_1422,43.56424,-91.351691
3/23/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,tried venting plunger to surface to change out. Vented for an hour and would not come in. shut in and will try again ,user_88,asset_1348,48.1470144,-103.6180489
2/14/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,Lateral is froze. lateral slopes up hill before it ties into WFS. dumped 2 gallons of methanol down lateral. Dumped 2 gallons of methanol down our sales line. freeze finally broke after 4 hours of working on it with wyatt hopkins found that the meter isn't showing flow onsite will ask measurment to come out. also would like to start methanol injection on that lateral. will need automation to come out and replace fuses and troubleshoot sun pump RTP'd well ,user_53,asset_168,40.5481548,-114.0112915
9/5/2017,Compressor - Gas Lift,Compressor,Valves,Ajax,,Trash,replaced bad discharge valve,user_87,asset_2029,40.5262342,-113.8824849
11/28/2018,Separator,Choke Valve/Loop,,,,Freezing,"choke froze, probably from burner being out",user_31,asset_1029,43.252261,-115.0567324
12/13/2018,Instrumentation,Switch,,,,,Tank level switch failed due to corrosion. Blowdown tank. Replaced with NRG.,user_108,asset_1422,,
9/27/2019,Wellhead,Manual Valve,Master Valve,,,Fouling,"Greased valves and worked them, pressure tested good!",user_21,asset_1850,46.2356189,-100.6010498
12/21/2018,Separator,Fuel Supply System, Big Joe Regulator,Fisher controls,,fluid,"found hi lo shut well not flowing, found cabinet doors open, cold air hitting big Joe and scrubber pot, found low pressure on fuel gas not able to keep high low open, drained scrubber and pressure came up, root case was cold air hitting scrubber and making warm gas condince flooding scrubber, shut doors and rtp'd well",user_144,asset_1212,48.1470144,-103.6180489
11/17/2017,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,"Issue: pad keep shutting in on a hi water # 2 tank alarm. Root Cause: the tank level has been taken out of service to keep the pad from triggering an alarm off that tank but it still going into alarm and shutting the pad in with a level of 9' 10"" Fix: I am starting to think it may be more of a programming issue rather than a device issue",user_136,asset_97,48.1470144,-103.6180489
7/31/2018,Instrumentation,Controller,,,,,"PV Well was down, attempted to flow well remotely. That was unsuccessful DVC was not opening choke Got to location and verified that the fuel supply for the DVC was dry. Tapped on the DVC then sent it a command to open 15% and it opened RTP'd well ",user_56,asset_1564,48.1573536,-103.621648
10/21/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Gardner Denver,,Freezing,"Down on high discharge psi, out of meth",user_77,asset_943,48.096024,-103.5400299
12/21/2017,Fuel Gas/Start Gas,Coalescer/Filter,Regulator,,,,stopped by and checked equipment. everything working. drained scrubbers.,user_71,asset_1213,48.1470144,-103.6180489
11/27/2017,Instrumentation,Switch,,,,,Condensate level switch failed due to water build up inside the level switch tubing and froze.,user_65,asset_1806,48.1470144,-103.6180489
1/30/2018,Separator,Liquid Level Control,,,,,Omart-Vega VegaFlex 65 level transmitter on the glycol bath Unknown cause. ,user_134,asset_10,48.1470144,-103.6180489
9/3/2019,Gas Scrubber Separator,Choke Valve/Loop,,,,Corrosion,"Winterization, had to replace plunger. Swapped out for a new dual pad. 03SEP19 Rebuilt the hi/lo stem and seat. Glycol was good Methanol was good. Needs new methanol pump.",user_56,asset_209,40.5262342,-113.8824849
11/7/2017,Compressor,Compressor (Intergral),Process Gas Supply,,,,Went down on low interstate 1 pressure ,user_50,asset_1492,48.32430894,-103.6003723
4/2/2018,Plunger System,Plunger,MSO,PCS,,Not Optimized,Well showed on arrow dispatch as plunger possibly froze in lubricator. Put well to sale found no apparent freeze issues. Watched flow rate and casing psi gradually drop. Opened well up to vent immediately liquids and plunger. I’ll get with optimizer to evaluate point forward possibly plunger not dropping completely down hole. ,user_58,asset_1286,48.33583305,-103.5982509
9/25/2018,Compressor - Gas Lift,Compressor,Regulator,Sullair,,Freezing,blew compressor down and heard freeze break. Code was cleared when I got there. The panel was in sleep mode. ,user_106,asset_2101,48.2575609,-102.9119612
1/18/2019,Separator,rupture disk,,,,system over pressure,"Hi-lo failed causing rupture disc to blow, work management in for hi-lo and rupture disc to be replaced. ",user_44,asset_416,,
3/22/2019,Separator,Manual Drain Valves,Body,,,Corrosion,"Under the A1H LP separator it appears that the bottom drain valve or nipple has corroded and come apart , it has a pretty good mess around the separator so that will need to be cleaned up as well prior to working on the valve. unit is isolated in and out of the vessel .",user_174,asset_1752,39.2506642,-92.4357879
2/24/2018,Tanks/Pits,Flare/Combuster,,,,,SCC showed that it was out. It was lit when I showed up to location. Checked regulators. No alarm.,user_153,asset_333,48.21129965,-103.6161667
5/23/2018,Pipeline/Piping,Valves,,,,human error,"$ pack units are designed with a 3 way valve that is disconnected and now makes a restriction on the cool flow of the well, freezing up and restricting the flow. Engineering needs to run economics on removing 3 way valves or keep methanol running.",user_60,asset_1102,40.7126799,-114.1193569
3/5/2018,Fuel Gas/Start Gas,Regulator,,,,,Loss of fuel gas due to bad glycol pump. ,user_153,asset_133,48.21090221,-103.6487548
11/13/2018,Separator,Liquid Level Control,,,,,"dumps are out of wack, vessel is froze probably from burner being out",user_31,asset_2107,43.252261,-115.0567324
12/14/2018,Heater Treater,Burner,Fire Tube,,,Pilot Went Out,Pilot went out due ti high winds,user_132,asset_683,,
7/24/2017,Wellhead,Choke Valve,Body,,,,"D4 casing valve on the gas lift malfunctioned, closed and will not open. Automation has been notified. ",user_41,asset_794,48.22060569,-103.5959341
5/9/2019,Wellhead,Valves,,,,End Of Design Life,"The 2"" ball valve on the flowline was leaking out the stem. The valve was removed and it was replaced.",user_68,asset_1467,48.1470144,-103.6180489
11/16/2017,Automation,RTU,Wiring,Vinson,Scadapack P4,Electrical Short,Pad went down on high false tank ,user_122,asset_2247,48.36316317,-103.7896572
3/8/2018,Tanks/Pits,Tank Level,Probe,,,Calibration Issue,Issue: called out hi water tank alarm Root Cause: false alarm Fix: wrote a work order for automation to look at it,user_136,asset_334,48.2594026,-102.9010889
1/26/2019,Separator,Liquid Dumps,Controller,Nalco,,Improper Adjustment, + LOW PRESSURE WATER DUMP CONTROLLER SET SCREW LOOSE AND OUT OF ADJUSTMENT. **ADJUSTED BUT NEEDS TO BE WATCHED,user_34,asset_787,43.56424,-91.351691
5/21/2018,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,Issue: called out hi water tank alarm Root Cause: transmitter tripped out and showed a hi level but cleared itself Fix: alarm was cleared before i could get it pulled up. left as is ,user_136,asset_601,48.2594639,-102.9009098
7/10/2017,Wellhead,Cyclonic Valve,Actuator,,,Corrosion,The cyclonic valve is sticking some what and is contributing to the actuator motor burning up.,user_162,asset_514,48.1470144,-103.6180489
12/11/2016,Gas Scrubber,,,,,,Frozen reg. For the choke DVC thawed and working,user_100,asset_1245,48.0997907,-103.6537882
7/26/2018,Compressor - Gas Lift,Engine,Battery,Cummins,,Electrical Short,"compressor down on high discharge psi. cleared alarm and attempted to restart compressor, noticed battery started smoking every time you engaged starter. engine will not turn over. contacted JW (bob). he made it out later that night said we possibly have bigger issues with engine. gas lift is currently down waiting on JW",user_120,asset_1284,48.1470144,-103.6180489
3/23/2018,Wellhead,Tubing,,,,,"Engineer requested fluid shot on well. shot down casing only, well was open to vent when request came in. Casing PSI 1270- 4005 foot of fluid above perfs.",user_62,asset_1686,48.1470144,-103.6180489
7/18/2018,Separator Inlet Valve (XV),Pneumatic Control System,Hi/Lo Pressure Controller,,,,"well is losing unit pressure in an off cycle.well shut in on an off cycle at 5:00am with around 310psi. starting losing unit pressure at 5;55 am. by 7:06 unit pressure was down to 22psi.which is obviously to low for the high low to stay open. checked all surface equipment for leaks and couldn't find any issues.while in an off cycle this unit supplies four abutec sccs and the pilot line for the flare.i believe this is our main issue as to why we are running out of unit psi, this issue will only worsen when the colder weather comes. this issue has occurred several times. currently working with optimizer to put in a burp setting to allow kimray to open and let pressure into the unit when unit psi gets to a certain low point (150). i believe this will help.but i think the main fix would be removing this valve on the flow line and tie it in down stream on sales line.a buy back line would be an issue also due to there being no dehy onsite and receiving wet fuel gas.this kimray on the inlet also increases our chances of a hydrate (taking multiple pressure cuts and smaller orifices) need to work with engineer on this a bit more",user_120,asset_2069,43.252261,-115.0567324
2/25/2018,Heater Treater,Burner,BMS,,,Corrosion,Issue: called out LP bath temp hi alarm Root Cause: only running off of one T-12 and the temp swings have the burner running hard so it shuts down before the temp set point but the burner tube is still so hot that it continues to raise the temp tell is cools down Fix: lowered the bath temp just a little and raised the computer set point up just 10deg to allow the heat trace to continue to function properly ,user_136,asset_1780,48.2594584,-102.9010654
1/19/2017,Instrumentation,Transmitter,Flow,Other,Other,Water,Freezing in fuel gas to ESD thawed and rtpd,user_175,asset_1464,47.95107352,-103.5791972
9/15/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Pilot tip was clogged I shut off gas to burner and was able to clean tip and relit glycol bath working good now ,user_52,asset_1297,48.11510163,-103.8425213
2/2/2019,Separator,Temp Control System,Thermostat,,,,High unit temp I went to location Bath was at 184 degrees I turned down temp and let bath temp idle down to 120 degrees.,user_159,asset_2007,48.1508,-103.6191904
12/4/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,freeze in big joe on the 4 pack thawed and got bath going again. Burner was out and froze the pilot line the the burner thawed and restarted burner.,user_100,asset_28,40.5262342,-113.8824849
1/10/2019,Compressor,Compressor (Recip),Lubricator,,,,comp is out of engine oil needs tank filled,user_37,asset_1624,43.56424,-91.351691
2/10/2018,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Freezing,Outside load line valve came apart pushing the ball out of the valve due to freezing,user_150,asset_241,,
2/2/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,"Cyclonic blow down leaking by internally causing flow line to freeze and esd to freeze shut. Thawed on cyclonic blow down valve, flow line and esd valve. Managed to break freeze, contacted optimizer to open esd and well would flow. Work management entered to have cyclonic blow down replaced. ",user_44,asset_1777,,
3/11/2017,Gas Scrubber,Pnumatic Dump Valve,Seat/Ball/Piston,Other,Other,Erosion,Won't Seal and hold back pressure ,user_138,asset_480,48.07973083,-103.438008
10/24/2019,Tanks/Pits,Valving/Swedges,Body,,,Freezing,Increased flow on injection #4. Started draining tanks some more on South Evap to get ready to drain #3 5K tank. 10/23/2019 Drained 5K tank and replaced 4 Valves on tank. Leak tested and no leaks found,user_31,asset_308,43.56424,-91.351691
2/23/2018,Fuel Gas/Start Gas,Regulator,,,,,Fuel gas to scc pilots completely froze. Took about an 1 1/2 to thaw out relit all five scc,user_172,asset_1513,,
11/20/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Drain and fuel gas scrubber of liqiuds ,user_109,asset_1364,48.3271733,-103.6565033
6/13/2019,Tanks/Pits,Valves,,,,End Of Design Life,Leaking load line replaced and returned to service,user_21,asset_2171,46.2356189,-100.6010498
3/16/2019,SWD System,SWD Pump,,,,Corrosion,"Walk through, take readings. Location needs a lot of snow removal. Cannot access lower portion. Pump building doors are snowed in. ",user_55,asset_2012,,
2/15/2017,Gas Scrubber,Pnumatic Dump Valve,Other,Other,Other,Trash,Turbine was plugged with rubber had to clean it out twice finally cleaned out and RTPd ,user_152,asset_1087,,
12/1/2017,Instrumentation,Meter,Turbine,Bristol,Wonder Card RS232,Freeze,"Meter is Flatlining when WFS Meter is functioning fine, right next to it. Well is Flowing but our Meter not measuring. Optimizer has turned over to Measurement Dept. for repairs.",user_138,asset_1644,48.16525596,-103.448656
4/7/2019,Gas Scrubber Separator,Choke Valve/Loop,,,,Corrosion,Choke stem had excessive wear on one side,user_157,asset_1936,48.1470144,-103.6180489
3/8/2018,Automation,RTU,Board,Vinson,GFC,Loose Connection,"OPS found choke hanging open at 1.5% MV. After cycling through manual and automatic choke settings the MV zeroed out. Engaged AUTO to trouble shoot and AUTO suggests it may be a deadband variation issue, cause of dead band variability unknown.",user_6,asset_1677,36.2541889,-91.2478009
2/28/2019,Fuel Gas/Start Gas,Coalescer/Filter,Level Controller,,,,"desi had lots of liquid, drained",user_31,asset_521,43.56424,-91.351691
12/8/2016,Wellhead,Primary Choke,Stem/Seat,Other,Other,,Freezing in Upper and Lower flow paths of re-configure on Tree to accommodate Plunger.. broke partially free and started Methanol pump/ sped up Glycol pumps,user_138,asset_2107,48.07718324,-103.4421299
9/18/2019,Tanks/Pits,Berm,Dirt,,,Wildlife/Livestock,fill in badger holes around tank berm,user_97,asset_913,46.2356189,-100.6010498
10/10/2019,Chemical System,Pump,Seals,Goulds,HBT2,Wear,The methanol pump was stalled and would not pump. It was replaced with a rebuilt pump.,user_68,asset_799,43.56424,-91.351691
12/11/2017,Automation,Radio,Wiring,Cellular,,Improper Install,Negative wire for power supply to radio slipped out of its terminal block. Re-inserted wire and tightened terminal block and verified communications.,user_65,asset_1817,48.1470144,-103.6180489
11/30/2016,Wellhead,,,,,,"Plunger loaded off, well supplies the fuel gas for the pad, when well bumps open it was using a little to much fuel gas, adjusted pump fuel gas pressures ",user_115,asset_1554,48.059201,-103.6376532
4/22/2018,Flare System,Flare Header,BMS,,,,Issue: called out SCC alarm Root Cause: looks like it was from yesterday when we had a 45minute ground pounder rain storm followed buy hi winds with snow and looks to have flooded out the pilot Fix: relight and returned to service ,user_136,asset_1237,48.2594956,-102.9009337
8/2/2017,Automation,Plunger Arrival Switch,,EDI,,, 3. High Point 27-125 - MSO not working • Found wiring issue from when site was built • Repaired wiring issue • Tested and verified Cyclops working correctly now ,user_92,asset_1160,40.5960545,-113.9323891
11/29/2017,Flare System,Flare Header,BMS,,,,Issue: SCC (A) down on valve fault Root Cause: found that someone shut the supply gas off to the pilot ESD casing the BMS to shut down Fix: opened valve and did the light sequence. returned to service,user_136,asset_76,48.1602546,-103.6172966
1/22/2018,Separator,Choke Valve/Loop,,,,Freezing,Found a freeze in DVC. Thawed DVC and choke. RTP'd well and returned to optimizer.,user_141,asset_2225,48.1470144,-103.6180489
2/9/2019,Separator,Temp Control System,Flame Arrestor,,,,"While on location to work on well 150, saw Snow had started to drift about half way up flame arrestor. Shoveled out snow drift before it caused the burner to go out. ",user_15,asset_882,40.5262342,-113.8824849
3/3/2018,Separator,Dump Line,,,,Corrosion,The #30 well went down on low mvt pressure. Went to site and found the water dump had a hole in the valve body. Shut well in immediately. Contacted team lead. Bleed down unit. Isolated sales line dump lines and inlet. Put tags on. Left down until we can get it repaired ,user_172,asset_1605,,
10/5/2017,Separator,ESD Valve,Actuator,,,Freezing,Troubleshoot downstream cyclonic went out of sync . The valve looks like its leaking passed the valve on the off cycle and freezing which is causing the cyclonic to get out of sync. Put work order into replace,user_100,asset_2157,40.5960545,-113.9323891
1/1/2017,Gas Scrubber,,,,,Other,Froze in 3way valve glycol bath at 68* turned up T12 and thawed valve out RTPd well,user_152,asset_919,,
5/19/2017,Tanks/Pits,Shell,Body,,Steel,Corrosion,"Tank floor failed at plum bob impingement area on coated tank with no anodes or striker plate due to internal corrosion. Tank coils were also near failure with dep pitting and corrosion and .04"" remaining wall thickness.",user_150,asset_1624,,
4/18/2018,Gas Scrubber Separator,Dump Line,,,,Erosion,"CL 29-150 tank #78007 at 12-4x3-0 tank #78008 at 12-8x1-5 left flowing to. Checked site dumps looked like they were working correctly, drained scrubbers. ",user_71,asset_1213,48.1470144,-103.6180489
1/14/2017,Gas Scrubber,,,,,,"Thaw out line heater, pumps and supply lines are open to the elements and freeze off",user_87,asset_107,47.95890075,-103.4368054
3/5/2018,Heat Medium,Pump,Plunger,Goulds,113,Wear,Graco 1040 and Western pump need to be replace,user_60,asset_129,40.5960545,-113.9323891
1/6/2018,Chemical System,Pump,PSV,Texam,HBC1,Debris,Replace methanol pump PRV. RTP'd methanol pump,user_141,asset_1850,48.1470144,-103.6180489
11/9/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash,kelvin burp setting failed ,user_53,asset_181,40.5481548,-114.0112915
4/10/2017,Wellhead,Other,,Other,Other,Other,"Well down, not flowing",user_141,asset_173,48.224585,-103.8291059
6/12/2019,Separator,Liquid Dumps,Seat/Ball/Piston,Nalco,,Corrosion,"Condo dump control valve leaking to tank. Was a gentleman here using FlareCam couple days ago, So went thru checked throughly and discovered the condo dump leaking",user_19,asset_486,48.1603117,-103.6188766
12/1/2017,Fuel Gas/Start Gas,Regulator,,,,,full of liquids,user_53,asset_1914,40.5262342,-113.8824849
3/2/2018,Separator Inlet Valve (XV),Pneumatic Control System,Regulator,,,,Well shut in on low MVT pressure I couldn't get the d-4 valve to open I went to location and cleared fuel gas to D-4 valve and brought back online.,user_51,asset_159,40.5960545,-113.9323891
6/25/2018,Automation,RTU,Board,ABB,Bristol 3310,Loose Connection,"Champ 320 in comm error flow and tank levels haven’t moved in Emerson , checked site everything working. Flowrate at 4.7 mil Tank #770087 at 14-6x2in #88 at 14-6x2in switched to #88 & #89. ",user_71,asset_1675,43.252261,-115.0567324
3/9/2018,Wellhead,Tubing,,,,,Well was froze in flowline. This well is a satellite to the monument 19-2.1050 on tubing and 1071 casing. Got flowline freeze to break by isolating wellhead and back blowing psi to AGT.brad funk did a fluid shoot on this well before I broke freeze in flowline and informed me that there was no fluid level in tubing and very little on casing. Rtp well. Informed optimizer well was rtp,user_172,asset_164,,
11/5/2019,Separator,rupture disk,,,,system over pressure,The rupture disc was replaced after being over pressurized.,user_68,asset_714,48.1470144,-103.6180489
6/11/2018,Separator,Back Pressure Valve,Seat/Ball/Piston,Kimray,,Corrosion,Replaced sales line cyclonic,user_173,asset_465,48.1470144,-103.6180489
2/22/2019,Automation,RTU,Relay,ABB,DACC 2000,Loose Connection,"called out on high condo tank. was showing 19-6 tank level on Emerson, checked tanks false alarm, checked site found water dump in LP leaking by shut and tagged valve notified TL and will submit WM.",user_37,asset_1383,43.56424,-91.351691
4/23/2018,Flare System,Flare Header,BMS,,,,Issue: found the flare was out on the HMI Root Cause: looks like the wind blew it out Fix: dropped boom relight and returned to service ,user_136,asset_1383,48.1470144,-103.6180489
6/11/2018,Wellhead,Tubing,,,,hydrate,"Dispatched to well, found well hydrated in the TBG. Rocked CSG back and fourth. Finally got hydrate to break. Root cause, out of methanol. submitted a chemical request.",user_53,asset_1532,48.264309,-102.8805585
5/18/2018,Heater Treater,Mechanical Dump Valve,Mechanical Linkage,Kimray,,Out Of Adjustment,"While working on other issues on heater treater, found no level in the oil site glass. Found mechanical oil dump improperly adjusted, the dump was partially open with no liquid level. Adjusted mechanical linkage and got fluid level in sight glass and got dump functioning properly. Root cause is human error. Dump was not set up for proper operation during construction or after field maintenance. ",user_62,asset_796,48.0614644,-104.8417043
8/19/2019,Safety Systems,PSV,Spring,,,Weather,"Valve is not locked/sealed under PSV. Have no seals with me, will replace it tomorrow. No weep holes, noted in Winterization checklist. PSV was set below, but noticed rain cap gone. Checked and PSV was leaking through. Notified TL and he advised that we are now able to replace them. Big Joe would not adjust pressure down on scrubber. Replaced Big Joe and PSV and verified all is working as designed. No leaks. Will return PSV to warehouse. ",user_55,asset_142,,
9/28/2017,Wellhead,Tubing,,,,,,user_35,asset_1181,48.29656132,-103.4076504
10/9/2017,Instrumentation,End Device,Durag,,,Passed Function Test, 11. Eight Mile 25-100 - Bath A Durag issues (enbase) • Found Pilot lit and Durag not picking up pilot flame • Found durag not aimed at pilot tip • Aimed Durag so its pointed to the Pilot tip • Durag now functioning correctly • Lit bath heater in auto Notified operations,user_92,asset_896,40.5960545,-113.9323891
4/5/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,fluid,Cleaned scc pilot and adjusted placement of temp probe,user_100,asset_2146,48.1470144,-103.6180489
5/29/2018,Instrumentation,Controller,,,,,Comm 2 on scadapack failed.,user_89,asset_1934,,
4/12/2018,Tanks/Pits,Flare/Combuster,,,,,SCC was out due to high winds. Relit and returned to service.,user_50,asset_1914,48.1470144,-103.6180489
1/24/2018,Heat Medium,Pump,Diaphragm Gears,Texam,HBC1,Wear,"Replaced 2 Husky 1040 glycol pumps, then un-tagged, closed glycol return valve discovered at RTP - very likely pumps did not need replaced and surface failure is human error. ",user_161,asset_1209,40.7126799,-114.1193569
11/7/2019,Separator Inlet Valve (XV),Sales Valve,Body,Valvcon,,Freezing,Found a freeze on flow line and inlet choke and hi-lo. Line was isolated from the wellhead and blown to to tank. Applying heat with the truck cleared the freezes in the inlet of the unit. All freezes cleared and well turned back on. Plunger did not arrived and it was vented for 45 mins. Plunger was in good condition. Left well on cycles.,user_83,asset_2278,43.56424,-91.351691
12/26/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,Well shut in on low unit pressure Julio went there and thawed out DVC and jumped well back on. I opened well back up and put back on plunger cycles.,user_51,asset_1445,48.1470144,-103.6180489
7/6/2018,Compressor - Gas Lift,Compressor,Panel,Ge Gemini,,Trash,Call out that the gas lift compressor went down/ Down on eics drained srcubber and restarted compressor,user_100,asset_1873,43.252261,-115.0567324
2/1/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,"freeze in ESD and between esd and choke, pumps going, depressurized line ad broke freeze RTP",user_88,asset_2101,48.2629608,-102.8997457
1/14/2019,Separator,Dump Line,,,,Freezing,"Check to make sure all dumps open and drained scrubber. Dump lines frozen, thawed on them and got both condo and water open to tanks. Drained scrubbers and fuel pots. RTP'd well",user_55,asset_1164,,
2/5/2019,Separator,Temp Control System,Flame Arrestor,,,,flame arrestor covered in snow hand shovel snow to allow air flow around flame arrestor,user_57,asset_1225,46.2356189,-100.6010498
1/25/2018,Compressor,Compressor,Dump Valve,Ariel,,Vibration,"Scrubber dump controller oring, gasket leaking. Vendor was contacted (Compressor scrubber). ",user_130,asset_1346,48.1470144,-103.6180489
1/21/2017,Wellhead,ESD Valve,Gate/Seat,Other,Other,Freezing,"Had a freeze between ESD and choke. Thawed line with thaw tube, broke freeze. RTP'd well",user_141,asset_1974,48.3619066,-103.2129855
11/3/2018,Tanks/Pits,Flare/Combuster,,,,,Abutec down on flame fail. Drained fuel gas cleared alarm and relit ,user_120,asset_298,48.32006136,-103.5849805
6/15/2018,Separator Inlet Valve (XV),Electric Control System,Actuator,,,,"Failed to shut in on high tank alarm. High tank was false, task request to troubleshoot both issues",user_35,asset_327,48.22101561,-103.4640518
1/17/2019,Fuel Gas/Start Gas,Regulator,,,,,"Esd was closed flow path from gound to ESD was frozen, depressurized line and needed to thaw on it and the filter pot to the ESD. Line froze just because 800lb sitting on it while down. Got ESD open returned well to production and it made its first arrival with no issues. Unsure of why this well ESD'd 4 days ago, could not find any leaks or a root cause other than a fluid plug in the fuelgas system at the red filter pot. ",user_106,asset_1137,48.0881279,-104.0266781
2/10/2018,Tanks/Pits,Tank Level,Sensing Cable,,,Weather,Issue: called out hi tank alarm Root Cause: every time it gets cold tank (D) shows a hi tank alarm Fix: wait for the alarm to clear,user_136,asset_337,48.1470144,-103.6180489
6/2/2018,Separator,Choke Valve/Loop,,,,Trash,Found fuel gas shut off to choke. Well has been long term shut in so ops shut off gas supply to prevent accidental remote start up. Opened gas supply and function tested choke. RTP well.,user_62,asset_1927,48.1470144,-103.6180489
2/7/2019,Separator,Choke Valve/Loop,,,,Freezing, +TRIED TO VENT PLUNGER- BLOW DOWN VALVE IS FROZEN **THAWED VALVE AND SURFACED PLUNGER,user_34,asset_1437,48.1470144,-103.6180489
3/5/2019,Separator,Dump Line,,,,Freezing,"arrived on location with steamer crew. found both HP vessels froze solid.was unable to move dis placers in vessels. attempted to get pressure in HP separators. coudnt get pressure into either vessels do to freeze in flowline. was unable to shut chokes on both line heaters do to freezes in choke/coils. attempted to thaw out fuel gas to fuel gas separator so we could at least get glycol pumps circulating heat. line is frozen solid. contacted team lead, and asked to get two heaters onsite and for them t be placed on each HP&LP. will return tomorrow with steamer crew. ",user_120,asset_580,39.2506642,-92.4357879
9/19/2019,Heat Medium,Pump,Seals,Texam,HBC1,Wear,Changed out to 2 New Sandpipers,user_5,asset_1700,41.474544,-90.6778637
10/25/2017,Wellhead,Tubing,,,,,well has a coil tubinfg freeze,user_179,asset_1211,40.5262342,-113.8824849
4/24/2018,Separator,Liquid Dumps,Seat/Ball/Piston,Fisher,,Erosion,Water dump leak due to wear and use,user_35,asset_923,48.22376806,-103.4824417
4/6/2018,Separator,Choke Valve/Loop,,,,Freezing,Broke freeze in the flowline and thawed out supply gas to the front end choke. Thawed out solenoid for the burner management system and got burner running again. Vented well and rtp'd,user_100,asset_77,48.1470144,-103.6180489
7/23/2018,Flare System,Flare Header,Regulator,,,,Found an SCC out. Was able to relight remotely,user_55,asset_615,40.5262342,-113.8824849
12/5/2016,Automation,,,,,,,user_162,asset_347,45.3811923,-72.6756707
10/9/2019,Tanks/Pits,Shell,Body,,Steel,Corrosion," 6 Risk Assessment Pressure hazards correctly identified and controlled? Yes Site was shut in for leaking blow down. After digging several feet of the trench and can not find where the leak is, we decided to remove the LOTO and pressure up the lines to see if was any signs of leakage on the lines. Pressure tested the blow line and both sets of underground lines (condo and water) and nothing, as we walking to the tank we noticed the bottom of the blow line was dripping some fluid, so we tested again and found a small pin hole. Not convinced the blow down did all the mess by the tanks, we stopped the job and maintenance specialist decided to test the condensate tank which does not look to been here since day one of the site (Addition Fee/Fed remediation) and possible been a water tank in the previous site where it came from ( suspicious corrosion tank failure) we added 6' of water and showed positive leakage under the tank, not good news but good proactive finding.",user_21,asset_1400,46.2356189,-100.6010498
10/9/2017,Instrumentation,Liquid Turbine,,,,,Tested both Water and condensate turbines. Check condensate turbine all looked good. Water turbine is functioning correctly signal is getting to PLC terminal but not see high speed counter active.,user_113,asset_1754,48.40642758,-103.580603
1/18/2017,Gas Scrubber,Dump Line,,,,,"Water dump line froze outside of unit, thawed and rtped ",user_148,asset_1349,48.29522173,-103.6582812
3/9/2018,Heater Treater,Burner,BMS,,,Pilot Went Out,"Issue: found bath 42deg on the HMI Root Cause: found multiple issues. first the pilot was plugged so i had to pull the burner clean the pilot tip. then I found the valve going to teh pilot was half plugged off not allowing enough pressure to the pilot to run correctly. Then after it was running the bath shut down on an over temp. That's Human Error, instead of fixing the issue the alarm kept getting cleared and relight the bath remotelyl Fix: I pulled the burner apart cleaned out the pilot tip then i had to pull the valve off and dig the Teflon out of it to get the pilot to run correctly. on the over temping issue I turned T-12 down",user_136,asset_118,48.1470144,-103.6180489
8/14/2019,Separator,Valves,,,,End Of Design Life,The three way on the glycol bath is leaking gas out of the stem area. The valve was removed and flowline pipe rerouted.,user_68,asset_429,41.4367965,-90.6727424
12/8/2018,Separator,Dump Line,,,,Freezing,Found water dumps on all the unit frozen had to thawed out the water dump lines at the tank and just outside of both 4 pack units. Also thawed out front end choke on the unit rtp'd,user_10,asset_1974,43.252261,-115.0567324
7/9/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_1633,48.1470144,-103.6180489
9/29/2017,Automation,Radio,Wiring,Bluewave,,Improper Install,Radio power was wired into a relay for some reason and the relay was activated and shut off power to the radio. Rewired radio to +12V fuse block.,user_65,asset_997,48.1470144,-103.6180489
10/18/2019,Tanks/Pits,Piping,Connections,,,Connections,Replaced coils and returned to service,user_21,asset_1559,46.2356189,-100.6010498
7/18/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Trash,"Replaced 4"" Load Line Valve ",user_119,asset_1291,40.5481548,-114.0112915
11/7/2017,Separator Inlet Valve (XV),Pneumatic Control System,Spring,,,,Choke leaking by. Task request in. ,user_35,asset_809,48.18294039,-103.5376456
12/20/2016,Gas Scrubber,,,,Other,Other,,user_24,asset_592,47.96710618,-103.6796864
1/30/2017,Automation,Battery,Battery,UPC,Other,Rodents,"Batteries were replaced due to age of the battery, the battery could no longer hold a charge.",user_65,asset_887,48.3619066,-103.2129855
2/5/2018,Flare System,Flare Header,Instrumentation,,,,Adjusted igniter,user_65,asset_1780,48.38469628,-103.5332782
5/30/2019,Gas Scrubber Separator,Containment,,,,Weather,Steamed cabinet,user_157,asset_2089,48.1553924,-103.6216253
2/10/2017,Wellhead,ESD Valve,Actuator,Other,Other,Liquid Plugging,Needs swapped with new one ,user_74,asset_1525,48.33948207,-103.6365839
6/30/2019,SWD System,Motor,Switch Gear,,,,"Found that pump went down for Low Suction Pressure. Looking at PLC, filter pots have not switched or turned yellow, as they do when dirty. Walked around looking for leaks. None found. Checked turbines, #3 went down for flame out. This could have caused pump to stutter, losing pressures. We have the pump running at capacity which requires 2 turbines running. ",user_55,asset_1489,,
10/29/2019,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,Thawed out red freeze pots in front of ESD's and chokes on all wells and got 130 and 150 back to normal ops. Drained scrubbers and dezi. ,user_63,asset_1525,,
12/29/2017,Tanks/Pits,Flare/Combuster,,,,,"regulator to scc pilots frozen, thaw out relight",user_87,asset_464,40.7126799,-114.1193569
6/2/2018,Automation,Tower,Antenna,,,Weather,pad was down on comm error. autotech fixed comms issue. pad then went down on an esd shut down. edwards re downloaded pad. got interlock to clear. rtp well on plunger cycles,user_172,asset_1573,48.1470144,-103.6180489
4/3/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Desi had very little liquid. Probably less than 2 gallons. North 4 pack 14 regulators had lots of liquid. Desi might not be working. No liquid in other regulators. ,user_156,asset_886,48.31048283,-103.6494395
11/7/2017,Tanks/Pits,Liquid Level Control,,,,,"Pad down on high tank alarm, tanks verified and reported as false alarm. Optimization notified and automation notified. Repressure units, start compressor and warm up, RTP pad",user_109,asset_140,48.3534356,-103.6555576
5/23/2017,Compressor,Compressor,Panel,Sullair,,Vibration,"Found compressor down on low suction. Restarted and loaded compressor. I was told well 150 had an ESD issue and would not open, causing little gas to go to the compressor and go down on low suction. I opened the ESD and started plunger cycles on the well with out issue.",user_62,asset_1087,48.1470144,-103.6180489
3/27/2018,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,Fuel gas wet and in all scrubbers Walked location down with Austin and Dean Looked at some solutions and going to attempt to run fuel gas off the location just using the cold finger after some minor piping adjustment are made. To see if that helps. ,user_58,asset_1823,48.40628471,-103.5808382
12/20/2017,Compressor,Compressor,Cylinder,Ariel,,Trash,Issue: called out compressor down alarm Root Cause: down on hi 2nd stage discharge Fix: cleared alarm restarted ,user_136,asset_1452,48.0614644,-104.8417043
4/5/2019,Tanks/Pits,Flare/Combuster,,,,,"All 6 SCC's were down upon my arrival. All of them had pilot gas, may have been a fuel gas freeze earlier in the winter. Blew out liquids in the under ground line from separators to SCC's and lit all 6 of them.",user_15,asset_318,48.1470144,-103.6180489
4/18/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Looks like it was on the list due to non arrivals. Someone kicked well on and is now making arrivals. No action necessary ,user_141,asset_1498,48.1507842,-103.6207266
12/31/2016,Sand Separator,,,,,Other,Loss of production ,user_163,asset_575,47.99209523,-103.3606459
12/11/2017,Heat Medium,Surge Tank,Shell,,,,"Glycol pumps won’t move glyco, root cause Found suction and discharge lines where backwards swapped lines and heat trace is working ",user_122,asset_793,48.3574328,-103.7792341
12/7/2016,Gas Scrubber,Dump Line,Dump Line,Other,Other,Trash,Dump line was plumbed into glycol heat trace system,user_179,asset_1714,48.01341984,-103.4973315
3/10/2019,Fuel Gas/Start Gas,Regulator,,,,,"getting some liquid carryover and cannot thaw all fuel pots completely because not able to get close enough to back quad pack, will get a WO in to maintenance to get a path clear to get closer ",user_106,asset_365,40.5262342,-113.8824849
11/28/2017,Gas Scrubber Separator,Back Pressure Valve,Body,Taylor,,Corrosion,"well is loading in off cycle checked all valves and dumps all look good, well isn't really strong enough to make cycles and supply fuelgas to operate separator. could have a leak somewhere not ob-vi. ",user_71,asset_1643,48.1470144,-103.6180489
2/4/2019,Plunger System,Plunger,Plunger,IPS,,Corrosion,"Plunger vent 20 minutes, Plunger under sized due to wear (1.867/1.861/1.871) last inspection MAY18, OPS replaced with new, dropped, reset cycles and verified next plunger arrival. Adjusted criteria for a tighter line psi shut in set point, well loaded and lost arrivals due to a 15 PSI line increase 31JAN19 3:15 pm. Plunger arrivals a little inconsistent, adjusted criteria so that adjustments the automation makes due to plunger arrivals not being spot on at 700 ft/pm are not as drastic each change. Troubleshooting checklist completed. Tubing transmitter causing erratic criteria issues, emerson not capable of unit/line S.T.OP.PSI as an option though well cycles below high hi set point. Glycol circulation not functional to 70,120,110 and 20 wells despite not finding any ",user_54,asset_461,46.2356189,-100.6010498
8/12/2018,Wellhead,Tubing,,,,,Vented ,user_94,asset_120,,
8/15/2019,Automation,RTU,Relay,Vinson,Scadapack P4,Corrosion,issue with false high tank. was troubleshot but repair didn't solve issue. will need more troubleshooting. new task request entered,user_17,asset_752,,
10/13/2018,Compressor - Gas Lift,Compressor,Valves,Ariel,,Freezing,"Found compressor down on high discharge, looking at the graph it looks like the 10 was froze off in the casing.Venting casing to the tank to break the casing freeze,vented casing down to 375psi. Compressor had been down since 10/11 at 630pm. Checked both meth pumps for the 10 and 20 well, found that the pump on the 10 well was not pumping meth and had locked up. Primed pump and got it pumping again verified that the meth was pumping by shutting the valve on the meth tank and watching the meth down out of the sight glass and then open meth tank again.Started compressor and set rpms at 1350 injecting about 600 down each well.Went through all unit glycol bath and lit pilot and burners all burners were shut off. Cleaned out pilot on well 10 and while was through units I notice that the dump box gasket for the dump controller for the 20 well was leaking/ replaced gasket and rtp'd. I stayed on location till baths were temped up and adjusted t-12 s .",user_10,asset_2055,43.252261,-115.0567324
1/17/2019,Chemical System,Pump,Connecting Rod,Texsteam,HBT1,Debris,"+NO ACCESS TO METHANOL PUMP DUE TO FROZEN COW PIES UP AGAINST THE DOOR. ** FINALLY ABLE TO PRY UP SAID PIES AND DISCARD +METHANOL PUMP NOT GETTING FUEL SUPPLY THROUGH REGULATOR. **REMOVED PLUGGED SCREEN AND PUMP WAS OPERABLE AGAIN. +OLD STYLE RUPTURE DISC IN METHANOL SYSTEM, BAD. **REPLACED WITH PRV +**METHANOL PUMPING INTO LUBRICATOR NOW. ",user_34,asset_893,43.56424,-91.351691
7/3/2018,Water Transfer,Transfer Pump,,,,Erosion,"Ibex developed a leak at rear end of water trailer, resulting in a 1.247 gallon spill onto the turn around. The driver had the trailer parked outside of the sump/containment area next the the offload building. When asked why, the driver stated that when any one of the three axles at the rear of the trailer is parked in the containment and the other two are outside the containment, they run the risk of damaging their air bag suspension due to the sumped nature of containment. I coached the driver, stating that the offloading containment is large enough to accommodate all three axles and should still catch any liquids that may spill during transfer/hook up and prevent spills outside of offload containment and still allow drivers to hook up and complete offload. Driver agreed and said he would spread the learnings to the rest of his co-workersd his trailer up into offload sump/containment. D. Kinsey to follow up and communicate the learning to other contract companies.",user_6,asset_523,36.2541889,-91.2478009
2/23/2018,Fuel Gas/Start Gas,Regulator,,,,,regulator gummed up with paraffin. replace regulator and put pumps back into service,user_11,asset_2209,48.1604834,-103.6178751
3/18/2018,Flare System,Flare Header,Process Indicator,,,,"Used Fieldbit with John Marley to troubleshoot SCC showing out, but is on. Further repairs are going to be necessary: replace thermocouple, replace ignitor",user_141,asset_780,48.1470144,-103.6180489
2/21/2017,Instrumentation,Other,Other,Other,Other,Other,Tested no issues found,user_113,asset_128,48.21574272,-103.6224985
6/2/2019,SWD System,SWD Motor,,,,Weather,power bump,user_31,asset_538,48.1511744,-103.6275517
9/13/2018,Compressor,Compressor (Recip),Solenoid,,,,"Found compressor down on low compressor oil level. Checked level, it was full. Checked day tank, it is half full. Checked for any oil leaks, none found. Started compressor and watched oil level in Murphy site glass. Oil level stayed in full mark for the 5 minutes i watched it. If compressor goes down on low oil level again, ill notify JW for further trouble shooting. ",user_15,asset_1383,48.281657,-102.8553755
2/25/2019,Fuel Gas/Start Gas,Regulator,,,,,"Well down on production due to natural decline. Checked location and found line heater down, someone had shut main burner off, and fuel gas froze. thawed and got back up and running. re-lit SCC's and drained scrubbers.",user_63,asset_247,,
7/25/2019,Plunger System,Plunger,Plunger,Well Master,,Corrosion,Plunger measured at 1.87. Replaced with new bar stock plunger,user_153,asset_2013,48.1717322,-103.5953017
3/6/2017,SWD System,SWD Pump,Other,Other,Other,Other,"Replaced filters due to low suction on pump, and to assure they run through the night.",user_141,asset_1931,48.224585,-103.8291059
1/3/2019,Heat Medium,Furnace,Tube,,,, Had to dig out burner and clean flare arrestor before starting burner. ,user_31,asset_1412,48.257296,-102.8647072
9/14/2017,Plunger System,Plunger,Plunger,PCS,,Not Optimized,well lost plunger arrivals and was deferring production,user_179,asset_132,48.3619066,-103.2129855
1/17/2019,Tanks/Pits,Liquid Level Control,,,,,"False high tank that only shut in the 40 and 80 wells????? The 50, 130 and 160 wells were fine??? Optimizer is going to watch and see if it happens again.",user_94,asset_1595,,
4/22/2018,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,"call out high condo tank-checked HMI and A tank flashing yellow at 17'5'-went and swapped to b tank @ 8.2'- actual gauge is 16'10 X 4"" good ready load-so the level indicator is off-i had to raise alrm to 17'6 to clear also-will turn in as ready load-automation wo to check level indicator? ",user_131,asset_1841,40.7126799,-114.1193569
9/25/2017,Compressor,Compressor (Screw),Dump Valve,,,,"Compressor dumps out of adjustment, adjusted 1st stage ",user_122,asset_1675,48.37795405,-103.8078794
4/6/2018,Tanks/Pits,Liquid Level Control,,,,,"Issue: night gauger called and said water tank was 16' 3"" Root Cause: Human Error/Dispatch, some how dropped off schedule Fix: called IBEX and they sent a truck and pulled the water tank with 3"" to spare ",user_136,asset_1345,48.2628762,-102.8980842
4/7/2018,Flare System,Flare Header,Instrumentation,,,,Issue: found Abeutec SCC down on the HMI Root Cause: pilot failure/ no flame detected. found the pilot gas solenoid wasn't working Fix: was able to get working again relight the SCC. We would have a lot less down time if we removed the low pressure shut down and made them run all the time it would get away from these little failures like this that could make us go out of compliance ,user_136,asset_2274,48.1470144,-103.6180489
4/29/2017,Wellhead,Tubing,,,,,Slick line was working on well they have a plug in tubing this is why I was asked to flow it on the casing side.,user_51,asset_1343,48.1470144,-103.6180489
4/22/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,kicked well on got plunger to come in. turned off burp settings,user_11,asset_96,40.7126799,-114.1193569
2/8/2017,Gas Scrubber,Other,Other,Other,Other,Other,"Pilot out to scc, relight",user_87,asset_283,47.99713812,-103.4415981
1/21/2018,Separator,Temp Control System,Heater/Burner,,,,ESD valve was shut to main burner. Glycol at 41 degrees. ,user_156,asset_2239,48.22171022,-103.7497411
1/24/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Burner pilot was froze I thawed out line and relit burner and put back online.,user_51,asset_609,48.1470144,-103.6180489
8/29/2018,Instrumentation,Controller,,,,,"ENG REQUEST ENG wanted to see if we are about to cycle this pad instead of using gas lift. Four wells are on gas lift, I had to manually shut the chokes on them. Results of my finds are CB 21-140, DVC seems to be operating choke properly. CB 21-130, DVC has choke hung open. CB 21-120, DVC is not operating choke. CB 21-60, DVC seems to be operating choke properly. Email ENG and let them know what i found. Waiting for a response. ",user_56,asset_606,48.1470144,-103.6180489
7/10/2019,Wellhead,Valves,,,,End Of Design Life,The wellhead ball valves were leaking to atmosphere on the tubing and casing flow paths. All three valves were replaced. ,user_68,asset_1683,48.1470144,-103.6180489
12/17/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Desi and fuel gas scrubber of liquids daily routine auto dump may be a solution to issue ,user_109,asset_217,48.3264021,-103.6562588
1/14/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,Lost Fuel Gas; Flow Line and Sales Line Froze,user_139,asset_494,,
11/9/2018,Separator,Dump Line,,,,Freezing,Thawed out water dump because pad went down on low fuel gas and froze overnight,user_10,asset_1016,43.252261,-115.0567324
2/28/2019,Pipeline/Piping,Pipe/Components,,,,End Of Design Life,choke was not holding and needed to get replaced,user_28,asset_202,48.160359,-103.6176962
3/8/2018,Flare System,Flare Header,Process Indicator,,,,"Flare out, relit and returned to service ",user_58,asset_580,48.37253012,-103.5167082
7/30/2019,Generator,Cooler,,,,,"Generator went back down after about 3 minutes. Did some further investigation, found that all of the blades have broken off of the radiator cooling fan. Contacted TL and advised of findings and that we need to get Moser out here to make repairs. Contacted water haulers and advised location is down until repairs can be made. ",user_55,asset_523,,
11/8/2017,Flare System,Flare Header,Process Indicator,,,,SCC's down due to fuel gas freezing off and getting liquid packed even though both knock out pots didn't have fluids ,user_58,asset_876,48.41629082,-103.5772252
2/5/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,"TBG transmitter is showing 8#, Unit transmitter showing 303 according to PI report. TBG on location was 580#, Unit on site was 320#, Found unit bath at 60 bumped up T-12 Found glycol pump stalled out, got it stroking again. Found hydrate in flow line, shut TBG master and opened flowing to Atmosphere, re-pressurized flow line and verified hydrate broke. Put back to unit and well started flowing. ",user_53,asset_476,40.7126799,-114.1193569
1/4/2018,Chemical System,Pump,Instrumentation,Texsteam,HBT2,Power Supply,"glycol pumps are not running, let automation know about issue. waiting for response from team",user_53,asset_1416,40.7126799,-114.1193569
3/31/2019,Surface Location,Well Pad,,,,Weather,"Have advised no trucks to location until we can get some more snow removed on the corner by the SCC. You have to drive into a low spot with standing water, ground is very soft under water. Trucks will get stuck.",user_55,asset_1489,,
12/28/2017,Tanks/Pits,Liquid Level Control,,,,,"Issue: found the water tanks at 16' 8"" on the HMI Root Cause: Human Error/ Dispatch Fix: called IBEX and got the tanks hauled ",user_136,asset_1258,48.2525318,-102.9484357
7/27/2018,Flare System,Flare Header,Regulator,,,,"heavy rain fall snuffed out scc , adjusted regulator and relit scc",user_144,asset_886,49.5499678,-102.9290839
1/9/2019,Fuel Gas/Start Gas,Regulator,,,,,Burner went out causing fuel gas to freeze and flood ,user_18,asset_1662,,
8/26/2018,Flare System,Flare Header,Instrumentation,,,,Both SCC's and flare was out tanks pressured up. relit and returned to service.,user_63,asset_2034,48.224585,-103.8291059
12/18/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Desi and fuel gas scrubber of liquids daily routine auto dump may be a solution to issue ,user_109,asset_1280,48.3271482,-103.6564695
9/20/2019,Plunger System,Plunger,Plunger,PCS,,Not Optimized,well is very loaded / needs multiple vents/ vented well to unload fluids and rtp'd,user_10,asset_1681,40.5262342,-113.8824849
10/23/2019,Separator,Fuel Supply System, Big Joe Regulator,,,corrosion,"arrived onsite found tubing pressure below line pressure with pumps and burners on. shut in well and attempted to vent in plunger, was unsuccessful. shut well in for several hours and returned to site. vented well again got well to unload but plunger never came in. pulled graph and judging by previous cycles this well does not have a plunger. pulled lubricator cap and found no spring or anvil.contacted engineering to find out if a BSSV had been installed,he is gonna get back with me.ordered a bar and big spring for this well. removed the plunger installed sign on wellhead. pressured up separator relit burner. put well back on shut in cycles. will return tomorrow and drop plunger if engineer clears it",user_120,asset_222,40.5262342,-113.8824849
12/14/2018,Compressor,Engine (Gas),,,,,"The heat trace was cold going to the compressor, I found one valve on the line blocked in and I pinched some of the valves on the header back to force more warm glycol to the compressor",user_22,asset_1339,38.4425988,-95.5406131
6/24/2018,Gas Scrubber Separator,ESD,,,,,"HP 23-80 low flow callout, line pressure was at 800 PSI, unit#155A & #155B were at 895PSI. shut in site at around 9:00, RTP at 1:30. wasn’t able to open chokes much because line pressure still wasn’t at normal range but units aren’t over pressuring. Dayshift will need to finish opening.",user_71,asset_341,48.1498113,-103.6213224
10/7/2017,Separator,PSV,Spring,,,Incorrect Set Point,PSV is popping off at 300 psi on Seperator needs replaced shut in currently.,user_51,asset_1723,40.5960545,-113.9323891
1/17/2017,,,,,,,Shut in well for pressure build,user_35,asset_54,48.0925054,-103.4978047
7/24/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash,"choke leaking by loading up well, cycled choke and it sealed",user_87,asset_1037,40.5262342,-113.8824849
3/2/2018,Compressor,Engine,Control Panel,Ajax,,Human Error,"Found wells 120 and 150 not getting full injection rate. Went to sight and found compressor was running, but RPMs were set to low from last restart. RPMs were set at 1490, it is wrote on the panel to run between 1550 and 1650. Increased RPM to 1600. Injection rate went up to 1.0 MMCFD, as it should be. Wells unloading good.",user_62,asset_794,40.5960545,-113.9323891
1/22/2018,Automation,Solar Panel,Glass,BP Solar,,Weather,Cleaned snow off of solar panels.,user_62,asset_2017,48.1470144,-103.6180489
11/24/2017,Tanks/Pits,Liquid Level Control,,,,,Pad shut in on false high tank. Night shift got pad back online but chokes need to be opened more. Opened choke 5-64,user_172,asset_876,,
3/24/2018,Heat Medium,Pump,Plunger,Sunpumper,HBT2,Freezing,"Found pump stoking very slow. Found pressure set for 15 PSI. Increased pressure to 20 PSI. Pump stroking much better. Root cause, this is a very weak well, ops trying to minimize fuel gas usage across location so pump was set to low pressure. I only increased pressure because water tank is frozen and needs to be thawed.",user_62,asset_1956,48.1470144,-103.6180489
11/7/2017,Pumping Unit,Engine,Battery,Waukesha,,Wear,Replaced battery & RTP'd.,user_161,asset_1789,40.7126799,-114.1193569
10/23/2017,Wellhead,Tubing,,,,,froze downhole broke freeze and lit bath heater,user_11,asset_2155,40.5262342,-113.8824849
11/22/2017,Heat Medium,Pump,O Ring,Texam,HBC1,Freezing,Tubing Transmitter still freezing hampering Plunger Cycles - Root cause is low level in Glycol bath starving pumps at Suction port. Have been waiting two weeks on Glycol top-off from BrennTag,user_138,asset_2152,48.16980993,-103.4463705
10/14/2018,Instrumentation,Controller,,,,,ASCO solenoid failed. Unknown cause. Possibly freezing.,user_12,asset_919,48.1470144,-103.6180489
7/4/2018,Wellhead,Tubing,,,,hydrate,"ARROW Dispatched to well, well is deferring. Found well froze in the WH. Root cause: out of methanol. Chemical order has been submitted waiting on chemical",user_53,asset_1499,40.5960545,-113.9323891
3/3/2019,Dehy,WFS Issue,,,,,"came to location to find both dehys have now been shut on this pad, the fed and the fee side, they are froze off and couldn't break freeze. On Thursday one dehy was up and now both are shut, heat is up but they are still froze off. Pad is sitting idle and can be addressed when Williams is up and ready to run. They were notified Thursday/Friday and are working the issues. ",user_106,asset_770,48.1470144,-103.6180489
8/8/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Trash,Replaced Load Line Valves and 2 Drain Line Valves On Both Condo Tanks ,user_119,asset_1267,48.1602508,-103.6173294
10/15/2019,Separator,Temp Control System,Pilot,,,,"fire blown out, lost unit pressure, bring back up and RTP",user_121,asset_1531,46.2356189,-100.6010498
6/22/2017,Pipeline/Piping,Pipe/Components,,,,Erosion Corrosion (Internal),"2"" Blowdown spool connecting to Blowdown tank replaced due to hole caused by internal erosion",user_150,asset_1808,,
8/9/2018,SWD System,SWD Motor,,,,Overload,ARROW PLUS SITE CHECK INJECTION DOWN AT 12:36 AM DUE TO A POWER BUMP SITE INSPECTION- EVERYTHING OK RESTARTED INJECTION 6:00AM INJECTION RATE 2100BBLS,user_34,asset_538,48.1470144,-103.6180489
3/22/2018,Compressor - Gas Lift,Compressor,Valves,Frick,,Liquid Carryover,Meter on injection line was reading in flowrate. Went to location to verify GL was still shut in it was. Thawed on injection meter. Had some fluid built up in meter causing it to read inaccurately. Got it all blown out and reading correctly ,user_172,asset_247,,
2/20/2019,Surface Location,Well Pad,,,,Weather,The turnaround and surface equipment need snow plowed or removed.,user_68,asset_1615,48.1470144,-103.6180489
6/24/2018,Automation,Radio,Wiring,Cellular,,End Of Useful Life,This is for a SixNet 5MS network switch. WHAT IS THE POINT OF THE REQUERED DROPDOWNS IF OUR ACTUAL EQUIPMENT IS NOT IN THEM? ,user_134,asset_1805,36.2541889,-91.2478009
3/1/2017,Sand Separator,Shell,Body,Other,Other,Other,Had a freeze in horseshoe between choke and vessel at HI/LO. Thawed and RTP'd well,user_141,asset_524,48.224585,-103.8291059
10/21/2017,Compressor,Compressor,Scrubber Level,Ariel,,Freezing,,user_48,asset_1675,,
10/14/2019,Instrumentation,End Device,Thermocouple,,,End Of Useful Life,"Replaced thermocouple and cleaned orifice, changed fuse to transformer, re-lit pilot and verified operations in RTU. Verified operation with optimizer.",user_44,asset_1901,46.2356189,-100.6010498
10/30/2019,Separator,Choke Valve/Loop,,,,Freezing,"Found all well down and frozen , looks like pad was down overnight . Thawed out front end of the unit and vented wells to unload so that the unit would stay up and run. After getting all the equipment up and run I could flow the well because the automated valve on the dehy would not stay open. Contacted dehy tech to troubleshoot problem. Jumped all unit on and started glycol bath and pumps to prevent the unit from freezing until dehy problem can get fix.",user_10,asset_71,40.5262342,-113.8824849
3/22/2019,Separator,Manual Drain Valves,Ball/Seat,,,Freezing,blow down valve was frozen and I had to thaw to blow down form well to separator,user_22,asset_1617,46.2356189,-100.6010498
4/17/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash,"Well was coded to OPS to RTP and gather data. Walked down location and surface equipment. Started with the dehy just to make sure it wasn't TD'd. Separator looked fine. WH, found TBG master open, top two flow paths (KF) valves closed. TBG was at 602 CSG was at 631 Attempted to open those KF valves, no success SI TBG master and opened third flow path to get the pressure off Still was not able to open valves, got a 24 inch pipe wrench and tried opening them, Valves are ceased shut pipe wrench was tripping the top of the valve. Also found that the choke was leaking liquids through the stem. Coded well",user_53,asset_1432,48.272436,-102.8742355
10/8/2017,Compressor,Engine,Starter,Caterpillar,,Wear,"Compressor had gone down on Hi Engine Water Jacket. Engine had cooled down, but wouldn't start. Contacted NGSG tech and advised of issue. NGSG tech found starter solenoid bad. Replaced and restarted compressor. He also mentioned they have a new radiator and water pump coming for compressor.",user_141,asset_551,40.5960545,-113.9323891
10/18/2017,Instrumentation,Switch,,,,,Unknown why they failed,user_65,asset_1522,48.0614644,-104.8417043
4/23/2019,Surface Location,Well Pad,Gate,,,Erosion,Gate and posts laying on ground around the old reclamation area.,user_146,asset_912,47.9751553,-103.6561574
4/5/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Corrosion,excessive wear,user_173,asset_2210,48.1470144,-103.6180489
4/3/2017,Wellhead,Primary Choke,Other,Other,Other,Other,drained dvc got alot of liquid to drain out dvc was able to completely blow down and choke closed completely and its not leaking.,user_11,asset_143,,
7/21/2018,Wellhead,Tubing,,,,,"LD 11-60 showing 168mcf deferral, looks like well was kicked on yesterday well made an arrival but looks like water dump stuck open and loaded well up. found dump box vent clogged and pressured up, dump parts are covered in scale, cleared vent hole, dump is functioning. Vented well and watched next cycle, made arrival but was slow and then wouldn’t meet load ratio. went back to site and shut FMC and ESD, pressure started dropping quickly vent line cyclonic is leaking, well looks like it started having issues on 6/12. Unloaded well and restarted cycles.",user_37,asset_76,48.1499168,-103.6211877
5/18/2018,Compressor,Compressor,Dump Valve,Ariel,,Liquid Carryover,"comp down on 1st stage scrubber lvl, adjusted dump and restarted comp, engineering is engaged and working on the fix",user_122,asset_1383,48.0614644,-104.8417043
8/3/2018,Gas Scrubber Separator,ESD,,,,,"3 mile 23-#110,#50,#90 had Emmet restart after automation work, watched cycles and wells made arrivals the rest of the night. Mike got HMI working around the same time. ",user_37,asset_2013,48.3619066,-103.2129855
4/27/2018,Automation,Radio,Wiring,3M,,Unknown,"Luman 8 in comm error showing no flow in Emerson or PI went to location and made sure well was flowing everything looks OK and is working, automation and TL aware of issue.",user_71,asset_1383,48.1470144,-103.6180489
6/15/2017,Tanks/Pits,Tank Level,Sonar,,,Weather,"*****Not able to enter ""Physical Damage"" in root cause***** 5. Latham Draw 17-10 - Tank level switch broken on water tank • Inspected al tank switches • Found no broken switches • Found a tank level transmitter case broken • Powered down transmitter • Went back to warehouse to get a new transmitter • Installed new tank transmitter • Programmed new transmitter • Configured new transmitter Gauged and verified new transmitter reading correctly to HMI",user_92,asset_809,40.5960545,-113.9323891
5/27/2019,Dehy,Meter (BP Check),,,,,Sales line frozen between separator and dehy,user_31,asset_1336,43.56424,-91.351691
7/15/2019,Separator,Valves,,,,End Of Design Life,The Invalco Dump Valve was washed out. It was replace with a new Kimray Dump Valve.,user_68,asset_479,48.1470144,-103.6180489
4/4/2018,Wellhead,Manual Valve,Master Valve,,,Erosion,"Both tubing master valves and the single casing valve all leaked. Attempted greasing all 3 valves but could not slow the leaks. Contacted production team leader and engineer. Engineering planning to put well on rig schedule to replace both tubing master valves and the single casing wing valve, including possibly adding an additional casing wing valve.",user_161,asset_747,40.7126799,-114.1193569
1/25/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Drained desi dryer while on location working on wells 120 and 30.,user_62,asset_296,48.1470144,-103.6180489
12/6/2017,Compressor,Compressor,Suction Controller,Ajax,,Liquid Carryover,Root cause of failure was liquid carry over causing freeze in pressure sensing line to suction controller. Recent significant drops in temperatures caused the liquid carry over. Bath temp will be adjusted to ensure proper gas temp to prevent further issues with liquid carryover. ,user_75,asset_774,,
9/25/2017,Flare System,Flare Knockout,Shell,,,,"SCC ""C"" on Pad extinguished by Rain last night- Relit ",user_138,asset_1187,48.18379627,-103.4260861
7/8/2019,Instrumentation,RTU,Io,Vinson,Total Flow Micro,Wildlife / Livestock,Swapped out plc card,user_16,asset_405,,
8/25/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Lost arrivals, production dropping off, time to catch and inspect plunger, should be producing around 160 mcfd. I will change out if needed, and log",user_84,asset_1091,48.05289563,-103.5296867
1/23/2019,Chemical System,Tank,Shell,,,Empty - Methanol,+METHANOL LOW **ORDERED 400 GALS METHANOL,user_34,asset_1579,43.56424,-91.351691
12/1/2017,Automation,Plunger Arrival Switch,,EDI,,,,user_0,asset_1202,48.2522043,-102.7574194
6/9/2017,Plunger System,Plunger,Plunger,PCS,,No Liquid,Plunger got one fast arrival and well didn't cycle after that,user_179,asset_1418,47.90808983,-103.6723982
3/29/2019,Pipeline/Piping,Valves,,,,End Of Design Life,"choke got washed out, crew replaced stem seat and packing",user_28,asset_425,48.1511744,-103.6275517
4/19/2018,Tanks/Pits,Flare/Combuster,,,,,"Did hand over with maintenance team. They added a down stream cyclonic on the 29-2 also installed a check valve in the sales line so the 120 wouldn’t back feed through sales into the 29-2. Meet with well site leader onsite, they are pulling tubing on the 2, but our currently shut down. Explained my job scope and how they would be effected.Maintenance team and I pressure tested there work using 100 psi from the 29-2. No leaks were found.cleared high tank alarm on hi/lo. Brought on well split flowing to blowdown and selling to Williams on a 16/64 choke. Currently flowing around 2.0mil. Lit line heater and separator bath. Will continue to open choke waiting on temp to increase on sales current temp is 43degrees. Relit scc’s ABC. Well rtp",user_172,asset_599,,
6/25/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,had karsky adjust the high line pressure set point kicked well on and achieved plunger arrival. cycles resumed,user_11,asset_383,43.252261,-115.0567324
7/26/2019,Fuel Gas/Start Gas,Regulator,,,,,Big Joe was leaking by and filling up separator with fluid. We contacted TL with the issue at hand and was advised to get rebuild kits for the big Joe. We closed all necessary valves and released all pressure before undoing the hammer unions on each side of big Joe. When we took apart big Joe we found a bolt floating around inside by the diaphragm. Bolt was worn and threads were missing. We STJ and went to BP office and got another big Joe out of junk pile to get the bolt we needed. We did full rebuild on big Joe and reinstalled and pressure tested. There were no leaks and big Joe was functioning correctly.,user_47,asset_362,48.1828685,-103.537814
2/15/2017,Gas Scrubber,Other,Other,Other,Other,Other,Cleaned tip,user_87,asset_2174,47.9673521,-103.4474092
2/8/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Dispatch to perform fluid shot surveillance after plunger has missed 2 arrivals during the optimization process post tbg repair and swab for RTP. Check pressures, tbg 574 psi and csg 695 psi. Pull WBD for tbg intake (EOT) depth and bumper spring (X Nipple) depth. EOT at 10774’ and BSSV set in nipple at 10729’. Shoot annulus and find 658’ of fluid over EOT. Shoot tbg and find 1153’ of fluid over BSSV. Conference with optimizer to adjust cycles to be more conservative targeting stronger LR between cycles with minimal after flow before re dropping plunger for next cycle. Optimizer to continue adjusting cycles for clean up and will re code once cycles are established and production stabilized. ",user_75,asset_21,,
3/9/2018,SWD System,Particle Filter,Element,,,,South filters changed. We’re just bypassed 2 week ago and not changed ,user_156,asset_1583,48.16508719,-103.6813387
6/15/2019,Separator Inlet Valve (XV),ESD Valve,Gate/Seat,,,Fouling,Stem was stucl not allowing Hi/Lo to open.,user_14,asset_338,46.2356189,-100.6010498
10/10/2017,Instrumentation,Communication Card,,,,,Needed to reload wonder card configuration. Confirmed updates in Reflections,user_99,asset_604,40.5960545,-113.9323891
2/28/2018,Separator,Choke Valve/Loop,,,,Freezing,Drained/checked Kimray drip pot on choke for fluids. No fluids present.,user_62,asset_1510,48.1507625,-103.6206926
12/6/2017,Gas Scrubber Separator,Dump Line,,,,Freezing,,user_126,asset_680,,
3/23/2018,Heater Treater,Burner,BMS,,,Loss Of Fuel Gas,"Issue: found bath (A) down. no (INT) Root Cause: Human Error, went to location and walked threw the bath and made sure nothing was tagged out and everything was lined up. looks like the pad had issues and once the work was done no one went back through the pad and made sure everything was in order before leaving Fix: relight bath remotely and returned to service While On location: i drained the desi and both scrubbers and there was a lot of fluid in all of them ",user_136,asset_175,48.0614644,-104.8417043
3/8/2019,Separator,Liquid Dumps,Controller,Kimray,,Improper Adjustment,Water dump hung open. Draining the unit and relieving the pressure. Pressured up vessel and adjusted dump. Lit fires once up to temperature started glycol pumps and RTP well,user_153,asset_820,48.23632805,-103.627035
1/1/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Kelvin lost plunger arrivals and failed to retrieve plunger ,user_53,asset_2262,48.1603614,-103.6174489
3/10/2018,Gas Scrubber Separator,Mechanical Dump Valve,Controller,Kimray,,Liquid,"Issue: Called out shut in alarm (INT) low unit pressure Root Cause: found the water dump is sticking by no water in the water side. The dump looked fine but when I manually dumped it then it wouldn't deactivate and the fuel gas was blowing back out of the piston. I pulled the snap controller out of the the dump body and found it had been flooded and got filled up with paraffin and plugged off the vent screen. Not allowing the dump to bleed off and deactivate. Fix: I was able to take the snap apart clean it up put back together and got working good again. Rest the dump and verified it was going to stay working and not restick While on location: I drained all the filter to the ESD's, chokes, drained the scrubber and desi",user_136,asset_661,48.2595296,-102.9010832
12/10/2018,Heater Treater,Burner,BMS,,,Freezing,"Issue: found heat trace cold Root Cause: Human Error, to start found the line heater set at 90deg. Not all the lines from the glcyol pumps were hot Fix: rest T-12s and got line heater at 150deg. then adjusted the valves to get hot glycol thought the location ",user_170,asset_1160,43.56424,-91.351691
4/2/2018,Plunger System,Plunger,Plunger,PCS,,Corrosion,PLGR worn out from long use. Dropped new PCS PLGR,user_107,asset_1114,,
2/26/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Line hater fuel system does not work in winter operations,user_60,asset_1257,40.5481548,-114.0112915
1/23/2017,Wellhead,ESD Valve,Gas Supply Line,Other,Other,Freezing,Fuel supply line was froze. Thawed it out and put back in service ,user_53,asset_1160,48.06804596,-103.3832559
9/5/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,Issue: well was deferring Root Cause: found a couple of leaking dumps and blow down. wrote a work management and got them fixed but the well was still logged off Fix: unloaded well turned back on. will get with optimizer to relook at the cycles ,user_170,asset_1181,43.56424,-91.351691
12/14/2016,Wellhead,Cyclonic Valve,Gas Supply Line,Other,Other,Liquid Plugging,"Filter issue, replaced ",user_74,asset_42,48.15915275,-103.6109495
3/20/2019,Chemical System,Tank,Shell,,,Empty - Methanol,empty,user_56,asset_1822,48.1470144,-103.6180489
7/5/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,Blowdown valve to tank was replaced it was installed backwards,user_165,asset_1192,48.1602556,-103.6173399
11/27/2017,Instrumentation,Meter,Orifice Plate,Bristol,1,Calibration Issue,Requested Williams to check their meter and reduce orifice plate size.,user_99,asset_2250,48.1470144,-103.6180489
11/27/2018,Separator,Fuel Supply System,Regulator,,,freeze,"desi is froze, probably from heat trace not being started until nov 26th",user_31,asset_1892,48.2718601,-102.8688141
4/16/2018,Pumping Unit,Engine,Fuel Gas Supply,Cummins,,Human Error,"Fuel gas pressure was over 30 psi, Cummins engine require 2-8 psi of fuel gas. I got fuel gas psi down to around 10 psi, there is top large of a regulator at separator making adjustments tedious. I will continue dialing in emissions later this week. ",user_161,asset_1083,48.2145975,-103.4532314
10/10/2017,Plunger System,Plunger,Plunger,IPS,,Not Optimized,,user_11,asset_11,40.5960545,-113.9323891
8/22/2019,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Well was cycling but plunger was not arriving. Vented well for 13 mins and got plunger to arrive. Swapped plunger, new dual pad dropped on 22AUG19 Put back on cycles.",user_56,asset_2257,48.1470144,-103.6180489
2/13/2018,Tanks/Pits,Liquid Level Control,,,,,"Issue: found live reads show tank # 3 16' 6"" Root Cause: Human Error, found the tank had 17' 1"" and was about shut in. This location has two water tanks with a cross over at 4' and one side of it was closed. On this older set ups the dump line only dumps to one tank and then it equalized to the second tank through a crossover at 4'. It looks like a truck driver shut the valve to pull the tank and forgot to reopen it Fix: opened valve and equalized the water tanks ",user_136,asset_1136,48.0614644,-104.8417043
6/15/2019,Wellhead,Wellhead Piping,,,,,"o-ring in lubricator torn, replaced",user_64,asset_819,41.4332083,-112.058189
12/15/2017,Tanks/Pits,Flare/Combuster,,,,,SccA and flare where out. Drained fuel gas relit both,user_172,asset_1800,,
1/3/2019,Tanks/Pits,Tank Level,Sensing Cable,,,Weather,Had 1 injection tank showing 15.3 ft and the others were at 6.5 ft. Guessed that the discharge side of tank had a freeze at the opening not allowing it to drain. Made up an extra long thaw tube and put it on tank. Waited about 15 minutes and checked the level on the PLC. Level was dropping fast. Continued to thaw to make sure it was correct. Ended up that the only thing wrong was the level tape. Just a little bit of heat fixed it.,user_55,asset_1489,,
7/24/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,,user_179,asset_14,40.5960545,-113.9323891
3/27/2019,Separator,Fuel Supply System, Big Joe Regulator,,,debris,Found the fuel gas line to the scrubber pot on this unit had no pressure / found that the fuel gas line to the scrubber was filled with desiccant and obstructing the gas from getting to the scrubber pot to supply the esd and chokes with pressure. Removed big joe and clear line of obstruction and rtp'd well . Contacted optimizer to review cycles,user_10,asset_362,40.5262342,-113.8824849
12/30/2016,Gas Scrubber,,,,,,"Well froze off in the above ground piping during the night, insulation and heat trace was added to piping today so that should not be an issue again",user_148,asset_1083,48.26319242,-102.8995669
8/12/2019,Chemical System,Pump,Diaphragm Gears,Texam,HBT2,Wear,The Western methanol pump was not stroking. It was replaced with a rebuilt unit.,user_68,asset_1794,36.247824,-91.2533664
7/31/2018,Flare System,Flare Header,BMS,,,,"Issue: found SCC (B) down on the HMI Root Cause: Human Error, looks like after the work got done and the location got turned back on the SCC's didn't get relight Fix: relight and returned to service ",user_170,asset_1286,48.224585,-103.8291059
2/28/2019,Wellhead,Manual Valve,Needle,,,Freezing,needle valve at tubing transmitter split and blowing gas. froze and split,user_64,asset_2007,39.2506642,-92.4357879
4/19/2017,Wellhead,Other,,Other,Other,Other,Loss of production,user_84,asset_266,47.88292597,-103.5195638
6/3/2019,SWD System,Coalescer/Filter,Elements,,,,changed both filters,user_31,asset_1847,48.1511744,-103.6275517
7/22/2018,Fuel Gas/Start Gas,Coalescer/Filter,Regulator,,,,"Site visit to check compressor and make sure it is online due to PI not reading in. Drained desi, found it full of liquid. Compressor was online, left as is ",user_56,asset_910,48.2726243,-102.8734951
12/23/2017,SWD System,SWD Pump,,,,Corrosion,2” valve in offload building has pin hole from corrosion ,user_156,asset_1583,48.27160115,-102.8690463
8/23/2017,Instrumentation,Meter,Orifice Plate,Kelley,1,End Of Useful Life,,user_113,asset_1029,48.23330214,-103.6526066
4/11/2019,Chemical System,Pump,Instrumentation,Texam,HBC1,Power Supply," 8. Five Mile 24-130 - Solar methanol pump issue • Found methanol pump disconnect switch off • Found fuse for methanol pump batteries removed with no tag as to why • Replaced fuse • Switched methanol pump disconnect to the ""On"" position • Tested and verified methanol pump is functioning correctly • I labeled Methanol pump control box for operations Left pump running",user_38,asset_1741,40.5262342,-113.8824849
3/19/2018,Pumping Unit,Sensor,,,,,Load cable broke ,user_46,asset_588,48.0614644,-104.8417043
7/22/2019,Wellhead,Tubing,,,,,Plunger was stuck in well head due to sand. Contacted engineer and are going to have slickline come out. SI tags on well head.,user_94,asset_1355,39.2506642,-92.4357879
9/13/2019,Separator,Fuel Supply System,Regulator,,,fluid,Unit was down on low unit pressure fuel gas supply was closed on the well with the downstream valve on it . Opened valve and pressured up fuel supply system and rtp'd well back in cycles.,user_10,asset_290,40.5262342,-113.8824849
3/15/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"plunger needed changed out, well needed vented",user_88,asset_1388,48.2574996,-102.9118189
11/27/2018,Heat Medium,Pump,Process Indicator,Texam,HBC1,Freezing,glycol pumps were running when glycol temp was 32 degrees- started burner,user_31,asset_854,48.2718734,-102.8688258
8/20/2019,Separator,Liquid Dumps,Seat/Ball/Piston,Nalco,,Erosion,"Found that the condo dump had stuck open. Checked everything, controller ok. Found that it was leaking by dump trim. Replaced dump trim stem, seat, and packing. Had a lot of rust in dump diaphragm. Cleaned it out, and got everything working normally. RTP'd well. Well is not loaded or anything.",user_55,asset_1458,,
3/13/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Brought up ,user_86,asset_1970,,
3/15/2019,Separator,Choke Valve/Loop,,,,Corrosion, + TAG ON GLYCHOL BATH T12 FROM DAN BAUMGRAS INDICATES T12 NEEDS CHANGED-METH PUMP PRV NEEDS INSTALLED- INVALCO INLET VALVE LEAKS. ,user_34,asset_2031,43.56424,-91.351691
4/25/2018,Compressor,Compressor,Instrument Gas Supply,Ajax,,Freezing,Out of methanol Frozeoff in injection point/casing,user_111,asset_1623,48.09446547,-103.342828
5/3/2018,Fuel Gas/Start Gas,Regulator,,,,,"choke loop freeze, took pressure off, blew to tank, RTP",user_88,asset_2101,48.1470144,-103.6180489
6/8/2018,Compressor,Compressor,Process Gas Supply,Ariel,,Trash,Compressor down on low interstate pressure when I went to location I found the low set point on the kills on for the interstate pressure were set above the low limit I reset it and put back online.,user_51,asset_652,48.1470144,-103.6180489
2/19/2019,Separator,Temp Control System,Heater/Burner,,,, +SEPARATOR COLD FIRES OUT,user_34,asset_1817,48.1470144,-103.6180489
12/15/2017,Compressor,Compressor,Suction Controller,Ariel,,Freezing,"Suction controller supply gas froze thawed out an turned rpms up to help warm up hot start gas and glycol lines , moc in to remove compressor ",user_122,asset_1675,48.35152243,-103.6543269
5/22/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,well was missing plunger arrivals,user_179,asset_1141,48.1470144,-103.6180489
11/12/2017,Fuel Gas/Start Gas,Coalescer/Filter,Level Controller,,,,Full of liquid ,user_156,asset_2239,48.22227507,-103.7509942
6/17/2018,Flare System,Flare Header,Process Indicator,,,,Flare out relit and returned to service ,user_58,asset_1417,48.37292088,-103.5168847
9/27/2017,Compressor,Compressor,Suction Controller,Ariel,,Liquid Carryover,"Found liquid in recycle controller, cleared out liquid form warm gas line temp that is cooling off and carrying over liquid, restarted compressor ",user_122,asset_1675,48.38725896,-103.8412683
8/4/2018,Compressor,Motor,Windings,,,,Gas lift compressor was done due to a power surge. Restarted and loaded compressor. ,user_68,asset_345,48.01076583,-103.429318
1/15/2018,Automation,RTU,Relay,Vinson,Bristol 3310,Wear,"the glycol pump which is electric going to the wells 10, 20, 40 is not working tried to restart and the fuse block is showing a red light will turn in work order to get repaired",user_176,asset_1707,48.1470144,-103.6180489
11/8/2016,Pumping Unit,Engine,Control Panel,Other,,,,user_179,asset_387,48.0252799,-103.4868033
11/27/2018,Separator,Temp Control System,Heater/Burner,,,,"Well was loaded. Pulled a graph, looks like it does good when casing pressure is around 400 psi. Vented casing down to 400, plunger arrived. Did not inspect, looking at history, plunger was replaced 11 days ago. Burner was out, big joe froze. Thawed it out. Attempted to relight burner, pilot would light but main would whoof real bad and blow pilot out. Left only the pilot on. Will write a work order to have pilot length adjusted so this doesn't happen",user_55,asset_826,,
10/14/2018,Compressor - Gas Lift,Engine,Fuel Gas Supply,Ajax,,Weather,"frozen fuel gas, caused by hooking into old glycol system and pump can't buck the additional line restriction",user_31,asset_1049,43.252261,-115.0567324
1/26/2018,Heat Medium,Pump,Seals,Texam,HBC1,Wear,2 Graco 1050 Glycol pumps quit working and would no longer pump glycol,user_150,asset_671,48.1470144,-103.6180489
4/3/2018,Compressor,Intrumentation,,,,,"`Compressor down on unknown reason; failure to crank code, no other code present. Restarted comp and it went down on second stage scrubber level. Confirmed fluids in the scrubber, confrimed first and second stage scrubber dump functionality and cleared fluids out. Thumbed the second stage scrubber dump. No audible fluid sounds going to tanks. Opened manual scrubber dump to the tanks and heard fluid moving through lines. Engaged bob with JW to come check his set points/functionality on the second stage scrubber dump. Fluid going to the flare and the compressor due to overnight temperature drop and both end devices are colder then the preceding pipe that feeds the gas in unisnulated sections, causing fluid drop out. (ambient temperature over night 10 F). Compression running with no leaks or spills @ 33 PSI suction when OPS left site.",user_6,asset_1383,36.2541889,-91.2478009
10/16/2019,Tanks/Pits,Flare/Combuster,flare knockout drain pot,,,fuel gas freeze,"one of the ESD's did not work out of the four on location while I was there a few days ago so I shut off the fuel gas supply to the ESD and pilot to what I thought was just that SCC and tagged it out. Today the Wyolectric hand called me to pull my tag, when I arrived on location I found all the SCC's down, the fuel gas supply is daisy chained together so when I shut in the fuel gas to what I thought was just the one that needed attention I actually shut in all of them. Opened valve, got pilots lit and Wyolectric hand fixed valve then had Brett open ESD's to all four SCC's, working good now.",user_22,asset_1152,,
9/13/2018,Pumping Unit,Engine,Starter,Waukesha,,Wear,Replaced starter & RTP'd pumping unit in automatic at 3.88 SPM.,user_161,asset_1644,48.1641874,-103.5767182
10/16/2018,Compressor - Gas Lift,Engine,Control Panel,Cummins,,Controller Failure,"CALLOUT Gas lift called out, got to location and found that it went down on EICS Walked down compressor and then blew it down and restarted it. Allowed it to warm up then loaded it RTP'd compressor and well ",user_56,asset_1976,48.1603837,-103.6188462
3/31/2017,Gas Scrubber,Other,,Other,Other,Other,,user_53,asset_747,36.2541889,-91.2478009
5/12/2018,Tanks/Pits,Flare/Combuster,,,,,"Flare was out due to high winds and rain/hail. Relit and returned to service,",user_50,asset_787,48.1470144,-103.6180489
9/15/2017,Separator,ESD Valve,Gate/Seat,,,Corrosion,Maintenance replaced washed out hi lo body. ,user_35,asset_1031,48.31199823,-103.4082404
1/16/2019,Fuel Gas/Start Gas,Regulator,,,,,Freeze in fuel gas to chokes and DVCs thawed where I could reach but need snow removal on turn around and around all equipment ,user_18,asset_910,,
6/11/2019,Pipeline/Piping,Valves,,,,Corrosion (Internal),Replace ball valve,user_157,asset_1271,46.2356189,-100.6010498
10/25/2018,Flare System,Flare Header,Instrumentation,,,,Had to physically relight SCC A. Ignitor not working,user_55,asset_329,,
5/10/2018,Wellhead,Tubing,,,,hydrate,"plunger stuck in lub cap, found meth tank empty, shut in cycles on well till meth is delivered, ordered methanol 5-10-18",user_122,asset_882,48.0614644,-104.8417043
1/30/2017,Wellhead,ESD Valve,Gas Supply Line,Other,Other,Liquid Plugging,Liquid in fuel gas supply got into regulator and froze off supply gas to ESD. ,user_58,asset_2167,47.99623425,-103.3744718
8/10/2018,Wellhead,Cyclonic Valve,Gate/Seat,,,Corrosion,cyclonic valve leaking thru,user_174,asset_8,48.1603206,-103.6187321
4/21/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,fluid,"Checked scrubber on rental line heater for fluids, no fluids present.",user_62,asset_567,48.1470144,-103.6180489
3/16/2018,Fuel Gas/Start Gas,Regulator,,,,,"Well went down due to liquids in the fuel supply line. Found bath temperature to be 90 degrees and suspect liquid carryover in the fuel supply lines. Drained all lines, set T12 at 80 degrees for bath temperature and rtp’d well ",user_163,asset_1904,48.1470144,-103.6180489
1/9/2019,Separator,Fuel Supply System, Big Joe Regulator,,,freeze,Found unit down on low fuel gas pressure with all esd's shut in. Jumped pad up and the dvc for the 150 well was not opening and maintaining unit pressure in the unit with the downstream valve which was causing the unit to go down with the pumps and burners running. Thawed out dvc /drip pot and drained checked all dumps to make sure everything was free and dumping. I did find a freeze in the big joe that may have caused unit to go down. Thawed big joe and rtp'd well plunger making arrivals.,user_10,asset_818,48.1483424,-103.6183712
5/10/2018,Separator,rupture disk,,,,premature rupture,Recent replacement rupture disc is currently leaking. Shut well in,user_35,asset_1115,48.18249594,-103.4937406
4/5/2017,Tanks,Valving/Swedges,Body,Other,Other,Corrosion,Valve leaking by,user_165,asset_187,48.224585,-103.8291059
9/11/2019,Pipeline/Piping,Valves,,,,End Of Design Life,"The 3-way valve on the front of the separator was leaking out the stem. It was remove, piping re-plumbed and pressure tested while I was onsite.",user_68,asset_429,41.474544,-90.6778637
11/27/2018,Separator,Temp Control System,Heater/Burner,,,,"burner was off on all 3 units, not sure why, maybe a reboot or possible high winds ",user_31,asset_854,48.2718734,-102.8688258
10/30/2017,Compressor,Compressor,Process Gas Supply,Ariel,,Trash,Compressor down on Lo 2nd Interstage Press. Appears to have gone down after I started gas lift compressor. Seems to be a normal thing. The gas lift pulls to much when starting it up causing the WH to loose some discharge.,user_141,asset_1264,48.1603937,-103.6172968
12/1/2017,Chemical System,Charging System,,,,,Dixon regulator ,user_156,asset_1625,48.19790528,-103.7897433
2/6/2018,Wellhead,Wellhead Piping,,,,,"worked on trying to break freeze in casing and checked tubing. Nothing stands out. Opened well back up,made some adjustments on compressor discharge valves. Will continue to watch",user_141,asset_1869,48.1470144,-103.6180489
9/4/2019,Separator,Choke Valve/Loop,,,,Freezing,"Arrived on location and found well still froze, trouble shot meth pump and found rupture dusk blown on pump. Ordered new prv for pump, left well open to atmosphere for awhile but the freeze never broke. ",user_18,asset_1843,,
4/27/2017,Automation,Other,Other,Other,Other,Other,Loss production ,user_88,asset_811,48.07945683,-103.669132
8/9/2018,Wellhead,Tubing,,,,,Shot fluid level down tubing and casing. Tubing is inconclusive due to broken co-rod and fish in hole. Casing fluid level 8809 from surface. 1484 feet of fluid in casing. ,user_15,asset_598,48.1470144,-103.6180489
6/18/2019,Automation,Antenna,,Bluewave,,Loose Connection,"cows have damaged antenna, has been pull off panel and laying on ground",user_144,asset_2019,48.1470144,-103.6180489
12/19/2017,Separator,Liquid Level Control,,,,,Apparently the condo dump level controller stuck open on the GC sep. and caused the LP sep to over pressure and esd the well. Reset interlock and rtp well. Stayed on location verifying everything working properly ,user_58,asset_876,48.41603018,-103.577396
4/20/2018,Pipeline/Piping,Valves,,,,End Of Design Life,2” Sales Linw Cyclonic was found to have a substantial leak from the the stem,user_150,asset_1008,,
12/16/2017,Pipeline/Piping,Pipe/Components,,,,Human Error,"30 HPG sensing line on the offskid recycle control valve on the discharge side not protected by a sensing line safety PSI device, allowing higher pressures than the 30 HPG is designed for to rupture the diaphragm and leak gas into the compressor building. OPS installed the safety PSI limiting device to stop this issue from happening and returned the off skid recycle line to service.",user_6,asset_140,36.2541889,-91.2478009
8/9/2018,Instrumentation,Communication Card,,,,,pulled graphs and shows communication error ,user_144,asset_1330,48.1470144,-103.6180489
2/23/2018,Gas Scrubber Separator,PSV,Body,,,Corrosion,"Started to vent well. While venting i started going through the separator to see what was using the most fuel gas Had to shut the glycol pump off to be able to listen. After shutting it off, i found that the rupture disc was leaking. SI well and tagged. Contacted TL and let him know about the issue. ",user_53,asset_836,40.5481548,-114.0112915
6/4/2018,Automation,RTU,Board,Schneider/Scadapack,Scadapack P4A,Weather,this is actually for a Yokogawa NFAP135 pulse input module. Unknown failure. WHAT IS THE POINT OF THE REQUIRED DROPDOWNS IF THEY CAN'T BE ACCURATE?,user_134,asset_1360,48.1470144,-103.6180489
6/4/2019,Gas Scrubber Separator,Liquid Dumps,Controller,Norriseal,,Improper Adjustment,Gauge was blowing gas.,user_94,asset_2099,48.1470144,-103.6180489
3/4/2019,Fuel Gas/Start Gas,Regulator,,,,,this well had high tanked in bad weather and was just now accessible for haul and to RTP,user_106,asset_1207,48.1470144,-103.6180489
2/7/2019,Separator,Choke Valve/Loop,,,,Freezing,Blowing and drifting snow preventing access to location coded to maintenance ,user_18,asset_1593,,
1/6/2019,Separator,Liquid Dumps,Controller,Norriseal,,Freezing,Water dumps froze.,user_94,asset_470,,
6/16/2019,Pipeline/Piping,Piping,Supply Line,,,Freezing,flowline froze,user_94,asset_1553,48.1470144,-103.6180489
10/25/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash, #80 shut in on consecutive non arrivals I went to location and found that the DVC wouldn't open up I cleared fuel gas and brought well back online I vented plunger to surface and lit SCC's B and C.,user_159,asset_648,48.1470144,-103.6180489
5/6/2017,Instrumentation,End Device,Ignitor Assembly,,,Passed Function Test,"-----Not able to select ""Ion Rod"" in sub component----- -----Not able to select ""pilot gas pressure"" in root cause----- 3. Monument 11-50 - SCC D no flame detect • Found Flame detect only getting up to 15% • Verified ion rod is set correctly • Found pilot gas pressure set at 30 PSI • Turned pressure down to 15 PSI • Started SCC in auto • Everything started up correctly ",user_92,asset_1276,40.5481548,-114.0112915
4/29/2019,Tanks/Pits,Flare/Combuster,,,,,"2 scc's out, probably due to wind, relit",user_31,asset_1167,43.56424,-91.351691
1/5/2017,,,,,,Other,Loss of production ,user_163,asset_1161,47.90780124,-103.4886461
12/5/2017,Tanks/Pits,Flare/Combuster,,,,,3 SCC’s out,user_50,asset_1800,48.40614951,-103.5803747
1/20/2017,Gas Scrubber,Shell,Body,Other,Other,Erosion,Plunger is worn out needs replaced,user_148,asset_1090,48.41302833,-103.5864879
10/18/2018,Separator,Choke Valve/Loop,,,,Freezing,"Checked equipment to ensure everything was in good working condition. Visual inspection of the equpment revealed the choke had a good freeze. Worked the freeze out of the choke and was able to achieve enough unit pressure to get the pumps and burners going. Waiting for the bath to get up to speed to help break the freeze within the coils. Once succesful, we were able to put the gas back to sales. Rates when we left were around 400mcf on a pinched choke.. Well is RTP",user_59,asset_327,43.252261,-115.0567324
8/7/2019,Gas Scrubber Separator,Fuel Gas Scrubber,Shell,,,,Gasket on top of scrubber,user_81,asset_327,48.2206396,-103.4646973
11/10/2017,Instrumentation,Controller,,,,,,user_60,asset_1020,48.1470144,-103.6180489
8/20/2019,Wellhead,Manual Valve,Stem/Seat,,,End Of Useful Life,Added stem packing to the upper master valve to stop the leak. ,user_118,asset_2071,48.20735209,-103.620963
12/27/2017,Tanks/Pits,Manway,Plate,,,Corrosion,Found leaking manway while performing LOTO on this location. Location will be shut in for other work and I will get a work order in to get manway replaced,user_119,asset_1523,48.1470144,-103.6180489
7/29/2018,Flare System,Flare Header,BMS,,,,"Issue: found SCC (A) down on the HMI Root Cause: Human Error, the (INT) had been cleared for some kind of work and the operator did not follow through checking the sight before moving on Fix: I was able to relight the SCC remotely ",user_170,asset_1437,48.1470144,-103.6180489
6/4/2017,Tanks/Pits,Liquid Level Control,,,,,"Verified that it was a false high/high tank alarm. It is, live read level showing .9 level. It is correct. Tapped on controller on tank, reset all interlocks on wells. Before i got them reset, pad shut back in on same thing. Contacted team lead, contacted Automation and they are on there way out to investigate. ",user_141,asset_201,48.1003415,-103.5854403
4/7/2018,Fuel Gas/Start Gas,Regulator,,,,,"Regulators full of fluid, need large drop out pot on end scc to help prevent this issue in future",user_35,asset_2237,48.18427664,-103.4264683
1/16/2018,Chemical System,Pump,Plunger,Texam,HBC1,Air Locked,"meth pump stalled, freezing plunger in cap, broke freeze, start pump. western pump not in pump selection",user_87,asset_807,40.7126799,-114.1193569
4/17/2017,Wellhead,Other,,Other,Other,Other,,user_35,asset_1392,48.34236868,-103.6048132
3/28/2018,Wellhead,Tubing,,,,,Was sent here to troubleshoot unit. No issues were found. Well was liquid loaded. Vent tubin to AGT to unload well. Got well unloaded and rtp,user_172,asset_749,,
5/22/2018,Flare System,Flare Header,BMS,,,,Issue: found SCC (B) down Root Cause: looks like the hi/gusty wind may have blown the pilot out Fix: relight and returned to service ,user_136,asset_1406,40.7126799,-114.1193569
10/3/2019,Separator,Dump Line,,,,Trash,"Pad shut in on glycol bath alarm / trended bath levels to make sure we did not have major leak , all looked good. Walked down location and found small glycol leak at the tanks , tightened fittings and stopped leak .Jumped unit back up and restarted bath and cycles .",user_10,asset_1191,40.5262342,-113.8824849
4/13/2018,Pipeline/Piping,Pipe/Components,,,,Human Error,"The 1"" insulated union on the glycol piping at the well head was found to be leaking - able to tighten the union to eliminate the leak.",user_150,asset_1536,48.1470144,-103.6180489
1/12/2018,Dehy,Meter (BP Check),,,,,Williams said there meter is working. Measurement is not reading to BP Please check the wondercard,user_163,asset_1330,48.1470144,-103.6180489
5/25/2017,Compressor - Gas Lift,Compressor,Suction Controller,Ariel,,Freezing,"Hydrate in injection control valve caused compressor to go down on high discharge pressure, valve was pinched back to control injection rate, injection rate was increased due to the 20 well freezing off in choke, more flow was forced over the 10 control valve causing the hydrate, also moved methanol injection from downstream of meter/ D4 control valve to uptream to help prevent hydrates",user_115,asset_2055,,
2/5/2019,Plunger System,Plunger,Plunger,PCS,,Not Optimized,plunger just worn out from use pads are loose,user_25,asset_1570,,
2/19/2019,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,"Checked location, drained scrubbers, verified water dump was going to pit and solar pumps running.",user_63,asset_580,,
11/24/2017,Instrumentation,Controller,,,,,kelvin burp setting failed and had to leave 40 well as a sacrificial well put back on cycles ,user_53,asset_2076,40.5481548,-114.0112915
1/27/2017,Tanks,Shell,Other,Other,Other,Other,Water tanks froze due to pump stall out. Changed pump and returned to service,user_152,asset_35,,
4/6/2017,Wellhead,Other,Other,Other,Other,Other,"Plunger stuck on rod, not arriving.",user_141,asset_289,48.224585,-103.8291059
12/22/2017,Separator,Dump Line,,,,Freezing,,user_126,asset_1948,,
12/28/2016,Gas Scrubber,,,,,,Choke leaking needs rebuilt ,user_148,asset_1573,48.16010169,-103.6172148
1/28/2017,Wellhead,Cyclonic Valve,Actuator,Other,Other,Freezing,Cyclonic actuator is burnt up need replaced. ,user_158,asset_514,48.06680875,-103.6700154
1/29/2018,Tanks/Pits,Piping,Load Line,,,Freezing,"4"" load line valve was leaking causing the load line to freeze and split open on the water tank.",user_150,asset_306,48.1470144,-103.6180489
5/22/2019,Separator Inlet Valve (XV),Choke Valve,Body,,,,"too small of or-phis plate, hydrating in tubing, need to let this well flow out for awhile. get casing psi down,",user_77,asset_1822,40.5262342,-113.8824849
3/12/2018,Fuel Gas/Start Gas,Regulator,,,,,No apparent cause determined (possibly burp settings removed). RTP'd well. ,user_141,asset_2010,48.1470144,-103.6180489
4/11/2019,Wellhead,Tubing,,,,,"master tubing valve needs replaced, crew greased valve but was still leaking ",user_28,asset_1611,48.1511744,-103.6275517
3/8/2019,Separator,Fuel Supply System, Big Joe Regulator,,,freeze,"supply comes directly from cold finger to big joe, line is not run through bath , this creates freezing in big joe even though bath is to temp",user_64,asset_1536,39.2506642,-92.4357879
9/2/2017,Compressor,Compressor (Intergral),Process Gas Supply,,,,"compressor went down on code #6 ""no left flow"" restarted.",user_71,asset_1574,48.3619066,-103.2129855
8/2/2018,Amine,Reflux Accumulator,Mist Pad,,,,Start date for lateral compression. IGNORE.,user_137,asset_1624,46.2321629,-100.6459029
1/29/2019,Heat Medium,Pump,Process Indicator,Texam,HBC1,Wear,"large graco pump had stalled out, pumping to wells 10, 70, &150. Bleed off and it took off again",user_31,asset_2120,43.56424,-91.351691
10/21/2018,Separator,Choke Valve/Loop,,,,Freezing,3 way valve froze,user_94,asset_350,,
12/18/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Desi and fuel gas scrubber of liquids daily routine auto dump may be a solution to issue ,user_109,asset_2224,48.181266,-103.6138866
5/14/2019,Pipeline/Piping,Piping,Discharge Line,,,Freezing,"WFS 1"" Dehy Line froze and broke Union so crew replaced it. 5-15-19",user_5,asset_849,46.2356189,-100.6010498
12/21/2017,Wellhead,Tubing,,,,,Well wscloaded due to natural flow unloaded and put into cycles ,user_58,asset_435,48.33963479,-103.6365873
2/26/2019,Fuel Gas/Start Gas,Regulator,,,,,"Pad was shut in for HighHigh Tank. One of the condo tanks where hot oiled yesterday causing this to happen. Level dropped low enough to clear alarm. Verified flowing into different tank. We are. Separators still had gas in them but ESDs wouldn't open. Found all 3 fuel gas scrubbers ball checked. Drained them all and got ball to drop. Checked all dumps, they are clear. Relit glycol bath burners. Opened all ESDs and started cycles on all wells. Road into location will need to be bladed for trucks to make it in. Believe Chrissy was going to redefer back to Maint.",user_55,asset_1650,,
5/15/2017,Separator,Choke Valve/Loop,,,,Corrosion,"replace 1/4"" by-pass valve on HI/LO",user_39,asset_1036,48.1470144,-103.6180489
2/1/2018,Fuel Gas/Start Gas,Regulator,,,,,Big joe froze do to burner went out I got it relit,user_0,asset_2094,48.1602799,-103.6173143
3/20/2019,Wellhead,Manual Valve,Ball,,,Freezing,"Blow down valve is frozen, could not get thaw tube on it to thaw. due to this there is still pressure on the piping from the well to the vessel. the bottom master is closed at the well head but the upper master is frozen, the tubing wings are both closed and tagged as is the ground valve , choke, and hi lo at the vessel.",user_22,asset_581,46.2356189,-100.6010498
12/11/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,Pulled to the edge of location and verified a PSV was abruptly Popping and reseating on the Compressor. Proceeded over to the compressor and verified it was the discharge PSV. Shut down the compressor and blew it down. Suspected freeze downstream or in the cooler which caused the event. Called ARCHROCK to come troubleshoot as the compressor should have killed itself. More to come after ARCHROCK investigates,user_59,asset_863,43.56424,-91.351691
5/1/2019,SWD System,Particle Filter,Shell,,,,Replace filters and restart pump due to dirty produced and pit water,user_55,asset_1633,,
1/20/2019,Gas Scrubber Separator,Mechanical Dump Valve,Float,Kimray,,Freezing,Issue: sight got shut in for a hi tank and the water dump line from the LP is froze to the pit Root Cause: the LP's dump line is temporary exposed iron to the pit and it from no volume and not being drained enough. I was able to verify there was pressure all the way to the scud at the pit and that's where i dug it out and found the scud isn't angled down wards into the pit. Fix: i was able to get my thaw tube on it and got the dump opened to the pit. then i started beaning up the well and bring more fluid that really warmed up the line. ,user_170,asset_2274,43.56424,-91.351691
1/19/2018,Separator,Choke Valve/Loop,,,,Freezing,,user_126,asset_1763,,
10/20/2019,Fuel Gas/Start Gas,Regulator,,,,,"got a callout for a high unit temp. It was false, bath is at 80ish degres. walked location down and made sure pumps and burners were all going. ",user_106,asset_1587,48.1470144,-103.6180489
11/21/2017,Tanks/Pits,Flare/Combuster,,,,,Relit SCC. Pilot was extinguished after losing fuel gas pressure from unit. RTP'd well. ,user_41,asset_907,48.19895406,-103.5970584
12/17/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Desi and fuel gas scrubber of liquids daily routine auto dump may be a solution to issue ,user_109,asset_1676,48.3264103,-103.6562705
1/6/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Vented well due to being loaded. Plunger arrived, RTP'd well, started cycles, and return to optimizer.",user_141,asset_1742,48.1470144,-103.6180489
3/1/2017,Instrumentation,Transmitter,3n1 MVT,Other,Other,Other,None,user_166,asset_920,48.05059873,-103.5251708
10/16/2017,Compressor,Cooler,,,,,Froze off in cooler due to temp swings broke freeze and returned to production.,user_51,asset_1707,40.5262342,-113.8824849
1/31/2018,Compressor,Compressor (Recip),Process Gas Supply,,,,"comp called out went down while I was at Dr23, it went down on high discharge, must have a lateral freeze again, I started it but the psi is climbing-nope went down again-high discharge watching the meter it looks like a lateral freeze again-shut the suction & blew everything down-",user_131,asset_1346,40.7126799,-114.1193569
4/19/2017,Sand Separator,Other,,Other,Other,Other,"bad seat, packing, and bonnet ",user_39,asset_1444,48.1582383,-103.6172162
9/22/2018,Pipeline/Piping,Pipe/Components,,,,Erosion Corrosion (Internal),MANUAL BLOCK VALVE UPSTREAM OF THE KIMRAY INLET VALVE AT THE COMPRESSOR IS LEAKING THROUGH. THE RECYCLE BLOCK VALVE CURRENTLY NEEDS SHUT TO GET SUCTION PRESSURES LOW ENOUGH TO START THE COMPRESSOR,user_34,asset_1049,43.56424,-91.351691
11/30/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Pilot plugged,user_86,asset_989,,
2/25/2018,Tanks/Pits,Flare/Combuster,,,,,2nd scc from east down on high temp. Restarted ,user_156,asset_1383,48.38856797,-103.8102135
5/17/2019,Surface Location,Lease Road,,,,Weather,We had a hole at the entrance cattle guard to location. Just wanted to recognize this driver for stopping and filling in the hole with dirt and gravel by hand.,user_55,asset_1489,,
9/25/2017,Flare System,Flare Knockout,Shell,,,,SCC pilot Burner extinguished by Rain last night- relit,user_138,asset_242,48.07944011,-103.4378306
10/15/2019,Separator Inlet Valve (XV),Pneumatic Control System,Hi/Lo Pressure Controller,,,,"Hi Lo had a bad Block and Bleed, I changed it out and separator is working great now, before it wouldn't maintain pressure or flow",user_22,asset_2011,46.2356189,-100.6010498
3/6/2018,Pipeline/Piping,Pipe/Components,,,,Human Error,"Surface piping sales line freeze. Approximately 100’ of salesline is above ground, line is shut in and depressured, heat trace running. Will check later in day",user_35,asset_611,48.19338093,-103.5418974
1/25/2017,Compressor,Compressor,Scrubber Level,Other,Other,Liquid Carryover,Water dumps froze off on seperators and cases liquid to carry over to compressor faster then the compressor dumps could keep up,user_148,asset_971,48.33997175,-103.6368724
3/20/2018,Instrumentation,Controller,,,,,Compressor went down on unit fire detection out of range. Automation worked on compressor. I do not know the root cause. Restarted compressor,user_53,asset_1426,40.7126799,-114.1193569
8/7/2019,Compressor - Gas Lift,Valves,,,,End Of Design Life,"2nd stage discharge valve on gas lift compressor cracked, replaced",user_64,asset_606,48.224585,-103.8291059
7/30/2018,Flare System,Flare Header,BMS,,,,"Issue: found SCC (A) down on the HMI Root Cause: Human Error, no (INT) so it got cleared but whom ever was working on the pad didn't finish before moving on Fix: relight remotely",user_170,asset_2224,48.2594106,-102.9008787
8/20/2018,Compressor,Compressor (Recip),Instrument Gas Supply,,,,"Got to site to do a compressor visit. Found pad and compressor down. All ESD's were shut and interlocked Found the fuel gas shut as well as the water dump line shut. Got all valves open in the proper position and then got units pressured up. Got compressor to start, allowed to warm up then got it loaded. Got all wells in there proper state. RTP'd compressor and pad ",user_56,asset_1996,48.1470144,-103.6180489
9/15/2019,Flare System,Flare Header,Instrumentation,,,,"Found pilots where lit, Durag not clicking. Reset Durags and got them working. SCCs returned to service.",user_55,asset_1921,,
11/29/2018,Wellhead,Manual Valve,Stem/Seat,,,Erosion,"ARROW PLUS WELLHEAD AND FLOW LINE FROZEN TRIED TO EQUALIZE WELL-- CANNOT DO SO BECAUSE THE CASING WING VALVE BLOWS GAS THROUGH THE STEM AREA BADLY ENOUGH TO SEE IT AS WELL AS HEAR IT. NO FLOW THROUGH THE SEPARATOR IS ALLOWING IT TO OVER HEAT JUST WITH THE PILOT LIGHT (SMALL SEPARATOR) 300 GALS METHANOL ORDERED 11/3/2018 STILL NOT DELIVERED SHUT IN NOW AT THE WELLHEAD, SALES LINE AND DUMP LINES. SEPARATOR DRAINED BURNERS OFF WM ENTERED TO GREASE MASTER VALVES AND INSTALL STEM PACKING",user_34,asset_1980,48.3619066,-103.2129855
5/31/2017,Automation,Battery,Battery,BP Branded,Model 112000,Electrical Short,"Cyclonic stuck in the open position, needs automation to trouble shoot",user_84,asset_2096,48.05326648,-103.4830705
9/7/2018,Compressor - Gas Lift,Engine,Fuel Gas Supply,Waukesha,,Weather,"Compressor was down on high AFR temps. Compressor building panels were removed earlier in the summer to keep temps down, they were installed again a few weeks ago. With day time temps in the high 70's low 80's, temps in the compressor building are to high and cause compressors to go down on high AFR temps. We will continue to have to start the compressor each day until panels are removed again or day time temps start to cool off more. Restarted and loaded compressor. ",user_15,asset_1833,48.2817029,-102.855422
5/21/2018,Gas Scrubber Separator,ESD,,,,,Mex flats 19-pad down on low unit pressure/ valve fault. jumped pad on and started wells with daily flowrate. ,user_71,asset_1418,48.1470144,-103.6180489
11/6/2018,Fuel Gas/Start Gas,Regulator,,,,,"Jam nut on big joe came loose causing stem to lift, shut off gas to hilow, fire went out, hung a dump, loss of unit psi",user_77,asset_597,48.01629617,-103.4932054
3/17/2018,Pumping Unit,Sensor,,,,,Rod pump down on no rpm,user_46,asset_2011,48.0614644,-104.8417043
1/5/2017,,,,,,,Location check and gauge,user_35,asset_1747,48.10774735,-103.4873519
7/22/2017,Pipeline/Piping,Valves,,,,End Of Design Life,5000# Sales line Cyclonic with side port failed due to trash brought up from well. Operator was able to close the valve but it would not hold pressure.,user_150,asset_1017,48.0568508,-104.907207
1/24/2018,Compressor,Compressor (Recip),Scrubber Level,,,,"Down on high scrubber level due to glycol pumps failing. WO was submitted, Maintenance team and crew replaced pumps 24JAN18. RTP'd compressor ",user_53,asset_1365,40.7126799,-114.1193569
2/21/2019,Surface Location,Well Pad,,,,Weather,Turn around on location is drifted in and cannot get a truck over to equipment to vent wells and thaw. Coded for plowing. ,user_15,asset_878,43.56424,-91.351691
4/3/2018,Flare System,Flare Header,Process Indicator,,,,1scc out and flare out most likely due to yesterday’s high winds 1 out 4 SCCs is good. I think definitely add the plates to these smaller producers on the scc definitely helped us this location has 3 to 4 down on a windy day ,user_58,asset_1574,48.4059346,-103.58102
2/27/2019,Surface Location,Lease Road,,,,Weather,CAN NOT ACCESS SITE DUE TO DRIFTED IN LEASE ROAD,user_34,asset_719,48.224585,-103.8291059
3/8/2017,Automation,Other,Other,Other,Other,Other,,user_87,asset_846,47.97248631,-103.4398369
5/30/2018,Wellhead,Tubing,,,,,Vented well ,user_86,asset_187,,
7/9/2019,Wellhead,Pipe/Components,,,,End Of Design Life, The wellhead insulation was removed in several areas. More insulation was applied. ,user_68,asset_748,48.1470144,-103.6180489
7/27/2017,Gas Scrubber Separator,Pneumatic Dump Valve,Packing,Kimray,,Wear/Tear,,user_53,asset_57,40.7126799,-114.1193569
11/6/2019,Separator,Choke Valve/Loop,,,,Trash,"Choke had stuck open causing well to load up. Closed ESD and checked choke operation. Vented well. Choke operating normal. Plunger arrived. Did not inspect, dual pad 6 weeks old. RTP'd well.",user_55,asset_2045,,
6/3/2019,SWD System,Coalescer/Filter,Elements,,,,changed west filter,user_31,asset_308,43.56424,-91.351691
10/7/2019,Instrumentation,Meter,Orifice Plate,Control Micro,4203DR,Recalibrated,Complete Scheduled Calibration within specification.,user_139,asset_1467,,
12/10/2017,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Well was down for non arrivals. Kicked well on and paused it open. Plunger arrived, returned well to production.",user_141,asset_2010,48.1470144,-103.6180489
1/29/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,Dump line split due to hydrate. Replaced line split and returned to service.,user_21,asset_1291,46.2356189,-100.6010498
4/27/2018,Recirc Pump,Pump,Instrumentation,Sunpumper,HBC1,Power Supply, 7. Creston Junction 44-6 - Methanol pump batteries dead • Removed 8 bad batteries • Installed 8 new batteries • Tested and verified good • Verified both pumps operate ,user_92,asset_722,36.2541889,-91.2478009
4/22/2017,Wellhead,Primary Choke,Other,Cameron,Other,Other,,user_51,asset_2250,48.1470144,-103.6180489
2/17/2019,Surface Location,Lease Road,,,,Weather,"Got to entrance of location and was not able to pulled up into location, had to walk in. Walked in and walked down the surface equipment. Found Produced water on the ground frozen. Troubleshoot were water was coming from, found water tank 761945 had a hole and was leaking water. Isolated tank took pictures and reported it to my TL Had to go back to my truck and get a tag. Attempted to flow 140 well but no flow through the choke. TBG has 1019psi CSG has 1031psi. Checked DVC and it has fuel pressure. will need automation to look into the DVC",user_56,asset_217,48.1082016,-103.9181984
5/28/2018,Compressor,Compressor (Intergral),Process Gas Supply,,,,CL 29-50 comp down on low suction RTP.,user_71,asset_1800,48.1470144,-103.6180489
11/12/2018,Instrumentation,Controller,,,,,Fisher DVC6000 had I/P and relay plugged with ice/paraffin ,user_12,asset_333,48.1470144,-103.6180489
12/4/2018,Heat Medium,Pump,Process Indicator,Texam,HBC1,Wear,"north 4 pack both glycol pumps had stalled out, bleed off and started pumps",user_31,asset_133,43.252261,-115.0567324
4/8/2017,Instrumentation,Transmitter,3n1 MVT,Other,Other,Other,,user_99,asset_920,48.2706656,-102.8873229
1/15/2019,Fuel Gas/Start Gas,Regulator,,,,,"both baths were down and at 40 degrees. When I got to location there was a tag hanging in the cabinet that the ESD supply gas was shut off due to dump line freezes and vessel freezes. Got baths going and one well open to supply the units. Solar glycol pumps are running. Could not drain any of the dumps, condo or water and could not drain scrubbers, fuelgas system was fairly dry though. Not sure why the baths were out, they lit with no issues and are coming up to temp. Need to let sit with heat on overnite and re-address tomorrow and see if dump are clear and if not take further measures to get them cleared. At lest 3 of the Vessels appear to be frozen inside. Looks like this pad has been down for a couple of days in extremely cold temps.",user_106,asset_736,48.0881279,-104.0266781
11/28/2017,Compressor,Compressor,Suction Controller,Ajax,,Freezing,"Compressor down. Dispatch to troubleshoot the compressor. Restart, load, and RTP Wells. Compressor went down at 05:15. Dispatch to location. Read controller and find compressor down on low suction. Pull graphs to troubleshoot root cause. No indication of issue initially. 20, 50, and 80 wells free flowing to sales at 85 psi suction. 150 shut in for pressure build awaiting criteria for next cycle. Suction kill set at 65 psi per Archrock design. Possible freeze across suction controller. Restart and load compressor. All wells make their first plunger arrival. Adjust recycle to call for gas sooner since wells are pulled close to the low suction kill. This will also decrease the DP across the suction controller helping to mitigate the suspected freeze. Adjust controller to 30 psi bringing suction pressure from 75-85 psi to 85-95 psi. Optimizer to monitor cycle settings. I will monitor suction pressure with recycle adjustment and make another adjustment if needed. Root cause low differential between suction pressure and suction low kill set point due to low flowing tbg pressures as wells have pulled down. Freeze caused by possible JT across controller. Freeze could not be verified as it was broke upon arrival so statement remains suspected and possible. ",user_75,asset_6,,
3/7/2019,Separator,Manual Drain Valves,Ball/Seat,,,Corrosion,"Blow down line leaking, lost 5 PSI over ten minute test, MAINT to replace cyclonic valve or install block valve. WM written and well coded. ",user_54,asset_2196,39.2506642,-92.4357879
6/10/2019,Tanks/Pits,Valves,,,,End Of Design Life,The condo tank inner valve was leaking by. The load line was removed and a new valve was installed on the existing valve.,user_68,asset_986,48.265488,-102.8737184
6/4/2018,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,Issue: well shut in on low unit pressure Root Cause: I checked and verified the dumps had fluid in them to prove its not a leaking dump. Pads been turned over to summer use so there isn't any thing using up fuel gas. looks like the wells are trying to bring up to be of fluid slugs and using up all the unit pressure to try and get rid of the fluid and then shut in on low unit pressure Fix: checked the dumps and made sure everything was working okay and then turned the well back on restarted the plunger cycles ,user_136,asset_486,48.259471,-102.9009493
4/15/2019,Flare System,Flare Header,Process Indicator,,,,re-lit SCC's abutec seem to have issues staying lit,user_63,asset_1421,,
3/9/2019,Separator,Liquid Dumps,Controller,Nalco,,Freezing,surface piping freeze issues due to cold weather,user_17,asset_1844,,
3/19/2019,Separator,Temp Control System,Thermostat,,,,we installed blue board insulation inside of the separator to keep heat and prevent freeze on lines,user_28,asset_1323,48.1603562,-103.6176013
4/29/2018,Flare System,Flare Header,Buckle Pin,,,,Flare out relit and returned to service ,user_58,asset_580,48.36732076,-103.5276142
6/15/2017,Compressor,Compressor,Process Gas Supply,Ariel,,Vibration,"Not vibration, it went down on low 1st stage pressure.",user_103,asset_1280,48.32774867,-103.6572096
9/22/2018,Compressor,Compressor (Recip),Level Controller,,,,"Checked control panel, compressor was down on low oil level. Checked oil level, it was full. Started compressor to warm it up and saw oil level drop down below low level in site glass. Contacted JW it seems the auto oil level controller was not allowing oil in to fill it. JW came to site, found that the float inside the auto level controller was out of adjustment so it was not allowing it to fill the compressor. JW pulled it apart to make sure it was clean, reset the level controller and low oil kill level float. Tested switch and started compressor. Watched oil level, auto level controller now working and keeping level were it should be.",user_15,asset_1383,48.2816738,-102.8553507
9/19/2018,Separator,Choke Valve/Loop,,,,Corrosion,"YOKOGAWA PAD- AUTO CHOKE STEM BENT AND LOCKED UP THE CHOKE 100% OPEN, LOADING WELL SHUT IN AT THE INLET VALVE NOW, WAITING FOR REPAIRS",user_34,asset_1864,48.224585,-103.8291059
4/30/2018,Wellhead,Tubing,,,,,"CG 25-130 vented once for an hour then flowed in, took 29 min and got an arrival. L.R. still didn’t look good, vented again and got an arrival. Needs someone who can spend the day venting it needs about 6 hours or a swab ",user_71,asset_293,48.1470144,-103.6180489
1/31/2018,Instrumentation,Controller,,,,,"Kelvin failed. Kelvin let all wells be on their off cycle at the same time, resulting in the compressor running on the off skid recycle, ending in compressor going down on low discharge. need kelvin to optimize this pad to where we don't have all wells off at the same time. drained compressor and scrubbers, restarted compressor warmed compressor and RTP'd well ",user_53,asset_1500,40.7126799,-114.1193569
12/24/2018,Tanks/Pits,Flare/Combuster,,,,fuel gas freeze,"regulator to one scc froze, thawed out and drained liquid",user_31,asset_1423,43.56424,-91.351691
12/22/2016,Automation,,,,,Other,Tristar controller faulted out. Not able to repair. ,user_92,asset_1128,47.97971248,-103.4578978
10/2/2019,Wellhead,Cyclonic Valve,Actuator,,,Corrosion,Removed and replaced cyclonic actuator and verified operations with optimizer,user_169,asset_2166,46.2356189,-100.6010498
12/10/2017,Instrumentation,Controller,,,,,This is for a Fisher DVC 6200. Two screws fell out of the feedback sensor and it fell away from the DVC.,user_134,asset_1423,48.1603113,-103.6174295
1/10/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,Salesline was frozen coming out of the separator. Opened salesline valves to atmosphere. Turned up burner temperature and equalized heat trace from glycol pump. ,user_68,asset_1932,47.95061772,-103.421215
1/5/2019,Separator,Liquid Dumps,Regulator,Fisher,,Freezing,water dump freeze heater main fuel gas freeze vent and unload tubing scrubber pot freeze comp. down need heater to thaw all freezes thawed unit rtp,user_57,asset_1103,48.0532244,-104.8722285
3/19/2018,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,"Knock out pots, to flare, fuel gas to flare, line heater, and line heater scrubber had liquids. Wells flowing over 110deg carries liquids through the gas stream which drop out in these pots and scrubbers. ",user_58,asset_876,48.41611186,-103.5770557
5/14/2019,Separator,Dump Line,,,,Trash,"Found unit ESD on low sep pressure. opened up cabinet and found the condo dump stuck open, throttled the dump control and was stiff. Worked back and fourth and freed it up, sprayed down with some liquid wrench and worked open/close again. everything seems good, started a cycle and watched levels, condo was set to low was dumping past bottom sight glass, set to stop dumping mid lower sight glass. ",user_25,asset_573,,
4/11/2018,Plunger System,Plunger,Plunger,Well Master,,Corrosion,Replace plunger to improve production/ Request from engineering/ Installed new viper,user_100,asset_431,48.1470144,-103.6180489
3/28/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Well was on arrow dispatch to inspect plunger, it had missed a few arrivals over the last couple weeks. Inspected plunger as requested, looked into cycles to see how they were set up. Found well is running off of time and not load ratio. LR is set for 1.00 and the minimum off time is set for 110 minutes. Well kicks on to flow after 110 minutes no matter how the tubing and casing pressure are. Contacted optimizer to review cycles to get well to be more consistent on getting arrivals. Root cause is well is not optimized.",user_62,asset_1000,48.1604917,-103.6180517
5/8/2019,Tanks/Pits,Tank Level,Sonar,,,Weather,"swapped 17' condo tank # 761603, 4 scc's out, cleaned 2 pilots, relit scc's",user_31,asset_365,43.56424,-91.351691
1/8/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,Well not able to sustain optimal off times for the type of plunger installed. OPS removed and installed a spiral bar plunger to better fit the off time cycles of the well. OPT notified and is adjusting cycles.,user_6,asset_1401,36.2541889,-91.2478009
1/18/2017,Gas Scrubber,,,,,,"All water dumps on location frozen, heat on and pumps running. Thawing with truck ",user_87,asset_1586,47.93868247,-103.5041473
4/3/2017,Heater Treater,Mechanical Dump Valve,Seat/Ball/Piston,Other,Other,Erosion,Replaced trim set. Lost production from leaking to tank,user_156,asset_74,48.22053185,-103.6444842
1/23/2019,Separator,Dump Line,,,,Freezing,"walked down location and found that the dehy was tagged and shut in because of a split dump line on the cabinet inside the dehy that needed fixed along with a tag that indicated that the dehy was down until production equipment got the water dumps thawed out. While I was inspecting the dehy dump line I also notice a flagged hammer union on the dehy water dump downstream of the check valve that was frozen and split. I believe this hammer union would be considered our equipment to fix . I looked at passed surface failures on this location to try and root cause the problem . I found that there had been a solar glycol pump that had been fixed on this location a few days ago but was turned off because the unit that was connected to this pump was shut in. This is a two well brown field location will two t-packs and two solar glycol pumps.The 140 well is shut in and tagged but with nothing written on the tagged, after getting more information it looks like the 140 well is a eng. well that has been a long term shut in well. After tracing the glycol lines on location it looks like the glycol pumps for the tanks are connected to the 140 well which is not in service so the tanks are not getting any heat which would cause tanks and dumps to freeze. I think we need to connect the second solar glycol pump to the 160 bath and tanks so that the whole location will get heat trace from the 160 bath.This would allow the tanks to get heat trace with the 160 well running only. I contacted the dehy tech about getting his equipment fixed and running he should have his end fixed in the next few days. I will code his to maintenance to fixed hammer union on the dehy water dump passed the check valve and to connected glycol heat trace to the 160 bath or we can jump gas from 160 unit to the 140 unit with approval from team lead. Could not reach equipment with thaw tube because of drifts but did get the bath going on the 160 well to start warming the unit and isolated water dump because of split hammer union at the dehy , water dump line is frozen. We may need a steamer to get the lines thawed out.",user_10,asset_165,40.5262342,-113.8824849
7/20/2017,Automation,RTU,Relay,Emerson,Bristol 3310,Wear,"The information on the page is useless. There is no correct items to select. The I2P is a fisher and should be under Automation; Controller, DVC I2P and/or Low Bleed Relay for the surface failure.",user_162,asset_18,36.2541889,-91.2478009
4/10/2019,Chemical System,Pump,Process Indicator,Sunpumper,HBC1,Air Locked,"4/10/2019 Burner out on the 140 well separator. Took pilot apart and cleaned out and adjusted position, it was partly plugged. Cleaned out and relit. Center methanol pump wasn't pumping again, bleed off and it started right away, the other 2 stayed pumping all night. Bleed off 110 flowline and broke freeze and RTP well.",user_31,asset_2040,43.56424,-91.351691
1/16/2019,Separator,Dump Line,,,,Freezing,"Found well shut in. Dump lines are frozen, both condo and water. Bath heat is on. Solar glycol pump not working and switched to off. ESD is also stuck in travel. Have steamers coming to thaw water dump lines, will have them thaw out the ESD. ",user_55,asset_1542,,
1/22/2018,Chemical System,Pump,Plunger,Texam,HBC1,Wear,Small graco pump on new fuel gas was shut off. Started pump and it didn’t start. Bleed off exhaust and pump started. Struggling with too much exhaust back pressure ,user_156,asset_1168,48.20716933,-103.6222294
7/31/2019,Automation,RTU,CPU,Control Wave,CWM,Weather,Replaced pad cpu,user_16,asset_140,,
3/29/2018,Tanks/Pits,Flare/Combuster,,,,,SCC was out. Pilot was blowing dry gas leaving no immediate indication of root cause. Left to assume the wind caught it just right and blew out the pilot. Relit and returned to service.,user_50,asset_2074,48.1470144,-103.6180489
10/2/2019,Separator,Fuel Supply System,Regulator,,,wear,"Pad went down on low unit pressure,this well will need a downstream valve installed to keep the pad up when running the glycol baths and pumps running. Work order was already turned in but i wrote another work order for the downstream valve. Pressured up units and functioned tested chokes and rtp'd. found that the choke on the 40 well was not responding, removed and cleaned I/P and put well back into service and function tested. Restarted all scc's and baths on location did not start pumps because of fuel gas issue.",user_10,asset_1082,40.5262342,-113.8824849
1/16/2018,Compressor,Cooler,,,,,"Compressor went down on possible cooler hydrate, louvers adjusted and compressor RTP'd",user_24,asset_609,48.1470144,-103.6180489
1/12/2018,Tanks/Pits,Flare/Combuster,,,,,"Relit SCC ""B"". Pilot was extinguished after losing fuel gas supply pressure. ",user_41,asset_21,48.18124876,-103.6145201
12/16/2018,Separator,Liquid Dumps,Seat/Ball/Piston,Norriseal,,Erosion,Dump trim worn out due to use and over tightening on bonnet spring. If dumps continue to leak OPS suggests replacing bonnet.,user_54,asset_118,46.2356189,-100.6010498
10/28/2019,Separator,Fuel Supply System, Big Joe Regulator,Fisher controls,Type 912,freeze,Fire was out in unit big joe frosted up,user_135,asset_1822,46.2356189,-100.6010498
10/23/2017,Gas Scrubber Separator,Pneumatic Dump Valve,Controller,Invalco,,Out Of Adjustment,unit lost pressure and well went down,user_179,asset_649,40.5262342,-113.8824849
10/10/2017,Fuel Gas/Start Gas,Regulator,,,,,"going through the HMI found the whole pad down, no unit PSI, all wells shut in on cycles with the cold weather burners & pumps going drained it might want to think about sacrificial well RTP wells, 25,70.110.100.60.relit baths & SCC's",user_131,asset_1423,40.5960545,-113.9323891
10/4/2018,Flare System,Flare Header,BMS,,,,Relight 2 SCCs that where out due to rain and wind,user_55,asset_2168,,
2/22/2018,Tanks/Pits,Tank Level,Sensing Cable,,,Weather,Adjusted starting range and created a new false echo suppression. ,user_65,asset_838,48.16875545,-103.4445733
1/14/2019,Plunger System,Plunger,Plunger,PCS,,No Liquid,Plunger worn. Replaced,user_153,asset_886,48.31108192,-103.6443885
4/21/2017,Sand Separator,Other,,Other,Other,Other,no sales,user_39,asset_1723,48.1498374,-103.6213567
1/2/2018,Compressor - Gas Lift,Compressor,Instrument Gas Supply,Ajax,,Freezing,Pull graphs to troubleshoot remotely before dispatching to location. Compressor discharge at 1000 psi. Compressor discharge recycle set at 998 psi with kill at 1100 psi. Csg pressures well below this value on both the 120 and 150 wells. Suspected freeze between compressor discharge and injection point. Check injection valve position and meter reading. Valves indicate 100% open with no injection rate. Suspect a fuel supply line at injection valve to be froze. Dispatch to location. Confirm freeze in fuel supply line. 120 and 150 are farthest downstream on fuel gas supply line from take off point at compressor. 120 is the farthest. Break freeze and resume injecting. Discharge recycle closes as set and wells begin accepting injection rate. Thaw and drain desi. Approximately 1-2’ of fluid in desi. Adjust separator A bath up at T12. Current bath temperature 74 degrees. Ambient air temp -7. Tanks temperatures good. Wellhead temperatures 60 degrees. Checked with laser. ,user_75,asset_794,,
2/26/2019,Separator,Temp Control System,Heater/Burner,,,,well was esd on vale misalignment.fuel gas to esd was froze. thawed out fuel gas and got esd open.DVC was also froze. thawed it out and function tested choke.both dumps are open to tanks.bath was out on A four pack.relit. drained dezy and scrubbers,user_120,asset_1975,43.56424,-91.351691
3/20/2018,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,"Knock out pots, to flare, fuel gas to flare, line heater, and line heater scrubber had liquids. Wells flowing over 110deg carries liquids through the gas stream which drop out in these pots and scrubbers.",user_58,asset_298,48.41647685,-103.5723041
10/30/2019,Separator,Choke Valve/Loop,,,,Freezing,"Found all well down and frozen , looks like pad was down overnight . Thawed out front end of the unit and vented wells to unload so that the unit would stay up and run. After getting all the equipment up and run I could flow the well because the automated valve on the dehy would not stay open. Contacted dehy tech to troubleshoot problem. Jumped all unit on and started glycol bath and pumps to prevent the unit from freezing until dehy problem can get fix.",user_10,asset_28,40.5262342,-113.8824849
6/4/2019,Plunger System,Wellhead Piping,,,,,The lubricator had a leak on the flange threads and needed to be replaced. A new lubricator and flow path valves were installed on the wellhead.,user_68,asset_1468,48.1470144,-103.6180489
7/24/2019,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"Rtp well after high tank. Attempted to vent plunger in, was unsuccessful. I'm thinking the plunger has been removed just never entered. Hasn't gotten an arrival in forever and there is a bar laying on the steps.well rtp",user_120,asset_1197,,
2/24/2018,Gas Scrubber Separator,ESD,,,,,Issue: found well was down on the HMI Root Cause: found the flame arrester was covered in snow and snuffed out the burner. After that happened the dumps froze and the unit flooded until it took out the fuel gas then sat there and froze up. Fix: I dug out the burner rigged up a jumper line got the bath relight and started the unit warming back up. if i get a chance to stop buy i will or come back tomorrow and see if i can turn the well back on after everything has thawed out,user_136,asset_297,48.2594705,-102.9010554
4/22/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,wear,Lost unit pressure. Wells shut in. Compressor down because 10&20 wells loaded ,user_156,asset_1124,48.32436607,-103.6009663
1/14/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,Piping Froze due to extremely Low Temperatures,user_139,asset_1361,,
5/13/2019,Sales Valve (PV),Sales Valve,Body,Valvcon,,End Of Useful Life,"The 2"" salesline cyclonic valve was leaking out the stem. The valve was replaced.",user_68,asset_1933,48.224585,-103.8291059
6/6/2019,Separator,Choke Valve,Body,,,,The choke stem was seized in the body and the valve was repaired.,user_68,asset_345,43.56424,-91.351691
7/19/2019,Automation,Battery,Battery,Universal,Model 112000,End Of Useful Life,Completed by Wyolectric,user_108,asset_281,,
10/1/2019,Plunger System,Plunger,Plunger,IPS,,Corrosion,"Plunger vent to inspect plunger, multiple missed arrivals. 500 PSI, Duration 12 minutes. Replaced Plunger (2 3/8 Dual Pad), with (2 3/8 Dual Pad). Returned to cycles good pressures, hopefully will kick off and go. ",user_2,asset_1364,49.5499678,-102.9290839
4/17/2018,Fuel Gas/Start Gas,Regulator,,,,,Pilot for main burner blew out. Root cause: wind. Manually relit,user_107,asset_1066,,
5/8/2019,Separator,Choke Valve/Loop,,,,Freezing,Found bath A down on this pad and well frozen in the flow line between wellhead and choke. Thawed choke and broke flowline freeze. Big joe was frozen / thawed and got burner going again . Rtp'd well.,user_10,asset_483,40.5262342,-113.8824849
1/5/2018,Sales Valve (PV),Sales Valve,Body,Automax,,Freezing,Froze in sales line cyclonic. Thawed and RTP ,user_156,asset_1758,48.23374458,-103.6138418
3/14/2018,Separator,Liquid Dumps,Controller,Fisher,,Improper Adjustment,condo dump running towards top of upper site glass adjusted to dump between mid and lower site glass,user_115,asset_1793,,
11/7/2019,Separator,Choke Valve/Loop,,,,Freezing,"Found well shut in on high line pressure, walked down location and could find no reason why, kicked well on and verified plunger Arrival.",user_18,asset_1793,,
1/27/2018,Flare System,Flare Header,Process Indicator,,,,,user_48,asset_1927,48.17177214,-103.5941546
4/21/2017,Wellhead,ESD Valve,Other,Other,Other,Other,,user_126,asset_1423,,
7/14/2018,Plunger System,Plunger,Catcher,PCS,,Wiring Shorts,"Plunger catch was very stiff. Greased catch, ran it in and out a couple times, working much smoother now.",user_62,asset_1404,43.252261,-115.0567324
4/22/2018,Chemical System,Piping,Discharge Line,,,Debris,Pump strokes until it pressures up and stop. Either pump is failing or there is an obstruction in the glycol circulation lines.,user_6,asset_2056,36.2541889,-91.2478009
9/29/2017,Separator,Temp Control System,Fuel Gas Supply,,,,"Found main burner pressure was set to 20 PSI, making the burner run way to hard. Adjusted burner down to 7 PSI.",user_62,asset_244,48.1470144,-103.6180489
9/7/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Electrical Short,"Issue: Williams had a power issue and knocked down all there compression causing line pressure to rise Root Cause: found the comp was down on hi discharge pressure and line pressure was 477psi with the suction scrubber PSV set point at 500psi Fix: i shut the suction, discharge, blew comp down and tagged out ",user_170,asset_1049,49.5499678,-102.9290839
7/29/2018,Instrumentation,End Device,Thermocouple,,,Installation Design,Issue: called out SCC down alarm Root Cause: found the SCC is running but the wind is able to move the pilot around enough it looses contact with the thermocouple and trips the callout Fix: adjusted the fuel air mixture and placement of the thermocouple to see if that will help fix it from calling out,user_170,asset_1274,48.1470144,-103.6180489
1/15/2019,Gas Scrubber Separator,Pneumatic Dump Valve,Float,Fisher,,Freezing,Dispatched to well due to its deferment. Got to location and found the hi low frosted over. Unit had 14PSI in it. Bath was cold. Started thawing on the hi low. got all the frost off of it and then started to pressurize the unit. Started the burner and heat trace. Found both dump displacers froze. Shut both valves inside the cabinet and flagged with orange tape. Contacted OPT to put a SI command on the cyclonic Continued to thaw on flow line because i could only get 94PSI into the unit. ,user_56,asset_535,48.1131168,-103.83464
10/18/2018,Heater Treater,Burner,BMS,,,Loss Of Fuel Gas,"Found heater treater pilot had gone out. Unknown reason why, we had pilot gas and fuel gas when I arrived on site. Lit pilot and opened main burner. Opened and closed main burner valve to make sure it was not snuffing pilot out, and it was not. ",user_15,asset_1383,48.2814851,-102.8554282
11/10/2016,Tanks,Valving/Swedges,Body,Other,Other,Corrosion,"4"" Tee on load line corroded causing a pin hole. Replaced tee and inner 4"" load line valve. ",user_8,asset_902,48.21693555,-103.2860364
12/2/2018,Heat Medium,Pump,Plunger,Texam,HBC1,Wear,"large graco pump is blowing gas through, probably a bad diaphragm ",user_31,asset_1122,43.252261,-115.0567324
10/14/2017,Tanks/Pits,Piping,Connections,,,Corrosion,Permanent glycol coils in 2 water tanks failed due to external corrosion. The tanks both have internal coating and anodes,user_150,asset_1974,,
5/22/2018,Wellhead,Cyclonic Valve,Gate/Seat,,,Corrosion,6250 PSI Blowdown Cyclonic found leaking from stem,user_150,asset_445,,
2/12/2019,Separator,Choke Valve/Loop,,,,Freezing,well frozen just before the temp. divert valve on the flowline past the esd . Thawed and rtp'd,user_10,asset_435,40.5262342,-113.8824849
7/12/2017,Compressor - Gas Lift,Engine,Back Pressure Valve,Cummins,,Vibration,shut in on high discharge cleared and restarted,user_176,asset_1366,40.5481548,-114.0112915
10/31/2017,Compressor - Gas Lift,Compressor,Scrubber Level,Ariel,,Freezing,Compressor call out found that the compressor had gone down on 1 stage scrubber level. Blew scrubbers down and restarted compressor . The insulation on the scrubbers had been removed to install new heat trace on the compressor.,user_100,asset_1366,48.1469338,-103.6177737
11/10/2017,Separator,Temp Control System,Fuel Gas Supply,,,,"Find 4-PAC unit down on low unit. Zero vessel pressure. SCC's down as well. Jump gas to unit. Begin returning well to production after breaking freeze in fuel gas header. Could not break freeze with first well jumped. Had to move jumper to another well to break freeze. All wells were in an off cycle at same time with pumps, burners and SCC's running dropped pressure enough to trigger ESD's. Buy back schedule dated 10/6/2017 shows buy back meter installation scheduled for the week of 11/13/2017. Return well to operation. Continue with other wells on pad. Relight SCC's and bath. Drain desi of minimal fluid. Longer wrench time due to having to break fuel gas freeze. ",user_75,asset_1719,,
12/10/2017,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"Vented well due to being loaded. Plunger arrived, RTP'd well, started cycles, and return to optimizer",user_141,asset_1142,48.1470144,-103.6180489
12/11/2017,Tanks/Pits,Temp Control System,Heater/Burner,,,,glycol pump stalled got pump started again and confirmed heat trace working ,user_11,asset_1006,48.1470144,-103.6180489
8/31/2017,Pipeline/Piping,Pipe/Components,,,,End Of Design Life,Repaired and retapped pipe insulation. ,user_41,asset_392,48.20731455,-103.5435757
6/7/2018,Compressor,Engine (Gas),,,,, Compressor down on low discharge due to A well getting well work done pressure I went to location cleared alarm restarted and put back online.,user_51,asset_576,48.1470144,-103.6180489
2/16/2018,Sales Valve (PV),Pneumatic Control System (3Pgra),,,,,Jumped separator back on. Found sales line DVC fuel supply disconnected. Reinstalled line and RTP'd well,user_141,asset_291,48.1470144,-103.6180489
11/8/2017,Compressor,Compressor,Instrument Gas Supply,Ariel,,Freezing,Compressor down due to frozen fuel gas lines and the big Joe's. Heat trace is going but seems like pump is not big enough to handle the compressor and the dehy at the same time. Loosing temperature before arriving to lines that need heated. Apply heat from truck with hoses to break freeze and RTP compressor,user_109,asset_1675,48.3877196,-103.8411233
1/16/2018,Fuel Gas/Start Gas,Regulator,,,,,"DVC to choke frozen, had to thaw poly line and scrubber, very little fluid but enough freezing to constrict gas flow. Thawed for 25 minutes and was able to bring back to operation. Cotinuous issue on this well",user_88,asset_613,48.2582459,-102.9043489
4/21/2018,Tanks/Pits,Piping,Connections,,,Connections,Issue: request to look at load line and try to fix bleed Root Cause: the treads on bleed broke off in the color. It looks very much home made and not sure why the bleed was there. there is a bleed on the main line that should be used to drain the line Fix: the hose coupler just needs to be pulled and then remove the swede out of the valve put the coupler in the valve and pull the tank,user_136,asset_263,48.1470144,-103.6180489
12/12/2017,Gas Scrubber Separator,Dump Line,,,,Freezing,"Desi dryer dump line was frozen. Root cause, crew that hooked up buyback meter shut return line of glycol pump. Opened up all valves and validated warm glycol through out the entire system. ",user_62,asset_1168,48.1470144,-103.6180489
3/11/2018,Automation,Antenna,,Bluewave,,Electrical Short,Arrow Failure. Dispatched to well incorrectly. Well is making good volumes with good flow and psi trends. No need to check this well,user_107,asset_641,,
10/24/2017,Compressor - Gas Lift,Engine,Cooler,Cummins,,Overheat,"Gas lift compressor down on Hi Discharge 1st Interstage Temperature. Opened louver up a little, should take care of temperature. Also, will kick methanol pump on discharge of compressor to try to compensate for opening louvers more. Is this one that maybe we could get switched over to T-12 controlled louvers?",user_141,asset_1264,40.5262342,-113.8824849
2/23/2018,Compressor,Compressor,Suction Controller,Ariel,,Freezing,"Issue: called out compressor down alarm Root Cause: went down on hi suction pressure. I found the suction controller was freezing up from the changing in ambient temp along with i found one side door open causing a cold side draft Fix: thawed out the suction controller, drained all the lines and returned compressor to service ",user_136,asset_879,48.2629356,-102.8996131
7/12/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_1489,48.1470144,-103.6180489
9/11/2019,Separator,ESD Valve,Gate/Seat,,,Corrosion,Hi- low replaced and returned to service ready to Ops,user_21,asset_672,46.2356189,-100.6010498
7/7/2017,Tanks/Pits,Thief Hatch/PVRV,Body,Enardo,,Corrosion,4 ENARDO 660 L thief hatch showed signs of corrosion on produced water tanks and were replaced,user_112,asset_365,48.0588754,-103.6378507
12/9/2016,,,,,,,"Fire blew out, unit and dumps froze solid, jumper was put on, temped up unit and thawed freezes, put unit back on",user_35,asset_2254,48.00609037,-103.6980491
3/31/2017,Wellhead,Other,,Other,Other,Other,Lost in production,user_130,asset_1807,48.224585,-103.8291059
7/18/2019,Separator,PSV,Body,,,Incorrect Set Point,"contacted team lead and verified bssv and bar stock plunger had been installed in well.met crew onsite to perform pressure test on wellhead reconfigure. found 6000psi no shock leaking out of weep hole. insulated 1/2 railroad union for tubing transmitter leaking and check valve on tubing methanol leaking.as far as the reconfigured piping i found no leaks and released crew.contacted team lead on leaking equipment and he brought out new parts out. we replaced the union,no shock and check valve.i vented in the plunger with starting pressures 710 tubing and 2300 casing. got plunger to come in and let it fall for approximately 60 minutes. i ended up venting plunger in three times, ending pressures 1200 tubing 1800 casing. well is still loaded due to kill fluid from new tubing install.while venting in plunger TL and i walked down separator. we found MAWP for vessel at 1440, PSV set at 720 and rupture disc at 800 psi. team lead requested we raise both psv and rupture disc set points to 1000 and 1200psi. we contacted avery with engineering to get his approval.he approved. i perfomed LOTO and removed psv, installed new psv with 1000psi set point. i then removed ruptures disc and found four 800psi disc were installed.i stopped the job and contacted team lead on my findings. i ended up having to leave the well shut in because the rupture disc i had did not match up to the union.i reinstalled one 800psi rupture disc and tagged out location. will return to site tomorrow with more parts.",user_120,asset_1031,38.4425988,-95.5406131
1/21/2018,Tanks/Pits,Flare/Combuster,,,,,Pilot out. Relit,user_156,asset_1927,48.17181476,-103.5941489
10/4/2017,Compressor - Gas Lift,Compressor,Panel,Ariel,,Freezing,Compressor went down on low suction pressure on the panel code could not find a freeze in the suction line and suction control valve seems to be working properly . Compressor started up without a problem. I will contact Williams to find out if they did a plate change on the buy back meter without opening the bypass valve which would have taken the compressor down.,user_100,asset_1873,48.1470144,-103.6180489
10/26/2019,Separator,Temp Control System,Fuel Gas Supply,,,,"glycol pump fittings broken and leaking gas when you turn pump on, got replaced parts and replaced all fittings and poly fuel gas line to the glycol pump.Function tested and restarted pump.",user_10,asset_315,40.5262342,-113.8824849
1/1/2019,Heat Medium,Furnace,Process Indicator,,,,"burners out, fuel gas lines full of liquid and frozen",user_31,asset_1761,48.1475232,-103.6200096
4/5/2017,Sand Separator,Other,,Other,Other,Other,cyclonic valve needs replace do to leak from stem,user_39,asset_1757,48.224585,-103.8291059
12/16/2018,Instrumentation,End Device,Durag,,,End Of Useful Life,"Issue: while on location performing my walk around i found the burner out and bath 52deg Root Cause: Human Error, The pilot bypass is open and the burner runs in manual do to the instability of the durag to keep working and constantly dropping the pilot flame and then shutting in the burner. some one closed the pilot bypass turned the burner on in auto and didn't recheck it to make sure it stayed running Fix: opened bypass relight bath and left running in MAN mode for reliability ",user_170,asset_1050,43.56424,-91.351691
4/9/2018,Heat Medium,Pump,Process Indicator,Texam,HBC1,Power Supply,Pump supply was over 45 and pump was hammering. Slowed down to about 30 psi,user_156,asset_102,48.32395485,-103.6179212
5/2/2017,Separator,Choke Valve/Loop,,,,Freezing,"choke leaks, need repair",user_39,asset_877,48.1470144,-103.6180489
7/27/2019,Separator,Pneumatic Control System,Hi/Lo Pressure Controller,,,,When pressuring up unit our high low block and bleed was leaking and not activating correctly and found multiple cracks in black tubing for fuel gas source we closed all necessary valves and bled the pressure off and changed block and bleed and fixed black tubing on fuel source After changing everything was working correctly on high low. Tested/adjusted high and low settings and brought back into service Low-50 High-600,user_153,asset_668,48.3389859,-103.6431246
11/20/2018,Pipeline/Piping,Pipe/Components,,,,hydrate,"Graph was showing some strange stuff. There was a small freeze in line from separator to big joe. Lit glycol bath, gave it about 10 minutes and it opened up. Made sure everything was good and started glycol pump. Water dump did have a freeze, but broke when I tripped it. Blew down sales line. Waiting for well to kick on and will blow it down while flowing. Had a freeze in the sales line. Got it thawed, well is flowing.",user_55,asset_2266,,
6/8/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"attempted to vent well for 1hr, did not make any progress, equalized and left shut. Well has not responded very good to new line pressures with lateral compression.",user_88,asset_150,48.2630395,-102.8996499
12/7/2017,Fuel Gas/Start Gas,Regulator,,,,,the supply gas going to line heater and SCC comes off hot from the gl compressor and when it hits the temp of the outside lots of fluid drops causing me to have to drain and thaw constantly going to put in work order to try to fix,user_176,asset_1707,48.1470144,-103.6180489
1/13/2018,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,Issue: Called out whole pad shut in hi water tank Root Cause: # 2 water tank switch shut the pad in on a false alarm Fix: cleared turned pad back on wrote work order ,user_136,asset_2251,48.1470144,-103.6180489
10/3/2019,Separator,ESD Valve,Gas Supply Line,,,Calibration," DR 27-pad shut in on low unit pressure/valve fault. jumped pad back on and checked dumps all holding, found sandpiper in middle unit blowing through shut off fuel gas to pump, pad stayed up for a few hours then went back down before I could save it, didn’t make it back to location. ",user_37,asset_1907,43.56424,-91.351691
2/13/2018,Separator,Temp Control System,Pilot,,,,"Burner was out because the pilot tip was plugged, cleaned tip and relit the burner.",user_48,asset_2114,48.19768399,-103.7897538
3/8/2017,Gas Scrubber,Dump Line,Dump Line,Other,Other,Corrosion,"1"" unit blowdown pipe corroded by bushing.",user_95,asset_1706,,
12/11/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Arrived on location and did walk down. Found location has been upgraded to electric glycol pumps. No heat trace going to any well head on cabinet A. Walked down glycol system and all valves were open. No globe valve installed in system so heat trace just goes to path of least resistance. So all heat going to oil tanks from cabinet A. Shut off supply to tanks and got heat trace going and warm to well heads then opened valves back to tanks. Thawed out ESD and blow down valve and tubing transmitter (it is in front of the units by ESD. Once Tubing transmitter was thawed, well kicked on on its own plunger came in on its own. it appears as though the electric pumps do not put out the needed pressure or volume to have one pump run the tanks and well heads on a Yokogawa 4 pack location. Really need to have this evaluated to avoid future winter problems due to lack of heat. ",user_15,asset_2106,43.56424,-91.351691
5/1/2019,Separator,Dump Line,,,,Corrosion,"there was a hammer union on the water dump line that was leaking, it looked like when it was put together originally it was cross threaded. I replace with an new hammer union and it is ot leaking any more.",user_22,asset_1278,46.2356189,-100.6010498
2/22/2019,Surface Location,Well Pad,,,,Weather,"Location snowed and drifted in, unable to get on to location with truck to thaw. Well coded down weather waiting on maintenance. ",user_44,asset_379,,
2/9/2019,Flare System,Flare Header,Regulator,,,,"Found 1"" fuel gas line to pilot was frozen just out side of were the heat trace and insulation stop. The line then goes into 2 90 degree elbows to raise elevation of the pipe and to get it to go around the knock out pot. Thawed the 90 degree elbows and got fuel gas to pilots. Drained out very small amount of liquids. Had to use the hand crank to lower the pilot and light it up. This is VERY SLOW. IT TOOK ME ALMOST 20 MINUTES TO DO THIS. WE NEED A BETTER AND FASTER WAY TO LOWER THESE TO LIGHT AS THEY GET BLOWN OUT WITH ANY AMOUNT OF WIND. ",user_15,asset_1383,48.1508,-103.6109984
12/13/2017,Compressor,Compressor,Suction Controller,Boss,,Trash,"Found compression down on high suction kill. After talking to OPT, found the 20 well to be the possible culprit. Well cycles against Line PSI and may build higher PSI than the compressor can handle on kickoff. OPS adjusted suction controller to engage 10 PSI sooner and removed the 20 well from compression to test root cause hypothesis.",user_6,asset_140,36.2541889,-91.2478009
3/29/2019,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,"Methanol injection was hooked up to the wrong spot, should have been hooked up before the D4 and was hooked up to casing injection port, re-plumbed methanol injection",user_31,asset_1623,43.56424,-91.351691
4/4/2018,Separator,rupture disk,,,,premature rupture,"when pressuring up vessel to less than 10psi found bad rupturdisk, root cause week disk or winter freeze weekend disk,",user_122,asset_2005,48.1470144,-103.6180489
11/14/2016,Tanks,Valving/Swedges,Seat/Ball/Piston,Other,Other,Corrosion,Valves leaking by,user_105,asset_1511,48.27250903,-103.6091848
5/12/2018,Chemical System,Electrical,Timer,Interstate,,Overload,"this is for a TxAm SmartTimer. The timer burned up but the external fuses were stil good, so it had to have been an internal failure of the unit. WHAT IS THE FUCKING POINT OF THE DROPDOWNS IF THEY CAN""T BE ACCURATE?",user_134,asset_676,48.1470144,-103.6180489
10/9/2017,Fuel Gas/Start Gas,Regulator,,,,,"Line heater was turned down, adjusted t12's",user_122,asset_1675,48.38730087,-103.8413073
12/14/2017,Compressor,Intrumentation,,,,,"Compressor went down on high suction pressure. Blew liquids out of suction controller. As soon as it got started again, went down again on high suction. I saw that the wells were kicking on harder and faster that the suction controller could respond. Contacted optimization to slow down the speed that the D-4 opens for the well to flow. Started and loaded compressor.",user_62,asset_1998,48.1470144,-103.6180489
2/5/2018,Heat Medium,Surge Tank,Instrumentation,,,,Vessel bath temp gauge broken for unknown reasons. OPS replaced with a new one and verified temps against a temp gun.,user_6,asset_1934,36.2541889,-91.2478009
4/4/2018,Tanks/Pits,Valving/Swedges,Body,,,Corrosion, Opened all condo tanks to operate battery as facility to maximize condo capacity onsite and align with predictive dispatch tools.,user_62,asset_1090,48.1470144,-103.6180489
10/9/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,Changed leaking 3'valves on both water tanks and removed load line,user_173,asset_953,40.5960545,-113.9323891
5/2/2018,Automation,RTU,Relay,Emerson,CWM,Damaged Enclosure,"The dvc small orifices became plugged with fluid and crap. This surface failure does not have any of the equipment needed to fill this portion out. The dvc is a fisher controller by Emerson. Should be under Automation, Controller, Fisher DVC, Emerson.",user_162,asset_1885,48.1470144,-103.6180489
8/26/2019,Plunger System,Plunger,Plunger,PCS,,Not Optimized,Replaced the water dump bonnet. Started cycles and waited for plunger to come in. Caught plunger and then replaced. Turning in a WM to MAINT to replace KF valves on WH. ,user_56,asset_935,40.5262342,-113.8824849
9/29/2019,Surface Location,Lease Road,,,,Weather,"Wet roads due to heavy rain causing limited visibility due to spray from other vehicles and the chance of hydroplaning, slowed my vehicle to 60 mph and gave myself at least 8 seconds between my vehicle and the one directly in front of me to allow extra braking time if needed.",user_22,asset_177,46.2356189,-100.6010498
1/23/2018,Fuel Gas/Start Gas,Regulator,,,,,supply gas froze going to the SCC's again rtp'd after thawing,user_176,asset_2055,48.1470144,-103.6180489
12/20/2017,Heat Medium,Pump,Diaphragm Gears,Texam,HBC1,Wear,Replaced 2 graco 1050 glycol pumps & RTP'd.,user_161,asset_665,40.7126799,-114.1193569
3/6/2018,Compressor,Compressor,Instrument Gas Supply,Ariel,,Liquid Carryover,"When getting onsite drained all scrubbers and fuel gas filter, found fuel gas filter full of fluid ( 2 gallons) drained and started compressor, Killed on lost RPM once again drained filter and was full, opened up 1/2"" bleed outside of compressor building and cleaned out fluid maybe a total of another 2 gallons, then checked desi drier and it was full past inlet, must have been pushing gas from desi to compressor and killed due o fluids being in the fuel gas line. submitted work order to install check on 1"" line on desi",user_115,asset_1264,,
8/24/2018,Wellhead,Manual Valve,Stem/Seat,,,Corrosion,"When doing location walk down, noticed upper and lower master valve was leaking out stem packing. Installed 2 sticks of packing in each and got leaks sealed. ",user_15,asset_1103,48.3085045,-103.6755158
11/1/2018,Flare System,Flare Header,Instrumentation,,,,"Found pilot on flare had been blown out by the wind. Igniter is not hooked up after the fire, lowered pilot, lit it and put it back up. ",user_15,asset_1383,48.2815295,-102.8554546
7/2/2019,Automation,Battery,Battery,Interstate,ECL 31,End Of Useful Life,PLC Batteries have been replaced. If issue with DVC persists please re-submit a WM.,user_108,asset_1606,,
3/11/2019,Chemical System,Tank,Sight Glass,,,Weather,Sight glass was leaking methanol. Tightened sight glass ,user_56,asset_916,48.1470144,-103.6180489
10/31/2017,Automation,RTU,Relay,Kimray,Bristol 3310,Corrosion,Tapped DVC ,user_86,asset_1202,,
9/19/2019,Plunger System,Plunger,Plunger,PCS,,Not Optimized,Plunger missing arrivals vented plunger to surface and rtp'd,user_10,asset_1155,40.5262342,-113.8824849
8/30/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_101,,
8/14/2018,Instrumentation,Controller,,,,,Pulled the graph in the morning and saw it needed a vent TBG pressure was low so I shut ESD\ Got to location TBG was at 589 CSG was at 796 Vented well for 19 mins got plunger to surface and then shut it in to allow plunger to fall will sit with well for next cycle to ensure we get another arrival RTP'd well,user_56,asset_1957,48.2744209,-102.8765361
10/10/2017,Chemical System,Pump,Packing,Texam,HBC1,Wear,"Meth pump leaking, packing nut seized up will need to replace",user_3,asset_1205,47.88190472,-103.4771931
11/11/2018,Separator,Choke Valve/Loop,,,,Freezing,"froze in choke, probably from burner being out, started burner",user_31,asset_892,43.252261,-115.0567324
1/8/2019,Separator,Fuel Supply System, Big Joe Regulator,,,freeze,"big joe frozen, thawed and relit",user_31,asset_2051,43.56424,-91.351691
4/10/2018,Flare System,Flare Header,BMS,,,,Issue: found flare out on the HMI Root Cause: location doesn't make enough to use the flare so last night in the 40+mph wind blew it out Fix: i got with an engineer to review the weather we need any of the LP and flare equipment any more,user_136,asset_2034,48.1474267,-103.6178421
5/3/2019,Separator,Liquid Dumps,Controller,Norriseal,,Improper Adjustment, +LIQUID DUMPS LEAKING THROUGH TO TANKS- THROTTLE CONTROLS- ADJUSTED CONTROLS BUT WILL NEED ADJUSTED WHEN RTP'D,user_34,asset_738,40.5262342,-113.8824849
11/14/2017,Separator,ESD Valve,Gate/Seat,,,Corrosion,Cyclonic blowdown valve at upstream of ESD and choke at inlet to separator used for isolation to blowdown tank failed negative test. Losing pressure during off cycle to blowdown tank causing liquid loading. Visual inspection inspection indicates washed/leaking sealing surfaces. Valve still needs full tear down and inspection. ,user_75,asset_998,,
3/1/2018,Heat Medium,Furnace,Instrumentation,,,,"CB 17-pad bath A callout, interlocked on no pilot, fire eye not seeing pilot wouldn’t reset automation needs to check. Opened main on burner in manual. ",user_71,asset_345,40.5960545,-113.9323891
9/4/2017,Separator,ESD Valve,Gas Sensing Line,,,Fouling,Replaced block and bleed ,user_156,asset_2218,48.1407886,-103.6013577
11/28/2017,Compressor,Compressor (Intergral),Scrubber Level,,,,comp down on suction scrubber level RTP,user_71,asset_1159,48.1470144,-103.6180489
10/6/2018,Flare System,Flare Header,BMS,,,,SCC out possibly due to rain or wind. Relit and back in service,user_55,asset_82,,
3/22/2018,Heater Treater,Burner,BMS,,,Plugging,"Issue: found bath (A) only running the pilot Root Cause: Human Error, who ever relight the bath didn't check back to make sure the burner went through the full light sequence Fix: pressed main start and the main came back on and the bath warmed up",user_136,asset_557,48.2591691,-102.9018403
4/25/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"OPT told an operator that the cyclonic was leaking, Went to location and found that cyclonic was not leaking. vented in plunger and put back to the unit Over and over this well needs a vent and plunger surfaces with a vent OPT to watch this and optimize this well ",user_53,asset_836,48.2591941,-102.9018668
10/27/2019,Separator,Fuel Supply System,Regulator,,,debris,Hi Lo Bypass is galded shut and needs replaced,user_22,asset_1045,46.2356189,-100.6010498
4/15/2018,Tanks/Pits,Liquid Level Control,,,,,Duck lake 1-110/80 high tank alarm tank #761165 at 17-1x10-0 site was shut in on LSH. I shut chokes and wellhead blew fluids out of units called ibex and got tank hauled. didn’t make it back to location dayshift will need to RTP.,user_71,asset_72,48.1470144,-103.6180489
12/22/2018,Separator,Choke Valve/Loop,,,,Freezing," Checked heat trace, it is ice cold going to and from well heads. Checked tanks and it is warm going to tanks. Checked dump lines and they are thawed. Checked pumps, they have been upgraded to electric and they are on and warm. There is no globe valves on tanks to pinch down heat trace to force it to well heads. I shut valves going to tanks to start thawing out blow down line and tubing transmitters. Once I shut off to tanks, heat trace to well heads jumped up to 85 degrees. Thawed out blow down valve and blow down line with thaw tube on truck and tubing transmitter. This is going to freeze again probably by tomorrow until we can get some help figuring out why the electric pumps do not put out the same level of heat. ",user_15,asset_303,48.1470144,-103.6180489
7/17/2019,Instrumentation,Cyclonic Valve,Actuator,,,Freezing,Wyolectric completed this work. Found a blown main fuse caused by a burned up cyclonic actuator. Replaced both.,user_108,asset_1291,,
11/6/2018,Separator,Choke Valve/Loop,,,,Trash,"Have had issues with pad trying to keep it online. Possibly due to fuel gas usage from burner. Jumpered pad back on, the 70 and 130 wells are RTP'd. Put a burp setting in the choke on the 110 well. It does need a vent. Relit glycol bath burner and all 3 sccs.",user_55,asset_324,,
11/17/2017,Wellhead,Choke Valve,Seat,,,,packing leaked ,user_119,asset_1904,48.1470144,-103.6180489
2/27/2019,Separator,Choke Valve/Loop,,,,Freezing,Fire out causing freeze in flow line and horse shoe,user_18,asset_2055,,
8/28/2018,Pumping Unit,Engine,Battery,Waukesha,,Wear,"Controller continually attempting to re-start pumping unit and then shutting off on pumpoff drained battery, necessitating battery replacement.",user_161,asset_1644,48.267245,-102.9231841
8/17/2018,Tanks/Pits,Flare/Combuster,,,,,"While on location, found SCC B was down. Pilot had pressure, unknown reason why it was down. Lit SCC",user_15,asset_768,48.1470144,-103.6180489
12/17/2016,Gas Scrubber,Dump Line,,,,,Dump line froze at desi dryer,user_148,asset_1525,48.33946703,-103.636673
11/20/2017,Dehy,WFS Issue,,,,,dehy is froze ,user_53,asset_1193,48.160134,-103.6170233
11/25/2017,Compressor,Compressor (Recip),Lubricator,,,,Compressor was down on low oil pressure. Rtpd comp ,user_107,asset_1426,47.99540281,-103.4072051
3/7/2017,Wellhead,ESD Valve,Gas Supply Line,Other,Other,Other,None,user_176,asset_89,48.08092764,-103.6020911
12/28/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,"call out GL compressor down again-troubleshoot/rtp-down on hi discharge psi now-had to adjust louvers again freezing off, this compressor sucks,trying to find a happy medium with the ambient temp swings had to open both doors- need auto louvers or????",user_131,asset_1869,40.7126799,-114.1193569
9/18/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Operator had tried to vent plunger to surface yesterday and was unable to and then left the well shut in I went to location and surfaced plunger and put back online I found that the MVT high pressure set point was at 100lbs causing the well to not be able to flow with out putting the well into keep alive mode I adjusted to 600 lbs like it is on every other well and surfaced plunger then put back online.,user_159,asset_1697,43.56424,-91.351691
4/17/2018,Tanks/Pits,Flare/Combuster,,,,,Pilot out. Not sure why. Everything seems ok possible due to wind. Relit.,user_156,asset_2005,48.27157701,-102.8691854
3/1/2019,Surface Location,Well Pad,,,,Weather," SNOW IS UP PAST THE INLETS TO THE QUAD PACKS, 3' DEEP ON THE WALKWAYS TO THE QUAD PACKS NEEDS HAND DIG CREW TO CLEAR AROUND EQUIPMENT",user_34,asset_1108,48.1470144,-103.6180489
5/26/2017,Instrumentation,Transmitter,Tubing Pressure,Rosemount,3051,Wiring,Underground cable from well head main junction box to well head was bad and was replaced.,user_65,asset_2247,48.1470144,-103.6180489
8/1/2018,SWD System,Particle Filter,Element,,,,SITE CHECK FILTER REPLACEMENT IN POD #2 MONTHLY TOTALS FORWARDED ,user_34,asset_538,48.1470144,-103.6180489
9/14/2017,Separator,Choke Valve/Loop,,,,Freezing,"High pressure, lit burner to try and prevent",user_35,asset_2176,48.25338161,-103.4657201
12/30/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_101,48.1470144,-103.6180489
5/30/2019,Wellhead,Valves,,,,human error,"No greasing program, valve need it maintenance, Greased valve and returned to service",user_21,asset_1877,46.2356189,-100.6010498
8/27/2019,Separator,Temp Control System,Electrical,,,,"Pilot fuel gas supply leaking at stainless and 90 piping inside burner housing. OPS tightened fittings and leak checked, verified no more leaks to burner. Found igniter cable burned, either due to the leak of the stainless fittings feeding the pilot caused a fire and burned it, it was improperly installed and fell off or was vibrated off due to incorrect 02 adjustment causing the main burner to pulsate and woof the pilot out on ignition, causing the igniter to arc to the housing, which may have possibly melted the cable if it wasn't the pilot fuel gas supply leak that melted it. The arcing to the housing could have ignited the fuel gas supply leak to the pilot causing a fire at the back of the housing melting components. OPS removed igniter cable from the module inside the panel, tagged the igniter button and created a WM for auto to repair. OPS manually lit burner, adjusted 02/fuel mixture, verified T-12 set points and main/pilot pressures. ",user_54,asset_2108,40.5262342,-113.8824849
4/11/2018,Plunger System,Plunger,Catcher,Well Master,,No Liquid,"Arrived on site to shoot fluid level. When I pressured up tubing to do the fluid shot, i heard the plunger catch has a small leak. I greased the catch and ran it in and out a couple of times and got the leak sealed. Root cause, O rings and threads need some grease to keep things lubricated and sealed. Plunger catcher had not been greased for a while. Well has been shut in for around a year. ",user_62,asset_398,48.1508659,-103.6206981
2/12/2018,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,"Issue: Callout shut in alarm Root Cause: couple of issues. wells have to much off time allowing the pumps to use up all the fuel gas and there is no saving it because the pressure shut down set points never got put back after the compressor got removed Fix: jumped pad back on, readjusted a couple of the wells set points to callout earlier so can catch the pad before there is no recovery. Long Term fix is to get the buy back meter in operation ",user_136,asset_479,48.2595091,-102.9010563
2/28/2019,Sales Valve (PV),Sales Valve,Body,Automax,,Freezing, High unit pressure alarm I went to location and I had to walk in from location sign I contacted the contractor before and after I walked in I shut the well head and drained separator to let it idle down the burner is still going but the cyclonic is still froze road will need bladed to get truck into location I put in a deferral status in on location. There was not an option for cyclonic on the sales line.,user_159,asset_590,43.56424,-91.351691
4/20/2018,Heat Medium,Furnace,Shell,,,,Checked for fluids in condensate to low pressure unit line heater scrubber. No fluids present.,user_62,asset_1675,48.1470144,-103.6180489
7/1/2017,Instrumentation,Controller,,,,, 6. Latham Draw 7-70 - DVC is not opening and closing correctly (216 Deferral) • Found feedback arm barley attached to DVC • Found feedback sensor out of range • Calibrated feedback sensor • Calibrated DVC Notified optimizer,user_92,asset_309,48.1470144,-103.6180489
11/18/2018,Chemical System,Piping,Discharge Line,,,Freezing,"compressor went down on high scrubber level, all dumps were frozen, took all pressure off, thawed on several different spots, put heat on scrubbers, finall got scrubbers t drain RTP compressor, has been running..new pumps were installed but not powered up. Trying to find out if pumps are done and ready to go.",user_106,asset_1154,48.2628392,-102.9008935
8/28/2018,Tanks/Pits,Flare/Combuster,,,,,A scc out probably due to high wind ,user_31,asset_1759,48.19681647,-103.6327586
10/27/2018,Compressor - Gas Lift,Compressor,Scrubber Level,Ariel,,Trash,Gas lift compressor was down for 2nd Interstage Liquid Level. Found main dump valve closed. Blew down the casing on well to confirm no hydrates. RTP'd compressor and well,user_55,asset_1359,,
8/16/2017,Separator,Shell,Body,,Steel,Corrosion,Pilot Burner Orifice Clogged with Carbon sediment. Cleaned and lit to test- Good,user_138,asset_100,48.12211594,-103.4690718
5/22/2018,Gas Scrubber Separator,ESD,,,,,"Issue: well shut in on low unit pressure Root Cause: went to location and checked the dump there wasn't any leaking dumps, the glyocl pumps were shut off, found the burner still on i shut that off but nothing that would have used up that much unit pressure. i also went through the dehy to make sure they weren't using up gas on something and all there stuff was good Fix: rest alarm turned well back on restarted the plunger cycles and the units are holding good now",user_136,asset_1050,40.7126799,-114.1193569
12/4/2017,Tanks/Pits,Flare/Combuster,,,,,SCC Fire Eye not sensing Burner being lit. This was turned in as a Task Request for Automation to fix two weeks ago. No resolution yet. All burners are up and going.,user_138,asset_1187,48.18395666,-103.4262128
4/25/2019,Wellhead,Manual Valve,Master Valve,,,Corrosion, +WELLHEAD MASTER VALVES LEAKING THROUGH THE STEM AREA AND VERY HARD TO OPERATE- *WM ENTERED FOR GREASING AND STEM PACKING,user_34,asset_1607,40.5262342,-113.8824849
11/16/2017,Wellhead,Cyclonic Valve,Gate/Seat,,,Fouling,LEAKING TO TANK,user_119,asset_998,48.1602747,-103.6173515
12/12/2017,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,Issue: whole pad shut in callout Root Cause: all the wells going into off cycles at the same time and then the unit runs out of gas and the pad shuts in Fix: turned pad back on left well running to keep the units pressured up. Long term fix is putting the buy back meter into service ,user_136,asset_309,48.1470144,-103.6180489
9/30/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_1633,48.1470144,-103.6180489
11/7/2018,Pumping Unit,Engine,Catalyst,Waukesha,,Wear,"Engine exhaust catalyst has 13,000 hours on it, typical lifespan is 8800 hours. Replaced catalyst and emissions were now compliant.",user_42,asset_2011,48.2669945,-102.8989171
4/17/2018,Tanks/Pits,Liquid Level Control,,,,,Well high ranked last night and tank has been pulled. Night operator found isolation valve between 29-2 and 29-120 not holding and well cannot be rtp’d until valve is changed out. I got with engineering to also install cyclonic valve while well is down. ,user_58,asset_599,48.40619163,-103.5810323
12/15/2018,Separator,Temp Control System,Fuel Gas Supply,,,,PLUNGER NOT MAKING ARRIVALS *GLYCHOL PUMPS TURNED OFF. *PUMPS NOW TURNED ON AND ADJUSTED GLYCHOL TEMP UP TO 90 DEGREES WATER DUMP LINE FROZE. ,user_34,asset_476,47.7434332,-103.4498
10/17/2017,Separator,Choke Valve/Loop,,,,Freezing,,user_35,asset_1928,48.31237932,-103.410107
12/11/2017,Tanks/Pits,Liquid Level Control,,,,,Issue: found live reads showed 17' condo tank Root Cause: Human Error/ Dispatch missed tank Fix: gauged and switched tanks,user_136,asset_42,48.1470144,-103.6180489
9/19/2019,Heat Medium,Pump,Seals,Texam,HBC1,Wear,Replaced both pumps with new Sandpiper,user_5,asset_1543,41.474544,-90.6778637
6/10/2018,Wellhead,Tubing,,,,hydrate,broke down hole freeze cycles resumed,user_11,asset_27,40.5960545,-113.9323891
11/12/2018,Heater Treater,Burner,BMS,,,Corrosion,"Issue: While performing my walk around found bath (B) at 88deg Root Cause: Human Error, T-12 is turned up a bit hi for this time of year. with fluctuating temps bath being this hot will cause lots of carry over Fix: bumped bath temp down ",user_170,asset_339,48.1470144,-103.6180489
2/27/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Stainless and fisher control box flooded with fluid. Most likely source coming from the buy back meter. OPS shut in the buy back on flowing well and tested fisher and all other end devices before RTP'ing the well and draining the fluids.,user_6,asset_226,36.2541889,-91.2478009
9/19/2019,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,"Found well loaded and not flowing, cycles were taken out since last month. Checked graph and well has not flow well since November last year. I did not find in formation about plunger in the programs. Equalized well to re mediate any freeze in the tubing. Started flowing, and after 20 mins of flow started the plunger vent procedure. Vented well for 30 mins and got a plunger arrival. Plunger was inspected and it was worn out. Dual pad plunger was replaced for a new plunger. Put cycles back and waited for fall time for the plunger. ",user_83,asset_537,40.5262342,-113.8824849
3/27/2018,Separator,Fuel Supply System,big joe regulator,,,debris,1/2 balon tying buy back gas into vessel and fisher controler was open. When another well on the pad turned on it would cause a false flow rate when well was in off cycle. Closed 1/2 balon leaving vessel sence line open to Fisher controler,user_109,asset_995,48.3531924,-103.774893
1/23/2018,Compressor,Compressor,Instrument Gas Supply,Compressco,,Freezing,Dump controller on the gas scrubber leaking thorough the vent due to a freeze. ,user_130,asset_1346,48.1470144,-103.6180489
3/14/2018,Fuel Gas/Start Gas,Regulator,,,,,"well was down due to maintenance, RTP warmed bath up, purged system put to sales",user_88,asset_1793,48.1470144,-103.6180489
6/22/2018,Separator,Choke Valve/Loop,,,,Corrosion,changed out leaking choke and replaced,user_11,asset_2161,43.252261,-115.0567324
12/14/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Desi and fuel gas scrubber of liquids daily routine auto dump may be a solution to issue ,user_109,asset_774,48.3272165,-103.6565078
1/7/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,vented plunger to surface and put back on plunger cycles.,user_51,asset_220,48.1470144,-103.6180489
8/26/2019,Surface Location,Well Pad,,,,Weather,Wet winter & spring combined with poor weed treatment in 2018 led to location needing to be sprayed.,user_42,asset_1587,48.263329,-102.917273
6/3/2019,Plunger System,Plunger,Plunger,Well Master,,Corrosion,Plunger undersized replaced with new bar stock. Lubricator inspected found to be in good condition. Well RTP ,user_153,asset_732,48.2223486,-103.6359511
4/1/2018,Dehy,Pump,Process Indicator,Texsteam,HBC1,Debris,Wfs dehy issue. Pump was hammering. Shit off and contacted wfs,user_156,asset_1384,48.287525,-103.6498187
8/7/2018,Separator,Choke Valve/Loop,,,,Trash,Well was flowing on the casing side and was loaded I vented well and brought back online.,user_159,asset_621,48.1470144,-103.6180489
9/16/2017,Compressor,Cooler,,,,,Froze in cooler I broke freeze and adjusted the louvers they are currently in manual because archrock was unable to fix the auto controller.,user_51,asset_780,48.3619066,-103.2129855
12/16/2017,Fuel Gas/Start Gas,Coalescer/Filter,Level Controller,,,,Desi drain froze Thawed for 1 hr still not able to break freeze. Task request entered to replace insulation ,user_156,asset_1087,48.21141661,-103.6387025
6/24/2018,Separator Inlet Valve (XV),Sales Valve,Pie Disks,Valvcon,,Freezing,Cyclonic valve frozen off and actuator hit torque limiter. If issue continues after kateral compression pulls well pressures down OPS may need to install methanol injection point just downstream of cyclonic or turn on heat trace.,user_6,asset_314,36.2541889,-91.2478009
12/9/2017,Automation,RTU,Io,Schneider/Scadapack,Scadapack P4A,Wear,well called out on false high tank for second time in 3 days.,user_71,asset_320,48.1470144,-103.6180489
5/9/2019,Separator,Choke Valve/Loop,,,,Freezing,"Found wellhead frozen, thawed both tubing valves on the well. Replaced block and bleed on the hi/lo pressured up unit and started glycol bath / check levels. Guaged tanks , lit scc . Contacted Williams to get the dehy up and running. Once Williams was done I pressured up the unit and function tested dumps and hi/lo.Contacted optimizer to review cycles and rtp well. Stayed on location to slowly get the choke open as the well flowed out. Completed all checklist for this location.",user_10,asset_127,40.5262342,-113.8824849
12/21/2016,Gas Scrubber,,,,,Other,DVC controller on automated choke had a freeze in it. Thawed controller and blew out any remaining liquids and RTP'd ,user_152,asset_334,,
12/7/2017,Heat Medium,Pump,Seals,Texam,HBC1,Wear,"Replaced Graco 1590 1 1/2"" glycol pump.",user_161,asset_616,40.5960545,-113.9323891
3/8/2018,Fuel Gas/Start Gas,Regulator,,,,,fuelgas system had a lot of fluid in it. Went though and drained all scrubbers and all drop pts and desi.,user_88,asset_1862,48.2630355,-102.8998958
1/14/2019,Separator,Choke Valve/Loop,,,,Freezing,"Check to make sure all dumps open and drained scrubber. Everything is open to tanks, heat has been on, glycol pump, Graco, has been on. Drained scrubbers and fuel pots. Had a freeze between ESD and choke. Thawed on it, closed FMC valve and opened blowdown valve. Opened choke, flowed backwards, freeze broke. RTP'd well",user_55,asset_1249,,
10/12/2017,Instrumentation,Transmitter,3N1 MVT,ABB,1151,Calibration Issue,Complete Calibration,user_113,asset_1577,40.5262342,-113.8824849
7/2/2018,Automation,Plunger Arrival Switch,,Tripmate,,,Tripmate failed. Likely end of useful life.,user_134,asset_123,43.252261,-115.0567324
1/13/2017,Automation,Cable,,,Other,Electrical Short,"No damage, the electrode was making contact with the piping. I readjusted the ignighter and reinstalled the pilot on both baths A & B. slj",user_162,asset_1404,36.2541889,-91.2478009
12/30/2017,Wellhead,Manual Valve,Body,,,Freezing,Wellhead froze. Bad insulation around plunger cap has been cut open. Repaired insulation ,user_156,asset_2196,48.22178632,-103.6301072
9/15/2017,Separator,Liquid Dumps,Body,Norriseal,,Improper Adjustment,Valves are installed in the wrong flow direction allowing pressure to push through,user_163,asset_111,48.20357614,-103.8164753
8/25/2019,Tanks/Pits,Piping,Connections,,,Connections,Leak appears to have originated from where the blow down tank vent piping threads into the top of the tank. Leak may have occurred during piping reconfigure or during a vent. ,user_54,asset_1383,40.5262342,-113.8824849
1/3/2017,Wellhead,Cyclonic Valve,Actuator,,,,No automation issue. Cyclonic actuator functions correctly,user_92,asset_742,48.3619066,-103.2129855
7/20/2017,Gas Scrubber Separator,Pneumatic Dump Valve,Packing,Invalco,,Wear/Tear,hi low packing was shot. rebuilt trim and seat put back in service,user_53,asset_16,40.5262342,-113.8824849
7/27/2018,Tanks/Pits,Flare/Combuster,,,,,ARROW Found piece of Teflon tape stuck in pilot gas regulator for SCC D. Removed tape and lit SCC. ,user_15,asset_339,48.1470144,-103.6180489
6/16/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,Flowline froze.,user_94,asset_1285,48.1470144,-103.6180489
11/10/2017,Separator Inlet Valve (XV),Electric Control System,Actuator,,,,Choke is leaking,user_35,asset_1538,48.18288838,-103.5378128
5/20/2019,Wellhead,Manual Valve,Master Valve,,,Freezing,Human error: Valves not completely opened up causing freezing issues.,user_54,asset_596,40.5262342,-113.8824849
7/26/2019,SWD System,Piping,Supply Line,,,Debris,"Information for land shark control: Pump shuts itself off at 22 mph wind. Also wind direction has to be between 190 and 240 degrees, direction setpoints, before pump will kick on. Had to pull foot valve out of the pond and clean it. Finally got it to prime and RTP'd. Filled generator up with fuel. Checked coolant temp, was 186 degrees. ",user_55,asset_2253,,
8/14/2019,Separator,Choke Valve/Loop,,,,Corrosion,"While RTPing well heard small amount of gas leaking, after further trouble shooting found sand probe on horse shoe leaking. Blew down unit removed sand probe and replaced with 1/2” plug",user_18,asset_1572,,
12/6/2017,Compressor,Compressor,Process Gas Supply,Ariel,,Trash,"Low suction, due to d4 install , turned over to engineering ",user_122,asset_676,48.3530129,-103.7749459
2/9/2017,Instrumentation,Other,Other,Other,Other,Other,None,user_74,asset_708,47.92587614,-102.4582459
5/10/2018,Separator,ESD Valve,Gas Supply Line,,,Freezing,Well froze off in choke causing well to esd due to lack off fuel gas. Froze off in choke because burners are shut off and they were trying to flow off pressure on a pinched choke. Backblew glowling to AGT. Broke freeze. Pressured up unit relit burner. Currently babysitting choke so we don’t have another freeze. Well rtp,user_172,asset_1083,,
7/31/2017,Separator,Choke Valve/Loop,,,,Trash,"packing was bad, replace packing and pressure test.",user_39,asset_2198,48.1603184,-103.6173195
3/7/2017,Instrumentation,Transmitter,3n1 MVT,Other,Other,Weather,None found ,user_113,asset_986,48.21403319,-103.6318959
11/5/2017,Instrumentation,Transmitter,Temperature,Rosemount,2088,Wiring,"Ruby Knolls 35-1 - Tubing transmitter not powered up. Cable had pulled out of the transmitter. Fixed for now, but cable needs to be replaced to take the tension off of it. Tight as a bowstring. ",user_92,asset_1928,48.1470144,-103.6180489
4/26/2019,Tanks/Pits,Flare/Combuster,,,,, **SCC'S OUT DUE TO WIND. * RELIGHTED AND READING IN TEMPS,user_34,asset_1510,40.5262342,-113.8824849
11/17/2016,Chemical System,Pump,Check valve,,,Debris,Turned glycol pump on yesterday. Noticed this morning had quit. Took cover off of air valve and it was full of paraffin. Cleaned up air valve system and sprayed with a lubricant. Rtp'd pump. Will confirm that it is still running later. ,user_141,asset_2225,48.11062221,-103.6689517
12/16/2018,Separator,Liquid Dumps,Controller,Norriseal,,Freezing,"dumps froze from burner being out, vessel froze",user_31,asset_2104,47.7434332,-103.4498
10/12/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,"Pad was down due to no fuel gas , repressure all 8 units and RTP",user_109,asset_886,48.3076525,-103.6410581
8/25/2017,Compressor,Compressor,Dump Valve,Ariel,,Freezing,Compressor went down on high fuel scrubber level was able to clear alarm with out draining the scrubber ,user_122,asset_1675,48.3629631,-103.7897382
6/9/2017,Compressor,Compressor,Suction Controller,Compressco,,Liquid Carryover,Found fluid in controller regulator cleared and restarted.,user_51,asset_835,48.1470144,-103.6180489
4/25/2017,Automation,Other,,Other,Other,Other,Pvc broke,user_162,asset_1142,,
4/12/2019,Separator,Choke Valve/Loop,,,,Freezing," 8. Tierney 22-160 - DVC won't open unless tapped on • Operator reported ""DVC won't open unless tapped on"" this indicates a fuel gas issue causing either a freeze or fluid buildup inside of DVC due to bad fuel gas • When I got to location I checked HMI and well has not flowed all day due to high line pressure • I tested DVC and DVC opened correctly • I checked fuel gas pressure to DVC and found pressure at 20 PSI this is not correct, pressure should be set at 40 PSI • I corrected supply pressure issue at regulator • I removed relay from DVC and blew out DVC best I could • I stroked DVC open and closed multiple times from HMI to verify functionality DVC tested and verified good NO AUTOMATION ISSUE FOUND",user_38,asset_627,40.5262342,-113.8824849
3/7/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Plunger fail to surface, will attempt pressure build and vent",user_35,asset_785,48.2006198,-103.5383854
3/27/2017,Instrumentation,Transmitter,Flow,Other,Other,Other,,user_99,asset_1359,48.3619066,-103.2129855
6/29/2018,Wellhead,Manual Valve,Body,,,Erosion,Well was shut in and tagged for leaking master valve. Master valve was greased and tested to be holding. Removed tags and opened well head valves in position to flow well. ,user_62,asset_2147,43.252261,-115.0567324
1/17/2018,Heat Medium,Pump,Diaphragm Gears,Sunpumper,113,Wear,"Pump just wouldn’t stroke any more, didn’t think sand piper pump had that problem, hit it with a hammer, still nothing, ",user_84,asset_662,48.06015159,-103.5299793
2/2/2019,Separator,Temp Control System,Heater/Burner,,,,bird cone missing,user_22,asset_2146,46.2356189,-100.6010498
10/6/2018,Compressor,Compressor (Recip),Crossheads,,,,COMPRESSORS DOWN 1ST COMPRESSOR DOWN ON LOW DISCHARGE PRESSURE 2ND VRU COMPRESSOR DOWN BECAUSE FIRST COMPRESSOR WENT DOWN RESTARTED- WENT DOWN AGAIN ON SAME THING RESTARTED- ADJUSTED RECYCLE VALVE SLIGHTLY SEEMS TO BE WORKING,user_34,asset_1383,43.56424,-91.351691
4/1/2018,Flare System,Flare Header,Instrumentation,,,,Scc out relit and returned back to service pilot plugged cleaned. Dirty wet gas the reason that pilot plugged off,user_58,asset_1421,48.40631375,-103.580907
6/26/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized, I surfaced plunger once at beginning of shift well didn't come back around I went back to location and surfaced plunger for a second time and put back on plunger cycles.,user_51,asset_182,43.252261,-115.0567324
5/10/2017,Compressor,Compressor,Process Gas Supply,Ariel,,Trash,"Compressor went down on lo suction , restarted compressor and let optimizer know what it went down on ",user_122,asset_140,48.36292643,-103.6390572
1/11/2018,Compressor,Compressor,Suction Controller,Ge Gemini,,Trash,Compressor down on low interstage pressure all pressures were fine cleared alarm and restarted,user_51,asset_1458,48.2649686,-102.890244
11/10/2017,Separator,ESD Valve,Gas Supply Line,,,Fouling,Well esd on low pressure. Pressured up rtp well,user_172,asset_1538,,
4/16/2019,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,"Dispatched to pad due to compressor going down Got to pad and found that the compressor went down on low 2nd stage pressure Got Compressor started and warmed up then got it loaded. This 10 well is froze in the flow line Unable to break freeze by popping it to the tank, had to put my thaw tube on it and got it flowing in 3.5 hours ",user_56,asset_879,48.1470144,-103.6180489
3/5/2019,Surface Location,Lease Road,,,,Weather,road needs bladed for access,user_25,asset_1876,,
2/7/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Well had consecutive non arrivals I went to location and vented plunger to surface and put back on plunger cycles.,user_51,asset_498,48.1470144,-103.6180489
3/28/2018,Tanks/Pits,Berm,Dirt,,,Wildlife/Livestock,Tank berm needed to be repaired due to live stock and inside the tank dike it needed to be cleaned up and fill low areas due to a previous spill.,user_150,asset_712,,
11/14/2016,Compressor,Engine,Fuel Gas Supply,Other,,Liquid,"Compressor is going down almost every day, due to liquid dropping out in the fuel gas supply off the discharge. Need to use the fuel gas off the 2nd stage scrubber that is locked out my measurement ",user_122,asset_676,48.36321145,-103.7895675
7/2/2019,Automation,Transmitter,Unit Pressure,Yokogawa,EJA530E,Calibration Issue,All the transmitters for pressure readings. No power. Optimizer unable to clear alarms. ,user_90,asset_660,48.03892483,-103.4294642
9/5/2019,Instrumentation,Transmitter,Unit Pressure,Rosemount,3051,Water,Found Unit transmitter with blank screen. Replaced transmitter and verified operation.,user_169,asset_1400,46.2356189,-100.6010498
10/11/2017,Wellhead,Tubing,,,,,,user_35,asset_2171,48.31198,-103.4082532
12/29/2017,Gas Scrubber Separator,ESD,,,,,call out wells shutting in /shut in on low unit psi/wells shut in to long on cycles and lose psi with everthing going in winter time/need sacrificial well or faster running metal in hole?????,user_131,asset_1362,40.7126799,-114.1193569
7/1/2018,Gas Scrubber Separator,ESD,,,,,"Frewen 14-pad shut in on hi tank, low inlet and low unit, all false looks like an automation issue. Reset interlocks and jumped pad on RTP and started cycles.",user_71,asset_174,48.1470144,-103.6180489
9/15/2019,Plunger System,Plunger,Lubricator Top,IPS,,No Liquid,"Lubricator spring is compressed about an inch, needs repaired or replaced. It is a weatherford lubricator",user_22,asset_1897,46.2356189,-100.6010498
1/22/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Relit pilot. Insulated fuel gas supply line to pilot to prevent possible freeze cutting off supply gas. ,user_41,asset_509,48.23556571,-103.543088
1/29/2018,Compressor,Compressor (Recip),Process Gas Supply,,,,"call out compressor down-down on low 2nd stg discharge psi-checked & drained control valves, no liquids and not froze, checked & blew down panel with test port valves they looked good, looks like cycles non arrivals-shut in too long and drained gas supply? rtp comp and paused open wells until arrivals, might need to keep one on open flow like i used to last winter?",user_131,asset_1346,40.7126799,-114.1193569
4/9/2018,Flare System,Flare Header,Instrumentation,,,,Flare out and relit no problem. Assuming to wind blew the pilot out. Root cause to much wind and not enough wind blocks. ,user_58,asset_2069,48.36531715,-103.5206164
5/3/2017,Instrumentation,Transmitter,3N1 MVT,Rosemount,4088,Recalibrated,,user_99,asset_2168,48.1470144,-103.6180489
10/14/2018,Separator Inlet Valve (XV),Electric Control System,Actuator,,,,"gas supply line to pressure transmitter froze, thawed out and drained liquid from line",user_31,asset_1534,43.252261,-115.0567324
9/23/2019,Plunger System,Plunger,Plunger,Well Master,,Corrosion,"plunger old needed swapped tried bringing up in cycle and needed to vent old one in, swapped and RTPin cycles, missing arrivals",user_106,asset_955,40.5262342,-113.8824849
2/21/2019,Separator,Dump Line,,,,Freezing,"Attempted to RTP well. Found that the scrubber was ball check. Drained scrubber, and got the ball to drop. Got the burner relit on Sep A. Started checking dumps, found that dumps are froze. Checked a few others and all are froze. Will write a work order to have steamer come and thaw dumps.",user_55,asset_628,,
11/18/2017,Compressor,Compressor,Scrubber Level,Ariel,,Liquid Carryover,,user_156,asset_1675,48.2715602,-102.8691564
2/3/2018,Gas Scrubber Separator,Water Meter,Turbine,,,Trash,Scrubber full of water on the glycol separator. Not sure why hooked to buy back,user_156,asset_793,48.35279798,-103.7750476
5/23/2019,Dehy,Piping,Discharge Line,,,Freezing,lateral freeze,user_22,asset_372,46.2356189,-100.6010498
1/12/2019,Separator,Manual Drain Valves,Body,,,Freezing,"Dump lines frozen, no burner, no fuel gas",user_31,asset_1055,43.56424,-91.351691
2/10/2017,Chemical System,Containment,Other,Other,Other,Weather,A spill of glychol,user_163,asset_277,48.22280301,-103.7532311
10/2/2018,Compressor - Gas Lift,Compressor,Suction Controller,Ariel,,Vibration,"RROWPLUS Compressor down on high suction pressure, went down a couple more times. Running about 86 psi then bounciing. Lowered suction controller closer to 80 psi still bouncing 73 to 85. Shut down at 90. Not quite hitting injection rate.",user_31,asset_1332,43.252261,-115.0567324
1/31/2017,Automation,Cable,Data Cable,3M,Other,Loose Connection,Breaker failed and needed to be replaced.,user_65,asset_1583,48.3619066,-103.2129855
2/28/2019,Heat Medium,Pump,Impeller,Goulds,HBT2,Wear,One of the solar powered pumps had a blown fuse. I replaced the fuse but the pump still didn’t run. Possible bad electric motor. WM submitted to maintenance for replacement. ,user_68,asset_2270,48.19351328,-103.5417477
3/4/2018,Compressor,Compressor,Suction Controller,Ariel,,Vibration,On skid recycle was opening at 55 psi which is shutdown. Increased to 62 psi. ,user_156,asset_794,48.22037452,-103.5957473
12/15/2016,Automation,Plunger Arrival Switch,,,Other,Other,,user_134,asset_508,36.2541889,-91.2478009
11/21/2016,Wellhead,,,,,,"2"" tubing KF valves leaking through stem ",user_105,asset_252,48.09116484,-103.6579404
6/1/2018,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,"Issue: well had no current or daily volume Root Cause: plunger was logged off. once i unloaded the well i found out why its logging off the DP wont go past 1.2"" so the well is only flowing 145mmcf and is bouncing off the hi/low. optimizer need to relook at there set points Fix: unloaded well and returned to service",user_136,asset_1361,48.1470144,-103.6180489
9/7/2018,Compressor,Compressor,Process Gas Supply,Ajax,,Trash,Issue: well was down from Williams power issues causing the hi line pressure Root Cause: found that once the line pressure came down i restarted the compressor but was having issues with the well under performing. once i was able to get the well to come around the comp stayed running Fix: i kept turning the comp back on and babysitting it along tell the well came around and started feeding it enough gas. both the comp and well is back into service ,user_170,asset_1417,49.5499678,-102.9290839
8/18/2018,Flare System,Flare Header,Instrumentation,,,,relit SCC A and fixed pilot solenoid on SCC B,user_37,asset_298,48.224585,-103.8291059
1/16/2019,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Location is set up for buy back gas from WFS. Checked valving and found buy back line is open and in service. However, all fuel gas lines from the units were open as well. With both lines open, there is not way to tell were we were pulling fuel gas from. Shut fuel gas from separators off so we are using buy back gas for fuel gas across pad. ",user_15,asset_2167,48.1499808,-103.6200096
9/13/2018,Wellhead,Casing,Lower Casing Head Valve,,,,Issue: Arrow Dispatch well is shut in for a SIPB Root Cause: found the well wasn't SIPB and I also found the national ball valve on the casing side of the well head leaking. That valve leaking is what is causing the well to load up and log off but no one was able to see that do to there is no transmitters on the tubing or casing Fix: found the wing valve holds so I shut the valve wrote a work management to replace the valve and i also found the blow down leaking so i shut the well in ,user_170,asset_1058,48.2815848,-102.8554084
4/4/2019,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,kimray fuel pot full of liquids ,user_56,asset_1365,48.1470144,-103.6180489
4/4/2019,Separator,Shell,Body,,Steel,Erosion,Blow down valve was leaking by and liquid loading the well. Valve was replaced.,user_68,asset_2087,48.1470144,-103.6180489
3/27/2018,Compressor,Compressor,Suction Controller,Ariel,,Liquid Carryover,Drained liquid pots on suction control that was completely full of liquid. ,user_156,asset_1735,48.2114459,-103.7734515
3/10/2018,Automation,Antenna,,Bluewave,,Corrosion,Arrow failure. Dispatched to well with a failure DH and is waiting on rig. Incorrectly dispatched to well.,user_107,asset_822,,
10/27/2016,Automation,,,,Other,Other,Rosemount transmitters not reading accurately on tubing and casing ,user_7,asset_485,48.0218082,-103.5637069
11/20/2017,Separator,Temp Control System,Pilot,,,,Burners were out on bath of unit causing unit to go down,user_109,asset_793,48.3596135,-103.7770335
3/15/2018,Fuel Gas/Start Gas,Regulator,,,,,Rain put all the SCC on the PAD out had to relight all of them,user_46,asset_342,48.0614644,-104.8417043
3/21/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,well lost plunger arrivals,user_179,asset_1790,48.1470144,-103.6180489
11/28/2017,Flare System,Flare Header,Regulator,,,,abbutec SCC went out on no pilot flame. the wind probably blew out.,user_71,asset_1213,48.1470144,-103.6180489
10/17/2019,Recirc Pump,Pump,Cam,Texam,HBC1,Debris,"Electric glycol pump was turned on but not running. Found the charge controller showed ""reset required"" Followed on screen prompts and got controller reset and pump turned on and started working. I am not familiar enough with electrical stuff to do the RCFA on the pump controller. ",user_15,asset_1383,46.2356189,-100.6010498
3/13/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Down on criteria, trying longer off time, new plunger on dec, 4th, may try different style plunger. ",user_35,asset_2211,48.20062923,-103.5384733
1/17/2019,Fuel Gas/Start Gas,Regulator,,,,,"Freeze in fuel gas to esds, chokes & DVCs ",user_18,asset_1067,,
6/5/2019,Separator,PSV,Body,,,Incorrect Set Point,"I was dispatched to work on the pad and noticed on the following well: #50, #130, #70, #60, the rating on the PSV and the vessel in 1440 psi on both. It looks like that this issue was already flagged by another operator since the tag on the wellhead indicates so. Those vessel does not have Rupture disk, and the unit is set to over pressure at the same time that the PSV will open. Also three of those well already have over 1100 psi on the tubing. TL and engineer notified. Left wells shut in until further investigation. ",user_83,asset_231,40.5262342,-113.8824849
3/8/2017,Sand Separator,Other,,Other,Other,Other,none,user_39,asset_554,36.2541889,-91.2478009
12/7/2016,Automation,POC,,,,,"Trying to vent plunger and pad goes in and out of communication status, it only last for a short time but can make some work difficult to complete ",user_148,asset_1286,48.33590883,-103.5981957
10/30/2019,Gas Scrubber Separator,Dump Line,,,,Trash,Site walk down dumb scrubbers check burners scrubbers dumped for 3 seconds,user_128,asset_1543,48.2221401,-103.6360437
3/18/2018,Gas Scrubber Separator,ESD,,,,,Issue: found well down on the HMI Root Cause: yesterday when the pad shut in on low unit pressure and was turning back on this well didn't show any flow so i wanted to verify everything was lined up before turning well back on Fix: all the dumps were open to the tanks and the sales valves open turned well back on found it was froze left shut in to equalize pressure and break freeze ,user_136,asset_501,48.1470144,-103.6180489
2/22/2019,Wellhead,Tubing,,,,,Vented well to unload liquids and surface plunger with no success. ,user_68,asset_8,48.20701712,-103.6213817
5/27/2018,Compressor,Compressor,Scrubber Level,Sullair,,Liquid Carryover,Compressor down on high 2 nd stage scrubber level. ENG engaged and is working the solution to the problem,user_6,asset_1383,36.2541889,-91.2478009
8/18/2017,Automation,Plunger Arrival Switch,,Tripmate,,,"Tripmate was wired carelessly, and damaged by the resulting short.",user_134,asset_916,48.1583852,-103.6173696
8/4/2018,Automation,RTU,Io,Schneider/Scadapack,Scadapack P4A,Weather,SCADAPack P4A had burned out analog inputs. Suspect lightning damage.,user_12,asset_1651,48.224585,-103.8291059
1/23/2018,Compressor,Compressor (Recip),Scrubber Level,,,,"Compressor was down on HI 2nd stage scrubber level. scrubber was froze, finally got it to break free. warmed up compressor and RTP'd well ",user_53,asset_354,48.1602435,-103.6172092
4/4/2018,Separator,Choke Valve/Loop,,,,Corrosion,"Negative tested choke, choke tested good. ",user_62,asset_1661,48.1470144,-103.6180489
1/11/2018,Instrumentation,Controller,,,,,Issue: found well down on the HMI Root Cause: couldn't find any reason why the location shut in. Everything was perfect must have had an automation glitch of some sort Fix: turned back on and returned to service ,user_136,asset_1623,48.1470144,-103.6180489
2/5/2019,Fuel Gas/Start Gas,Regulator,,,,,Big Joe freeze thawed with heat tube ,user_57,asset_83,46.2356189,-100.6010498
1/13/2019,Separator,Temp Control System,Fuel Gas Supply,,,,"fuel gas buy back was frozen, thawed out before starting burner",user_31,asset_793,43.56424,-91.351691
4/4/2017,Gas Scrubber,Other,Other,Other,Other,Other,No damages,user_112,asset_202,48.00446214,-103.7340782
4/9/2018,Wellhead,Tubing,,,,,well was loaded,user_179,asset_198,48.1470144,-103.6180489
3/27/2018,Instrumentation,Tank Level,Sonar,,,Calibration Issue,"Found pad down on false high tank. water tanks at 2.4 Had to bypass pad to be able to jump pack on Air compressor was on and had 125psi on it After getting pad jumped on. I restarted the compressor. Compressor said it was down on low suction, due to ESD's closing RTP'd well ",user_53,asset_345,,
10/20/2018,Wellhead,Tubing,,,,,"vented well for 60 min, didn't unload left shut in to build pressure ",user_37,asset_1975,48.1602512,-103.6200315
11/12/2018,Instrumentation,Transmitter,Flow,IPS,Ashcroft Pressure,Weather,frozen transducer got unfrozen and back to normal operations,user_121,asset_1898,48.3580576,-83.27272
10/4/2019,Tanks/Pits,Berm,Steel,,,Vehicle,"Corner post on fence around tank berm is broken off at ground, needs replaced",user_22,asset_564,46.2356189,-100.6010498
5/25/2019,Surface Location,Lease Road,,,,Weather,County road north of Wamsutter is horrible. Has BIG holes in road everywhere.,user_55,asset_2253,,
12/23/2017,Compressor - Gas Lift,Compressor,Cylinder,Ge Gemini,,Trash,Gas lift went down on high cyclnder temp #2 I opened louvers cracked open the doors and restarted.,user_51,asset_1264,48.1470144,-103.6180489
12/22/2017,Compressor,Compressor,Panel,Sullair,,Electrical Short,"electric air compressor wouldn't allow faults to be cleared, might of had a power loss.",user_71,asset_600,48.1470144,-103.6180489
12/14/2016,Compressor,Compressor,Suction Controller,Other,,Trash,"Compressor down on low suction. Restarted compressor, adjusted wells, ",user_141,asset_620,48.3619066,-103.2129855
9/19/2019,Plunger System,Plunger,Plunger,PCS,,Not Optimized,Well was missing arrivals and needed at vent / vented plunger and rtp'd,user_10,asset_1929,40.5262342,-113.8824849
11/17/2017,Plunger System,Plunger,Plunger,IPS,,Not Optimized,not optimized ,user_53,asset_181,48.2729261,-102.8610114
2/26/2019,Fuel Gas/Start Gas,Regulator,,,,,"Pad was shut in for HighHigh Tank. One of the condo tanks where hot oiled yesterday causing this to happen. Level dropped low enough to clear alarm. Verified flowing into different tank. We are. Separators still had gas in them but ESDs wouldn't open. Found all 3 fuel gas scrubbers ball checked. Drained them all and got ball to drop. Checked all dumps, they are clear. Relit glycol bath burners. Opened all ESDs and started cycles on all wells. Road into location will need to be bladed for trucks to make it in. Believe Chrissy was going to redefer back to Maint.",user_55,asset_220,,
8/20/2019,Instrumentation,Meter,Orifice Plate,Control Micro,4203DR,Passed Function Test,Check Communications between PLC and MVT; Tested Thru Sams System; Data and Graphing worked correctly. ,user_139,asset_2094,,
12/7/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,"Weather, freeze",user_84,asset_148,48.08609957,-103.545304
2/12/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,changed out worn dual pad with new dual pad,user_11,asset_305,48.1470144,-103.6180489
4/12/2018,Gas Scrubber Separator,Dump Line,,,,Erosion,CL 29-50 checked location drained scrubbers everything looked OK. ,user_71,asset_1574,48.1470144,-103.6180489
4/25/2018,Instrumentation,End Device,Topworks,,,Wiring,Issue: called out well shut in alarm Root Cause: really hard to trouble shoot. the (INT) doesn't show any reason why and i have been there a couple times and i cannot find any issues Fix: well turns right back on restarted the plunger cycles ,user_136,asset_841,48.2595694,-102.9009394
5/17/2019,Separator,Liquid Dumps,Seat/Ball/Piston,Norriseal,,Corrosion,"Valve bonnet , trim and seat were removed and found that the top seal in the bonnet section had failed, valve bonnet , trim and seat were replaced.",user_174,asset_1033,36.2491825,-90.9490505
5/6/2019,Instrumentation,Meter,Orifice Plate,Control Micro,4203DR,Passed Function Test,Complete Calibration,user_139,asset_1983,,
8/4/2017,Automation,Plunger Arrival Switch,,Tripmate,,,End of useful life,user_134,asset_1545,48.1584072,-103.6173515
9/27/2019,SWD System,Particle Filter,Process Indicator,,,,"Leak detection and monitoring wells gauged, ponds gauged. Pumped out leak detection on lower east cell, took about 60 minutes, level was 17"" to 15"". 9/26/2019 shut off generator to start getting ready for winter",user_31,asset_969,48.2556576,-102.8647072
9/14/2018,Pipeline/Piping,Pipe/Components,,,,Erosion Corrosion (Internal),We have sludge in the tank. To much for the strainer to handle. Have to remove and clean several times,user_55,asset_101,,
4/7/2017,Tanks,Valving/Swedges,Body,Other,Other,Corrosion,Valves leaking by,user_165,asset_419,48.16455574,-103.5471232
4/28/2018,Compressor,Compressor (Recip),Scrubber Level,,,,1st stage scrubber had fluid in it. Blew fluid for roughly 3 seconds ,user_107,asset_1001,,
11/1/2016,Automation,,,,,Other,No damages. ,user_92,asset_584,48.16025251,-103.6172268
5/26/2018,Separator,Fuel Supply System,Regulator,,,fluid,"Found and drained approximately 4 OZ of fluid in first scrubber on line heater. This is due to warm temperatures of fuel gas upstream (well flows at 120F) and the end devices (line heater scrubber) sitting at ambient temp (67 F).The pumps and burners are shut off for the summer, but fuel gas is still routed through to the line heater. If a bypass was built in to go around the unit we could keep fluid from filling up the scrubbers here, but that would send the fluid elsewhere. ENG to further trouble shoot and supply plan forward. There is a shut in sivals unit onsite that does not appear to be doing anything, we could utilize it as a fuel gas scrubber.",user_6,asset_1675,36.2541889,-91.2478009
6/7/2017,Dehy,WFS Issue,,,,,compressor down on high line pressure due to williams planned outage. line pressure came down put compressor back online,user_11,asset_835,,
9/1/2019,Fuel Gas/Start Gas,Regulator,,,,,"Well was shut in at choke. No tags, verified well had been flowing. Looks like possibly a new PSV. Brought well on, choke and Hi/Lo both working good. Had to replace a Dixon regulator to the Fisher Hi/Lo controller. RTP'd",user_55,asset_2195,,
3/10/2018,Automation,Antenna,,Bluewave,,Corrosion,Arrow failure. Dispatched to well making good volumes and positive flow trends. Incorrectly dispatched.,user_107,asset_634,,
4/4/2018,Separator,Manual Drain Valves,Ball/Seat,,,Corrosion,"Negative tested blow down cyclonic, tested good.",user_62,asset_2138,48.1470144,-103.6180489
5/15/2017,Pumping Unit,Engine,Clutch,Caterpillar,,Vibration,"Murphy CO-3 Actuator travel rod nut backed out and cross threaded, which prevented clutch from engaging. Attempted to replace nut, but had to replace actuator to RTP.",user_161,asset_939,40.5481548,-114.0112915
3/9/2018,Pumping Unit,Wellhead,Integrity Failure,,,,Went down on high pipe pressure,user_46,asset_1343,48.0614644,-104.8417043
8/14/2019,Flare System,Flare/Combuster,,,,,All SCCs out. Was able to relight 4 remotely. ! will not light. Had to light physically. Ignitor not working and pilot ESD not opening. Will write a work order.,user_55,asset_1919,,
3/23/2017,Instrumentation,Transmitter,3n1 MVT,Other,Other,Other,,user_113,asset_887,48.34968633,-103.6719103
3/30/2018,Tanks/Pits,Valving/Swedges,Body,,,Corrosion,Opened both condo tanks on location to operate battery as facility to maximize condo capacity onsite and align with predictive dispatch tools.,user_62,asset_2237,48.1470144,-103.6180489
3/11/2017,SWD System,Other,Other,Other,Other,Other,,user_117,asset_1489,36.2541889,-91.2478009
1/27/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,call gl compressor down-down on high discharge-drained -reset rtp comp.,user_131,asset_551,40.7126799,-114.1193569
4/27/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Drained desi while on location. No fluids present.,user_62,asset_1286,48.1470144,-103.6180489
9/26/2018,Tanks/Pits,Liquid Level Control,,,,,Issue: Arrow Dispatch for well Deferring 72mmcf Root Cause: once i got on location and performed a walk around that's when i found the location was being held out by a hi tank switch Fix: got with fluid management to get the tank hauled ,user_170,asset_1926,43.56424,-91.351691
10/10/2018,Chemical System,Pump,Plunger,Goulds,HBC1,Debris," Replaced methanol pump, collar that tightens packing was rusted and would not turn; pump was leaking product out of the packing weep hole, due to corrosion evidenced on packing adjustment collar. MEOH injection running at 1.5 GPD.",user_54,asset_1267,36.2535584,-91.2689312
3/29/2018,Chemical System,Pump,Packing,Goulds,HBC1,Wear,"Western meth pump, packing wore out due to use, replaced packing, rtp pump to service",user_35,asset_1976,48.19882506,-103.4823075
11/30/2017,Heater Treater,Burner,BMS,,,Pilot Went Out,Issue: burner out. (INT) shut down no pilot flame Root Cause: the durag (cat eye) is dropping the flame in the wind and shuts the burner down Fix: durag needs to be changed out with a thermocouple and or the druag needs to be a monitoring device not a shut down,user_136,asset_896,48.1602546,-103.6172966
3/18/2017,SWD System,Other,Other,Other,Other,Other,,user_117,asset_1489,40.5481548,-114.0112915
1/25/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"Vented well due to being loaded. Plunger arrived, vented casing down to 480 psi. Seems like well runs better with casing below 500. RTP'd well, started cycles, and return to optimizer.",user_141,asset_150,48.1470144,-103.6180489
5/11/2018,Flare System,Flare Header,Instrumentation,,,,LD 8-70 SCC callout. Relit SCC.,user_71,asset_539,48.1470144,-103.6180489
3/10/2018,Flare System,Flare Header,Instrumentation,,,,"Issue: called out SCC alarm. SCC (A) (INT) no pilot flame Root Cause: looks like both SCC's run off of one regulator and it cant be drained so it had some fluid in it that i drained out. but i wrote a work order i couldnt relight the SCC's remotely but i was able to relight right up with the sparker button. I don't think the sparker is working during remote lighting Fix: drained regulator relight and returned to service Along with the warmer weather i was able to drain all the ESD filters and blew all of them dry, Choke filters drained and blew all of them dry, drained desi, drained all three separator scrubbers and drained comp scrubbers as well",user_136,asset_601,48.1470144,-103.6180489
12/13/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_1633,48.1470144,-103.6180489
7/21/2017,Flare System,Flare Header,Process Indicator,,,,Relit scc. Probably due to weather ,user_156,asset_1892,48.2103371,-103.648858
9/14/2018,Tanks/Pits,Shell,Body,,Steel,Corrosion,"Found some new standing water in tank berm. Observed on HMI that on tank is lower than the rest. Went to tank, and dug around and found that it is very wet underneath top gravel, of tank 761605W. Went and checked other tanks, they were dry. Isolated tank, tagged it out of service. Contacted team lead and BJ to advise of findings. Contacted Chrissy to have IBEX come out and empty tank. Information only, we now have 2 of the 4 water tanks out of service on pad.",user_55,asset_365,,
2/14/2018,Flare System,Flare Header,Regulator,,,,Issue: found SCC #1 down on the HMI Root Cause: found fluid in the regulator. going from 48deg during the day to 18deg at night is causing and excessive amount of fluid to drop out of the fuel gas in the regulators Fix: drained the regulators and relight ,user_136,asset_1297,48.1470144,-103.6180489
12/8/2016,Wellhead,Cyclonic Valve,Actuator,,,Freezing,Froze in blowdown thawing,user_176,asset_1681,48.11411592,-103.5972654
2/21/2019,Surface Location,Lease Road,,,,Weather,Cannot access location due to snow drifts on lease road and turn around. Coded to get location plowed.,user_15,asset_807,48.2816237,-102.8553911
12/22/2017,Instrumentation,Transmitter,Differential Pressure,Rosemount,4088,Weather,,user_13,asset_1934,48.1470144,-103.6180489
2/23/2019,Pipeline/Piping,Pipe/Components,,,,hydrate, +SALES LINE IS FROZE BETWEEN THE SEPARATOR AND THE DEHY--NO METHANOL ON SITE TO PUT INTO LINE,user_34,asset_1810,48.224585,-103.8291059
9/8/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,"4"" load line valve on condensate tank found leaking",user_150,asset_2263,,
11/30/2017,Wellhead,Manual Valve,Wing,,,Fouling,"The wing and master valves on this well are FMC. And are really loose, the turns aren’t what there supposed to be, they need to be exactly 12 turns open from tight closed, the plunger was getting hung up on one or the other, depending on which one was off, ",user_84,asset_1983,48.05342318,-103.4833399
2/5/2018,Tanks/Pits,Shell,Body,,Steel,Corrosion,4” bull plug corroding. Will drain tank and replace plug. ,user_35,asset_486,48.21109529,-103.463917
5/10/2018,Automation,Cable,Data Cable,3M,,Electrical Short,"Scc 2 not controlling psi to scc , pinched back valve to scc up stream Scc 4 thermocouple error needs new thermocouple ",user_122,asset_1383,48.36576588,-103.7989115
2/17/2019,Tanks/Pits,Flare/Combuster,,,,,"Low pressure flare and 1 scc out, relit",user_31,asset_2034,40.5262342,-113.8824849
3/25/2018,Fuel Gas/Start Gas,Regulator,,,,,Adjusted pump speed,user_86,asset_662,,
12/12/2018,Chemical System,Piping,In-Line Check Valve,,,Debris,Check valve leaking through and the pressure was pushing methanol out of the breeder at the tank,user_21,asset_676,48.0883164,-104.8922287
2/7/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,"Got to location, wasn't able to get any pressure into the unit. Found the hi low was froze, threw my thaw tube on there and covered it with a blanket. Finally got pressure into the unit. Checked both dumps they were clear of any freezes. Got unit warmed up and called OPT to start a cycle. ",user_53,asset_618,40.7126799,-114.1193569
9/11/2019,Separator,Temp Control System,Heater/Burner,,,,found freeze on choke coil loop. broke freeze RFCA main burner was out and temp set too low. reset temps and surfaced plunger cause well was loaded.,user_121,asset_1876,46.2356189,-100.6010498
3/5/2018,Tanks/Pits,Flare/Combuster,,,,,"Lit SCC B. While on location, noticed SCC's were not lit. Pilot light on all 4 SCC's were out. Shut down all SCC's to let them purge, lit pilots and put them back in service. Cannot Identify root cause as to why they were out, i did not have to thaw or repair any thing to get them on.",user_62,asset_998,40.5960545,-113.9323891
11/10/2017,Separator,Temp Control System,Fuel Gas Supply,,,,"Find 4-PAC unit down on low unit. Zero vessel pressure. SCC's down as well. Jump gas to unit. Begin returning well to production after breaking freeze in fuel gas header. Could not break freeze with first well jumped. Had to move jumper to another well to break freeze. All wells were in an off cycle at same time with pumps, burners and SCC's running dropped pressure enough to trigger ESD's. Buy back schedule dated 10/6/2017 shows buy back meter installation scheduled for the week of 11/13/2017. Return well to operation. Continue with other wells on pad. Relight SCC's and bath. Drain desi of minimal fluid. Longer wrench time due to having to break fuel gas freeze. ",user_75,asset_1332,,
4/14/2018,Generator,Engine,Fuel Gas Supply,Cummins,,Weather,This is a diesel fueled generator. Ran out of fuel,user_141,asset_1489,48.0711909,-104.844295
7/5/2018,Compressor,Intrumentation,,,,,"see tdxm temp scan code 27, no issue found cleared alarm and started compressor, monitored temps , flowing 5.3mmcfd , loaded compressor flowing 7.5mmcfd",user_122,asset_701,43.252261,-115.0567324
1/1/2018,Fuel Gas/Start Gas,Coalescer/Filter,Level Controller,,,,Drained desi last Friday. Checked today no liquid. ,user_156,asset_2051,48.23906641,-103.6177726
3/1/2018,Plunger System,Plunger,Plunger,PCS,,Corrosion,"Pulled and inspected old Venturi plunger, dropped new 6 shooter bypass",user_35,asset_369,48.20569877,-103.5011501
12/8/2017,Tanks/Pits,Liquid Level Control,,,,,Lost unit pressure for high tank.,user_48,asset_1054,48.24745402,-103.7007184
12/4/2017,Compressor,Compressor,Instrument Gas Supply,Ajax,,Freezing,Issue: compressor down on low suction pressure Root Cause: found the regulator to the recycle valve froze. Fix: pulled regulator thawed out drained line and returned to service. all the fuel gas on this location is wet scrubber need drained daily in colder temps ,user_136,asset_224,40.5262342,-113.8824849
4/27/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_1489,48.1470144,-103.6180489
6/8/2019,Separator,Choke Valve/Loop,,,,Trash,Dvc was not closing the choke on the off cycle and the well flowed out. DVC was filled with paraffin/ cleaned and function tested.,user_10,asset_1862,40.5262342,-113.8824849
2/16/2018,Automation,Antenna,,Bluewave,,Electrical Short,"Pad was down on COMM ERROR. Contacted automation, they reset the PLC remotely. They stated the Radio card is going bad and have one on order. It should be in next week. Until the card comes in and gets installed, power cycling the PLC resets the COMM ERROR for a few days and we can run the pad. Performing the power cycles shuts the pad in due to no power to any end device. RTP well on plunger cycles.",user_62,asset_175,48.1470144,-103.6180489
4/15/2018,Compressor,Compressor (Recip),Scrubber Level,,,,2nd stage scrubber had fluid in it. Blew for an est time of 4 seconds,user_107,asset_570,,
3/9/2018,Recirc Pump,Pump,Bearings,Sunpumper,375,Weather,Found pump supply air turned off. After a walk around I found no reason for pump to be off and returned pump to service to thaw equipment.,user_107,asset_1721,,
6/11/2019,Pipeline/Piping,Valves,,,,End Of Design Life,Ready crew loto'd the check valve. We opened check valve and it had came apart and the flapper was lying half blocking the discharge side. Reinstalled the lid and left the guts out of valve. ,user_55,asset_2112,,
7/27/2019,Plunger System,Plunger,Plunger,PCS,,Corrosion,"Plunger has been missing arrivals since 7/8 and cycling . Well is very loaded, vented plunger to surface and inspected . Plunger was worn out installed new plunger and rtp'd well back in cycles.",user_10,asset_536,39.2506642,-92.4357879
9/9/2019,Compressor - Gas Lift,Compressor,Process Gas Supply,Leroi,,Freezing,Call out compressor down on high discharge blew compressor down left open to atmosphere while I re-lit flare and 2 SCC's that i re-lit yesterday. All issue weather related due to temps and wind with heavy rain.,user_63,asset_2046,,
5/11/2018,Automation,Tower,Antenna,,,Weather,"was down for programming issues back up, brought back up",user_88,asset_251,48.1471577,-103.6180098
12/29/2017,Fuel Gas/Start Gas,Regulator,,,,,"Durag to fire eye tripped, had to reset, work order put in to have automation look at, ths has happened a few times and apparently has been a problem in the past before this was my well site",user_88,asset_84,48.2594063,-102.9010365
1/29/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,"froze in cont actor, notified wfs. low priority. but pat will get to it, hole in TEG, heat trace, not much he can do. ",user_77,asset_867,43.8924729,-117.7282144
11/20/2017,Dehy,WFS Issue,,,,,dehy is froze ,user_53,asset_178,48.160134,-103.6170233
6/4/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_2012,48.1003415,-103.5854403
4/13/2017,SWD System,Other,Other,Other,Other,Other,Cracked cement.,user_117,asset_533,36.2541889,-91.2478009
2/14/2018,Gas Scrubber Separator,ESD,,,,,pad went down on valve fault. caught pad before it totally ran out of gas and restarted remotely.,user_71,asset_1785,48.1470144,-103.6180489
2/28/2019,Chemical System,Pump,Instrumentation,Sunpumper,113,Electrical Wiring,Solar glycol pump is down. Fuse is ok and would not reset on battery disconnect. Loss of pump caused dumps to freeze and flood out fuel gas system,user_147,asset_660,,
2/12/2019,Surface Location,Well Pad,,,,Weather,"The access road, turnaround and surface equipment needs snow plowed or removed. ",user_68,asset_638,48.20234333,-103.5986981
11/28/2017,Automation,Plunger Arrival Switch,,EDI,,,"No power at well head , transmitters have no power ",user_122,asset_2005,48.35173549,-103.8058823
10/8/2017,SWD System,Particle Filter,Element,,,,Replaced filters due to low suction on pump and restart pump.,user_141,asset_1633,40.5960545,-113.9323891
3/27/2019,Separator,Choke Valve/Loop,,,,Freezing,"Inlet freeze between hi-lo and coils, thawed and broke freeze. No insulation on hi-lo valve. ",user_44,asset_180,,
8/4/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,The valves on the water tank load line are leaking causing loss of 2gl on the out side with f the berm ,user_102,asset_1400,48.06681487,-103.6961351
3/2/2017,Chemical System,Pump,Check valve,Other,Other,Debris,,user_50,asset_1485,47.96911188,-103.4404864
2/28/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Drained scrubber on cabinet A while on location RTP pad. No fluids present.,user_62,asset_635,48.1507625,-103.6206926
1/9/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_2012,48.1004898,-103.5858588
3/31/2018,Tanks/Pits,Flare/Combuster,flare knockout drain pot,,,,Drained fuel gas knock out pot for SCC pilot fuel gas. Less than 1 cup of water drained.,user_62,asset_2046,48.1470144,-103.6180489
1/22/2018,Compressor,Engine (Gas),,,,,D-4 supply gas froze,user_111,asset_1623,48.09437863,-103.3426452
7/1/2019,Sales Valve (PV),Cyclonic Valve,Gate/Seat,,,Fouling,Attempted rtp after repairs were done. Pressured up equipment and found the cyclonic leaking out stem,user_81,asset_1099,48.17079824,-103.5946951
3/16/2018,Gas Scrubber Separator,ESD,,,,,"not openi g, locked programming issue",user_88,asset_1388,48.2628623,-102.8996151
2/7/2019,Gas Scrubber Separator,ESD,,,,,"Fuel gas line with some liquid causing the the ESD regulator to froze, keeping the ESD closed. ",user_83,asset_104,40.5262342,-113.8824849
2/27/2019,Flare System,Flare Knockout,Instrumentation,,,,"team leader dispatched mike martinez and i to location.2' 1502 iron that was split has now been replaced and all other piping has passes UT inspection according to previous code. before beginning work we confirmed two inch line had been replaced.above ground flowline was completely drifted over and master valves where frozen open with no pressure to sand can or valve manifold/choke. we called team leader and requested a steamer/loader to clear snow where we could get in and access equipment. we started on wellhead with steamer, thawed out master valves until we able to isolate both valves with 13 turns. made are way from wellhead to sandcan with steamer and eventually got flowline freeze to break. once we got pressure to mainfold we installed a jumper from the mainfold pass the esd. filled green complete unit with 100 psi and was able to get esd open.water dump off green complete unit was froze out to the pit/scud. we used steamer to break freeze.isolated green complete and injected into line with warm water.got it to break. had freeze from sales on green complete unit to high pressure unit, which we also broke with steamer. thawed out fuel gas header sytem and got pressure over to fuel gas separator which also has the glycol pumps. lit burner and started circulating glycol.back pressure valve on heater treater was froze, thawed out with steamer.water dump on LP was froze thawed with steamer. got everything nice and warm and started selling gas opening choke to 20/64.oil dump on LP unit is open to tanks.currently baby sitting choke flowing around 5.2 at 78 degrees, with temperature increasing(well flows hot).out at the flare the containment around the KO pot is filled with around 20 inches of ice,so we are unable to drain it. tried thawing this out with steamer but no luck. may need to set heater on containment tub and find a way to drain tub/get it sucked out.going to have night ops do a site visit tonight to insure well stays flowing with no issues. well rtp",user_120,asset_796,43.56424,-91.351691
11/14/2018,Separator,Temp Control System,Fuel Gas Supply,,,,Pilot went out due to high low freezing and running out of unit pressure. Lit pilot. ,user_15,asset_1054,48.2815208,-102.8554263
11/3/2019,Separator,Fuel Supply System,Regulator,,,fluid,"Pad lost pressure. Jumped pad back online. Started cycles on the 10, 110, and 160 well. Using the 70 for winter operations, it is in engineering. Relit bath heater and SCCs. Adjusted temp on bath heater. Blew down scrubber.",user_55,asset_1063,,
8/14/2018,Separator Inlet Valve (XV),Sales Valve,Body,Valvcon,,Grease Washed Out,"wasn't sure what to put for the choke, found it 1/2 turn open, rtpd",user_77,asset_1865,46.0240507,-101.4208674
10/24/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"plunger not coming in , well is loaded and have been vented multiple time's contacted PE",user_144,asset_704,48.1475348,-103.6185209
12/22/2017,Compressor - Gas Lift,Compressor,Cylinder,Ariel,,Liquid Carryover,gas lift compressor down on high cyclinder 2 discharge temp. opened a couple of louvers and returned gas lift back into service,user_11,asset_1264,48.1470144,-103.6180489
8/22/2019,Tanks/Pits,Piping,Load Line,,,Freezing,Removed all load lines and recap inside load line valves,user_21,asset_1783,48.1070664,-104.8936909
11/8/2019,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,Blow down cyclonic replaced and returned to service,user_21,asset_1614,46.2356189,-100.6010498
6/15/2018,Separator Inlet Valve (XV),Pneumatic Control System,Regulator,,,,"Hi lo trim leaking. Replaced, tested and rtp",user_35,asset_1295,47.99569316,-103.4044511
2/26/2017,Compressor,Compressor,Instrument Gas Supply,Other,Other,Other,Knocked compressor down on various issues,user_88,asset_2089,48.26314854,-102.8996255
11/14/2017,Automation,Radio,Wiring,3M,,Unknown,comp callout pad shut in on comm error.,user_71,asset_1159,48.1470144,-103.6180489
12/9/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Trash,JW Power replaced broken wire that was chewed through by a rabbit on WH compressor. Compressor is back online. Gas lift compressor was down for lack of fuel supply to run engine with WH compressor down. Restarted compressor and put back online.,user_141,asset_1264,48.1473689,-103.6174915
7/5/2019,Separator,Choke Valve/Loop,,,,Freezing,"Arrived on location and pulled history and did location walk down. Found well was down on missed plunger arrivals. Using my super slooth detective skills, i found the choke was not opening during the on cycle and then causing the well no to get arrivals and shutting in. Checked gas supply to front end choke and found some fluids in the Kimray drip pot. Drained drip pot and tapped on DVC. Choke then opened. ",user_15,asset_255,39.2506642,-92.4357879
11/22/2018,Separator,Temp Control System,Pilot,,,,Fuel gas was dry and pilot tip was clear. Looks like burner blew out. Relit pilot and tested main. No issues found,user_120,asset_2135,48.36310132,-103.7895339
11/8/2017,Plunger System,Plunger,Plunger,PCS,,Not Optimized,PCS Spiral Bar was missing arrivals and slipping fluid causing liquid loading. Change out to dual pad to better carry fluids and optimize arrivals. ,user_75,asset_816,,
11/20/2017,Instrumentation,Controller,,,,,KELVIN IS LETTING THIS WELL SIT ON LOAD RATIO FOR WAY TOO LONG. WELL IS DEFERRING!,user_53,asset_181,48.160134,-103.6170233
10/17/2018,Separator,Temp Control System,Coils,,,, WELLHEAD MASTER VALVES ARE LEAKING BADLY THROUGH THE STEM AREA- CAN NOT INSTALL STEM PACKING DUE TO HARD LINE HEAT TRACE BEING IN THE WAY.,user_34,asset_1645,43.56424,-91.351691
12/8/2018,Tanks/Pits,Liquid Level Control,,,,,"Walk through, take readings. No issues found at this time. Ibex brought some water up last night. Sump at offload will need to be pulled. Will not pump when it gets cold and freezes. Will have them pull the pump building sump too.",user_55,asset_1489,,
3/15/2017,Recirc Pump,Pump,Check valve,Other,Other,Wear,,user_149,asset_780,48.224585,-103.8291059
4/14/2017,Tanks,Valving/Swedges,Seat/Ball/Piston,Other,Other,Other,,user_173,asset_2036,48.1602457,-103.6174073
3/2/2017,Heater Treater,Firetube,Firetube,Other,Other,Other,"Froze water dump and flow line, I got unit warming up and pumps going. Will come back to this later, on top deferral,",user_84,asset_1468,48.1368082,-103.525474
9/3/2019,Separator,Choke Valve/Loop,,,,Corrosion,The choke was leaking out through the stem. All the internal parts were replaced.,user_68,asset_496,48.1470144,-103.6180489
2/22/2018,Separator,Choke Valve/Loop,,,,Freezing,Choke froze,user_86,asset_589,,
1/14/2019,Fuel Gas/Start Gas,Regulator,,,,,Fuel gas frozen ,user_153,asset_2279,48.3030485,-103.6608666
3/1/2018,Sales Valve (PV),Sales Valve,Body,Valvcon,,Freezing,Froze in valve ,user_126,asset_1040,,
5/14/2018,Compressor,Compressor,Scrubber Level,Sullair,,Freezing,compressor down on high first stage scrubber level ENG working fix in interim,user_6,asset_1383,36.2541889,-91.2478009
11/6/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,Issue: Arrow Dispatched for Deferral Root Cause: well was logged off bad Fix: unloaded well returned to service and coded the well for the cycles to be relooked at. ,user_170,asset_278,48.224585,-103.8291059
5/8/2019,Automation,RTU,CPU,Schneider/Scadapack,Scadapack P4A,Wear,"THIS WAS A YOKOGAWA FCN, AND THE ROOT CAUSE WAS A CORRUPTED FILE. CAN WE PLEASE GET THE DROPDOWNS UPDATED WITH ACCURATE INFORMATION?",user_12,asset_243,40.5262342,-113.8824849
1/24/2019,Separator,Liquid Dumps,Diaphragm,Norriseal,,Corrosion,"Diaphragm in bonnet was cut, replaced bonnet",user_94,asset_1401,48.072976,-103.3906336
10/4/2019,Separator,Choke Valve/Loop,,,,Freezing,Pad continues to shut in due to pumps and burners. RTPd pad and left well 20 in end cycle to stay pressured up and keep pad up.,user_18,asset_1524,,
1/21/2017,Automation,POC,Relay,Cameron,POC,Weather / Improper Enclosure,Tank level switch on water tank is frozen or bad and needs trouble shot repaired or replaced. Thanks ,user_175,asset_934,48.04143849,-103.5397805
11/13/2018,Fuel Gas/Start Gas,Regulator,,,,,TRANSDUCER FROZE AND PART THE SCRUBBER,user_121,asset_1898,48.3580576,-83.27272
2/1/2019,Separator,Shell,Body,,Steel,UV Degradation, +TURN AROUND BLADED CLEAR OF SNOW *NEEDED TO CLEAR SNOW FROM AROUND EQUIPMENT FOR ACCESS,user_34,asset_892,48.1508,-103.6191904
3/14/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,Opened well to flow but could not verify five minutes of flow. Well loaded or frozen. No methanol onsite. Pump functional. OPS ordered methanol. Sign on well head states plunger installed. OPS to treat as if plunger is in well. Without five minutes of flow OPS cannot verify whether or not tubing is frozen. OPS pinched the choke on the unit and equalized casing around to tubing to help with possible hydrate or to drain fluids out of tubing in case of BSSV. OPS to return 3/15 and attempt to flow out plunger and vent as needed.,user_6,asset_1990,36.2541889,-91.2478009
4/7/2018,Sand Separator,Manual Drain Valves,Body,,,Corrosion,"drained sand trap, little bit of sand in the trap, no big issues found on location",user_122,asset_1383,,
12/9/2017,Dehy,WFS Issue,,,,,"Dehy dump hung open since the 5th of December, looking at the graph. Adjusted the dump, well is rtp'd",user_163,asset_1758,48.1470144,-103.6180489
2/5/2018,Compressor - Gas Lift,Compressor,Valves,Gemini,,Freezing,compressor went down on high discharge pressure.the 140 had a freeze on the casing / Meth was pumping but tank is low will but in a meth order for the 140 well. Broke freeze and RTP compressor and both wells,user_100,asset_863,48.1470144,-103.6180489
3/24/2017,Instrumentation,Transmitter,Other,Other,Other,Other,,user_99,asset_2018,48.3619066,-103.2129855
12/3/2017,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"Kicked well on due to non arrivals. Paused opened and watched. Plunger came in, restarted cycles.",user_141,asset_1856,40.5262342,-113.8824849
4/22/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,well was missing plunger arrivals,user_179,asset_372,48.1470144,-103.6180489
7/19/2019,Separator,Choke Valve/Loop,,,,Trash,"Pressure up unit and flowed out well until pressure came down before i put well in cycles, had some trouble with the dvc on the front end choke drained fuel gas and cleaned i/p function tested and rtp'd well. Contacted optimizer to adjust cycles until pressures are back to normal.",user_10,asset_1021,39.2506642,-92.4357879
4/24/2019,Fuel Gas/Start Gas,Regulator,,,,," +FOUND DVC HOLDING THE CHOKE OPEN. * CLEARED THE DVC BLOCKAGE, DRAINED THE LIQUIDS OUT OF THE FUEL SUPPLY LINE, OPERATED THE CHOKE OPEN AND CLOSED SEVERAL TIMES TO VERIFY OPERATION. AND PUT WELL ON CYCLE",user_34,asset_1404,43.56424,-91.351691
1/23/2018,Separator,Choke Valve/Loop,,,,Freezing,,user_126,asset_1081,,
3/8/2018,Wellhead,Casing,Intermediate Casing Head Valve,,,,"Flow line is frozen, had left it open AGT overnight. When i got to location i opened TBG to AGT and flow line is still froze. SI TBG master valves and left flow line open to AGT Rocked the CSG back and fourth. Dumped 2.5 gallons of methanol into flow line and let sit on freeze. Pressured up flowing with the CSG and it started breaking freeze. Bled off flow line and did it again. Finally freeze broke. Opened TBG master and got pressure to the BD valve. Started cycle and RTP'd well ",user_53,asset_1867,48.2649339,-102.8791315
2/23/2018,Flare System,Flare Header,Regulator,,,,"Tci losses fuel gas to pilots daily in cold weather, keeps freezing in flex line coming out of the heat trace an insulation at inlet of scrubber knock out pot, and freezing off at both 1/4” regulators at the tci, needs heat trace and insulation on supply gas line all the way to the regulators at tci ",user_122,asset_1675,48.38745347,-103.8420631
5/28/2018,Compressor,Compressor (Intergral),Process Gas Supply,,,,5 mile 31-comp B down on high discharge. RTP went back down 2 hours later didn’t make it back to location.,user_71,asset_1620,48.1470144,-103.6180489
3/27/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,fluid,"Checked scrubbers onsite and found fluid in the first scrubber at the line heater. Found water in the first scrubber and drained approximately 1/2 oz of water in first scrubber on line heater due to warm temperatures of fuel gas upstream (first unit 110 F, 88 F at first scrubber on HP unit, 85 F at fuel gas LP unit, 88 F on stainless piping as it nears the scrubber, 58 F at the first scrubber on the line heater.) Well flows at 120 F, ENG to further trouble shoot and supply plan forward. There is a shut in sivals unit onsite that does not appear to be doing anything, we could utilize it as a fuel gas scrubber.",user_6,asset_1675,36.2541889,-91.2478009
2/13/2017,Pumping Unit,Engine,Control Panel,CUMMINS,Other,Other,,user_179,asset_387,48.0252641,-103.4868428
2/26/2017,Gas Scrubber,Mechanical Dump Valve,Controller,Other,Other,Other,Freeze to DVc and ESD ,user_88,asset_2045,48.26314921,-102.8996277
5/27/2019,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"attempted to vent the plunger up and change out. Left open for hour, tubing blew dead, casing climbed the whole time, deferred to Engineering to look at.",user_106,asset_1966,48.1475232,-103.6191904
2/20/2017,Automation,Other,,Other,Other,Other,RTU did not automatically download from the Host system.,user_65,asset_1608,48.3619066,-103.2129855
6/25/2018,Automation,RTU,Wiring,Schneider/Scadapack,Scadapack P4,Human Error," 5. Continental Divide 32-1 - test high tank shut-in and callout • Tested both tank switches • Water tank switch failed • Found bad sensor in switch, switched over to other set of switches inside HLA switch • Tested and verified all switches functioning correctly now • Tested high tank shut down • Solenoid did not shut in well • Troubleshot issue • Found close pulse not making it all the way solenoid • Found scada mis-wired on relays • Relay 0 did not have positive ran to it • Corrected wiring issue • Tested and verified solenoid now opens and closes correctly • Tested and verified that high tank shut in now shuts in the well Notified operations",user_92,asset_327,43.252261,-115.0567324
8/21/2018,Flare System,Flare Header,Instrumentation,,,,1 of 2 SCCs out relit and returned to service ,user_63,asset_2062,48.40595648,-103.5807762
3/3/2019,Wellhead,Casing,Braiden Head,,,,"High water tanks. SI pad and compressor was down. Solar glycol pump is still not working. Need heat trace to the compressor and injection line reconnect a sand piper for this. 85 well, compressor down, found compressor down on low compressor oil pressure. got it restarted and allowed compressor to start up. After it was warm i loaded it. It ran for a hour or so and then went down on high discharge pressure. Onskid bypass is froze, finally got pressures bled off and restarted the compressor. It went down again. Found that the injection line at the CSG is froze. Started thawing on it. Isolated line and CSG and bleed down to get it to break freeze. Started compressor again and started injection. We are injecting but with no heat at the compressor and no this injection line we will be going down due to a freeze again. 160 well. compressor down, found compressor down on low compressor oil pressure. got it restarted and allowed compressor to start up. After it was warm i loaded it. It ran for a hour or so and then went down on high discharge pressure. Onskid bypass is froze, finally got pressures bled off and restarted the compressor. It went down again. Found that the injection line at the CSG is froze. Started thawing on it. Isolated line and CSG and bleed down to get it to break freeze. Started compressor again and started injection. We are injecting but with no heat at the compressor and no this injection line we will be going down due to a freeze again. 90 well, found well had not produced any volume yet. Started a cycle and found that the sales line is froze. Thawed on this line it it cleared and then started cycle again. ",user_56,asset_1623,48.1470144,-103.6180489
5/19/2017,Wellhead,Tubing,,,,,Flow line froze see comments on resolution ,user_131,asset_1498,48.00455648,-103.7338967
2/16/2018,Tanks/Pits,Flare/Combuster,,,,,SCC was out. Pressure to pilot 6lbs. Turned up to 8. Rtp SCC,user_153,asset_1232,48.17178409,-103.5941352
10/14/2017,Compressor,Skid, back pressure valve,,,Weather,Williams was down and caused high line pressure,user_51,asset_1408,40.5262342,-113.8824849
7/27/2018,Flare System,Flare Header,Instrumentation,,,,Issue: called out SCC down alarm Root Cause: the on board computer shows its still shutting in on Master Power Fix: Using the on board computer i rest and got it to restart up using its sequence ,user_170,asset_1383,48.1470144,-103.6180489
4/22/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,well was missing plunger arrivals,user_179,asset_786,48.1470144,-103.6180489
9/24/2018,Chemical System,Pump,Packing,Texam,HBC1,Electrical Wiring,"Pump leaking out of packing weep hole, OPS could not pull packing housing to replace, created WM for MAINT to attempt fix and tagged pump.",user_54,asset_907,48.1489648,-103.6197021
2/27/2018,Separator,Choke Valve/Loop,,,,Freezing,"Suspect that the choke or high low froze off during bad weather days and broke on it's own. Methanol tank is empty, will put in for refill. Location put back to sales.",user_49,asset_549,48.32696527,-103.6237103
4/19/2018,Tanks/Pits,Flare/Combuster,,,,,"Did hand over with maintenance team. They added a down stream cyclonic on the 29-2 also installed a check valve in the sales line so the 120 wouldn’t back feed through sales into the 29-2. Meet with well site leader onsite, they are pulling tubing on the 2, but our currently shut down. Explained my job scope and how they would be effected.Maintenance team and I pressure tested there work using 100 psi from the 29-2. No leaks were found.cleared high tank alarm on hi/lo. Brought on well split flowing to blowdown and selling to Williams on a 16/64 choke. Currently flowing around 2.0mil. Lit line heater and separator bath. Will continue to open choke waiting on temp to increase on sales current temp is 43degrees. Relit scc’s ABC. Well rtp",user_172,asset_599,,
3/21/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Drained desi while on location working on well 30. Desi was dry, no fluids present.",user_62,asset_1187,48.1470144,-103.6180489
2/13/2018,Chemical System,Piping,Supply Line,,,Vibration,Vibration caused the regulator supply to back off to 20 psi. Increased to 30 psi and pump began moving methanol. See full resolution comments below. Arrow dispatch for Fed based gauge. Gauge oil and water tanks. No hauler action requested. Pull graphs while on location. Find plunger missing arrivals. Graph indicates the plunger is freezing in lubricator. Pull coding history to find out if well has had this failure in the past. Confirmed well has a history of hydrate hanging plunger in lubricator. Check methanol. Tank over 90% full. Find methanol pump stalled out. Regulator backed off due to vibration to 20 psi. Increase back to 30 psi and methanol begins injecting. Find choke at 30/64”. Rate is controlled on this site by the cyclonic downstream. Open choke to 64/64”. Well head recently re insulated. Valve access on tbg and csg sweep not cut back to access for actuation. Cut insulation back for valve access. Dig out dirt accumulation on berm stairs to tank. No further action needed. ,user_75,asset_494,,
3/29/2018,Pipeline/Piping,Pipe/Components,,,,Human Error,Open separator condensate dumps to all condensate tanks due to pipeline issues,user_163,asset_2213,48.1470144,-103.6180489
1/18/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Found the Kimray drip pot on ESD to be full of liquid. Found the fuel gas for the location was not routed correctly through desi dryer to more thoroughly dry the gas. Corrected valve position and drained liquids from drip pot. While on location, checked the WFS dehy and saw the meter for Buy back has been installed. I will check the MOC to make sure we are good to commission the buy back meter to start getting dryer gas to the end devices.",user_62,asset_1092,48.1470144,-103.6180489
1/13/2019,Instrumentation,Meter,Orifice Plate,Nuflo,4203DR,Freeze,Frozen liquid on meter,user_153,asset_1740,48.22234319,-103.6360259
1/8/2019,Tanks/Pits,Tank Level,Probe,,,Calibration Issue,"Got to location and found that tank had filled up and had sprayed out when the unit dumped. Level of tank was 20' 6"" x 3' 9"" froze at 2 feet Went through unit and didn't find any issues. Water dump was clear, condo dump was clear as well. Unit bath was good, unit didn't have any pressure but it was still warm. pressured unit up and got heat trace going. Shut condo dump inside of cabinet and tagged it. Pinched choke and tagged it as well. Notified TL. I will write WM for automation to check if it has a hi level switch and if so then why it failed. Also will write WM for maintenance to come steam clean the stairs and tanks.",user_56,asset_1817,48.224585,-103.8291059
6/22/2017,Tanks/Pits,Shell,Body,,Steel,Corrosion,Blowdown failed due to internal corrosion caused by MIC,user_150,asset_1611,,
11/10/2016,Gas Scrubber,Back Pressure Valve,Seat/Ball/Piston,Other,Other,Corrosion,Bleeds by,user_105,asset_692,47.91294073,-103.6408048
12/22/2018,Separator,Choke Valve/Loop,,,,Freezing,Found tubing transmitter froze due to heat trace pumps (electric) not pumping enough to keep every thing thawed out. Thawed out transmitter. ,user_15,asset_1152,48.1470144,-103.6180489
11/9/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_1633,,
9/13/2018,Compressor,Intrumentation,,,,,"down an emergency stop switch, button was not pressed, no issue found, restated comp and monitored ",user_144,asset_2073,48.1458495,-103.6162571
4/20/2018,Separator,Back Pressure Valve,Body,Kimray,,Corrosion,Cyclonic valve - stem packing wore out and leaking to atmosphere ,user_105,asset_2242,48.19643496,-103.6194662
2/19/2019,Surface Location,Lease Road,,,,Weather,"Attempted to go to location, snow is to drifted in on roads into location to make it in. Road into location needs bladed.",user_15,asset_787,48.2816106,-102.8553863
4/20/2018,Heater Treater,Dump Line,,,,Freezing,Checked for fluids on heater treater scrubber pot. No fluids present.,user_62,asset_1383,48.1470144,-103.6180489
2/25/2018,Fuel Gas/Start Gas,Regulator,,,,,"Issue: well called out shut in alarm. (INT) valve falut Root Cause: found the scrubber filled up and ball checked and took down whole cab (C). do to the colder weather a temperature fluctuations the scrubbers and desi are going to need to back drained more often than normal. Fix: drained the desi, thawed out the water dump line and got the scrubber to drained. turned well back on",user_136,asset_1347,48.2594584,-102.9010654
12/31/2017,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"Vented well due to being loaded. Plunger arrived, RTP'd well, started cycles, and return to optimizer.",user_141,asset_1845,48.1470144,-103.6180489
8/16/2018,Instrumentation,End Device,Asco,,,Water, 9. Five Mile 31-110 - ESD wont open • Found Asco Solenoid not outputting air • Verified good signal to Asco • Removed failed Asco • Installed new Asco • Tested and verified good ,user_38,asset_521,36.2551968,-91.268112
8/4/2017,Automation,Radio,Wiring,Cellular,,End Of Useful Life,This is for the Cambium PMP100 radio. ,user_134,asset_500,48.1584072,-103.6173515
1/16/2019,Separator,Liquid Level Control,,,,,"condo dumpline freeze broke and took unit down, displacer arms froze in vessel, RTP separator and shut dumps to keep unit up choke is cracked to move warm gas into unit from bath,",user_37,asset_2040,43.56424,-91.351691
5/19/2017,Instrumentation,Transmitter,3N1 MVT,Rosemount,4088,Wiring,WFS repaired their meter. Repaired our card and established comms. Verified production data updating in Reflections.,user_99,asset_397,48.1470144,-103.6180489
2/26/2018,Dehy,Contactor,Flow Controller,,,,Dehy froze,user_111,asset_286,48.02824043,-103.3719474
11/23/2017,Flare System,Flare Header,Process Indicator,,,,,user_48,asset_1643,,
9/22/2019,Fuel Gas/Start Gas,Regulator,,,,,"Inline pressure regulator for 3/8 tubing / stainless line for SCC has a bad gauge and cannot tell how much gas the pilot is getting. The 1/2"" ball valve at the SCC is pinched back because of this, need to replace inline regulator with new one so pressure can be set and 1/2 inch valve can be opened fully",user_22,asset_2232,46.2356189,-100.6010498
1/6/2019,Fuel Gas/Start Gas,Regulator,,,,,"Issue: sight down getting hot oiled turn back on Root Cause: Human Error, when the sight was shut in no one opened up the buy back gas line and the sight went down and froze everything up Fix: got the buy back open relight all three burners and got the sight warming back up.",user_170,asset_2001,43.56424,-91.351691
10/14/2019,SWD System,Particle Filter,Element,,,,"200"" of H2O on filter DP. Changed filters. Currently down on low level. Turned condo in to have mud pulled from tank",user_31,asset_523,48.2663072,-102.8745376
6/25/2018,Tanks/Pits,Liquid Level Control,,,,,High tank alarm knocked pad down automation tech on site to repair pad rtp’d ,user_58,asset_1915,48.37174012,-103.5206297
4/12/2017,Gas Scrubber,Other,,Other,Other,Other,,user_35,asset_2066,48.42007018,-103.6290932
11/12/2018,Chemical System,Pump,Packing,Goulds,HBC1,Wear,"OPS: Paused well on and ensured plunger arrival, witnessed normal plunger arrival but left paused open and unloaded the well with one post plunger arrival slug. Restarted cycles. Plunger is experiencing hydrates not allowing it to drop all the way down hole. Checked MEOH injection system and confirmed sufficient chemical level but ordered more. Pump is leaking out of packing, OPS attempted to tighten tension collar but was unable to stop leak. OPS did not have sufficient replacement packing on hand to fix and ordered more. OPS left pump tagged out until parts can arrive and be installed. WM created. OPS to replace and verify no leaks and up rate of injection to help inhibit fast arrivals.",user_54,asset_1274,48.0831902,-104.8694549
4/17/2017,Tanks,Valving/Swedges,Seat/Ball/Piston,Other,Other,Corrosion,Valves leaking by,user_165,asset_141,48.224585,-103.8291059
1/19/2018,Flare System,Flare Header,Instrumentation,,,,Mon 11-150 checked location. flare was out relit flare and drained scrubbers everything looks good. ,user_71,asset_2046,48.1470144,-103.6180489
1/2/2018,Compressor,Compressor (Recip),Dump Valve,,,,"Compressor went down on hi scrubber level, i drained each scrubber just fine. next time when Archrock is on location doing a PM i will ask them to look into the dump controller.",user_53,asset_1365,36.2541889,-91.2478009
1/7/2019,Separator,Liquid Dumps,Float,Kimray,,Freezing,Float inside unit froze causing controller to keep dump open causing well to go down. Bumped t-12 up a little bit to hopefully remedy any future issues.,user_147,asset_6,,
4/28/2019,Separator,Water Meter,Body,,,Corrosion,Hammer union for the water meter is weeping,user_22,asset_852,46.2356189,-100.6010498
6/11/2018,Separator,Fuel Supply System,Regulator,,,debris,Pressured separator up. Not sure why it lost pressure. Possible dirty block and bleed. Checked for leaks. Found none. RTP ,user_156,asset_245,48.20344538,-103.6283076
8/29/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_1633,,
12/9/2016,Gas Scrubber,Dump Line,,Other,Other,Trash,Thawed gas supply to glycol pumps,user_62,asset_1600,,
11/10/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Find freeze in fuel gas header while jumping wells back on in 4-PAC unit. Drain desi can and find fluid present. Root cause suspected liquid carry over. Break freeze by jumping multiple wells and getting bath heater relit. ,user_75,asset_1811,,
8/11/2017,Instrumentation,Controller,,,,, 3. Five Mile 31-130 - DVC not actuating correctly • Got to site and tested DVC • DVC tests good • Found no issue • Called optimizer and he said that everything is working correctly now No automation issue,user_92,asset_296,48.3619066,-103.2129855
5/8/2017,Automation,RTU,Board,Schneider/Scadapack,Scadapack P4,Wear,RTU was reading a false high tank and sales line cyclonic was out of sync. Operator removed actuator from cyclonic and got back in sync and cleared false high tank in RTU with vision meter ,user_7,asset_1898,48.01349649,-103.5445883
12/14/2016,Gas Scrubber,,,,,,Gas scrubber and pilot were frozen. Thawed them up and light up burners.,user_60,asset_1197,48.3243812,-103.5870367
6/30/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,"DEFERAL CB 1-2 well was on deferral list. Choke was froze and unit was down. Broke choke freeze and RTP unit, got choke fully open after an hour.",user_71,asset_587,48.1470144,-103.6180489
4/18/2019,Separator,Temp Control System,Pilot,,,,"High Unit Temp on line heater, pilot was jacked up on pressure and heating up bath with just pilot. ",user_2,asset_1780,46.2356189,-100.6010498
1/29/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,replaced block and bleed relay on fischer controller cycles resumed,user_11,asset_30,48.1470144,-103.6180489
2/18/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Noticed bath B was 60 degrees. Went to turn up t-12 but fuel gas was froze. Thawed on line and got main burner working ,user_172,asset_337,,
3/27/2018,Compressor - Gas Lift,Compressor,Valves,Ariel,,Electrical Short,"Found pad down on false high tank. water tanks at 2.4 Had to bypass pad to be able to jump pack on Air compressor was on and had 125psi on it After getting pad jumped on. I restarted the compressor. Compressor said it was down on low suction, due to ESD's closing RTP'd well ",user_53,asset_1112,40.7126799,-114.1193569
2/21/2018,Separator,Temp Control System,Thermostat,,,,Lit burner and tested T-12. T-12 on vessel would not shut off due to liquids in the fuel gas supply system. Pulled apart T-12 and blew out all liquids. Tested T-12 and set vessel temp to 70 degrees F.,user_62,asset_1220,40.5481548,-114.0112915
8/27/2017,Compressor,Compressor (Recip),Valves,,,,Flagged high temp #4 cyclinder ,user_156,asset_1087,48.21056995,-103.6392192
9/21/2019,Separator,Fuel Supply System,Regulator,,,wear,"Location went down on low fuel gas pressure , the 100 well has the downstream valve on it and holds up all the fuel gas for the whole pad and is very loaded and did not have the tubing pressure to keep the pad up. Vented the well multiple times to get pressure better so the well will hold up the pad . Pressured up pad and rtp'd wells",user_10,asset_515,40.5262342,-113.8824849
3/5/2018,Gas Scrubber Separator,Dump Line,,,,Erosion,Mon 11-150 checked equipment and drained scrubbers.,user_71,asset_2046,40.5960545,-113.9323891
4/2/2019,Surface Location,Well Pad,,,,Weather,Ground is soft due to melting snow and still some snow on location.,user_55,asset_1370,,
3/7/2017,SWD System,SWD Pump,Other,Other,Other,Other,,user_117,asset_1489,36.2541889,-91.2478009
10/18/2019,Compressor - Gas Lift,Compressor,Suction Controller,Ariel,,Freezing,"Found compressor down on high discharge, broke freeze in the discharge line and rtp'd compressor set rpm at 1400 manual.",user_10,asset_1493,40.5262342,-113.8824849
11/11/2017,Compressor,Compressor (Intergral),Process Gas Supply,,,,comp down on high discharge RTP,user_71,asset_1812,48.1470144,-103.6180489
2/27/2017,Automation,Other,,Other,Other,Other,no damages,user_92,asset_616,48.224585,-103.8291059
11/5/2018,Compressor,Engine (Gas),,,,,There was a leak on the oil circulation system. Arch rock was called out to troubleshoot and RTP.,user_54,asset_701,48.1470144,-103.6180489
4/8/2018,Wellhead,Tubing,,,,,Loaded,user_86,asset_589,,
12/31/2017,Fuel Gas/Start Gas,Coalescer/Filter,Mist Pad,,,,Drained desi and scrubbers.,user_48,asset_1280,48.34565233,-103.7107339
2/17/2018,Tanks/Pits,Flare/Combuster,,,,,Flare blew out from wind. Relit flare. Blew out before I walked back to my truck. Every time you relit wind blows pilot ,user_172,asset_2069,,
8/10/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Arrived on site and checked all scrubbers for fluids, they were dry, ",user_15,asset_1383,49.5499678,-102.9290839
6/6/2017,Dehy,WFS Issue,,,,,"Williams tech indicated that the solar panel went bad, and he will replace it as soon as possible. ",user_130,asset_968,48.1470144,-103.6180489
10/28/2018,Separator,Fuel Supply System,Regulator,,,overpressure,"80 psi going to 60 psi gauge, damaged gauge and pump, replaced gauge and lowered regulator",user_31,asset_1059,43.252261,-115.0567324
4/19/2018,Wellhead,Tubing,,,,,Suspect residual kill fluid after well work last year preventing well from flowing,user_35,asset_1964,48.18313464,-103.504838
9/10/2019,Separator,ESD Valve,Gate/Seat,,,Corrosion,"needs hi/lo replaced and water dump trim and seat replaced. Locked out unit, got hi/lo and water dump packing changed, fixed nice, pressured unit nicely, everything holding and working correctly. So continued to sell, and do a long term RTP high pressure sell off. Then turn optimizer to put cycles into it. ",user_2,asset_1477,46.2356189,-100.6010498
3/4/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Well lost plunger arrivals. Kelvin continued to add off time and never added additional flow time to try and get plunger up. Opened the well to flow, and paused open. Plunger still wouldn't arrive. Opened to AGT for 20 mins and got a plunger arrivals.",user_53,asset_1056,48.2639983,-102.8811755
3/25/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Found well equalized and SI Opened flow line to AGT, Had to leave location so I Shut BD valve. Came back and popped open. Had good pressure, Opened ESD and started cycle RTP'd well ",user_53,asset_1353,40.7126799,-114.1193569
4/19/2017,Compressor,Engine,Other,Other,Other,Other,,user_35,asset_694,48.334012,-103.5944308
12/12/2017,Automation,Radio,Wiring,Cal Amp,,Improper Install,Cyclonic control valve won't open ,user_111,asset_587,48.04197367,-103.3530272
12/8/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_101,,
2/28/2017,Instrumentation,Transmitter,3n1 MVT,Other,Other,Other,None,user_166,asset_1834,47.93458037,-103.6410893
4/11/2019,Pipeline/Piping,Valves,,,,Corrosion (Internal),The Vent Valve (cyclonic) Leaks by just a little when it had 1600 pounds on it. With lower pressure no leak. ,user_2,asset_2002,46.2356189,-100.6010498
2/27/2019,Separator,Dump Line,,,,Freezing,"Dispatched to pad, I knew that this pad was down and has been down for a few weeks. Pulled into location and saw JW onsite working on the compressor. Spoke with the tech and found out that the batteries were dead. I contacted leadership to have them run me down 2 boostpro's Onsite i found that the line heater was up and warmed up, found only one solar glycol pump working. Notified Travis 90 well, I found that burner was off, unit had pressure in it so i started burner and got bath warming up. After getting burner lit i checked both dumps and found that the condo dump was clear to the tank and that the water was froze. Started to thaw on the water dump line as well as the unit blow down. After thawing for 2.5 hours i got the water line cleared to the tanks. Proceeded to troubleshoot well and found that TBG had 130 and CSG had 800. Decided to vent well, got it cleaned up and put well back on cycles. RTP'd 90 well 85 well, found this unit completely down, TBG has 1244 and CSG has 844. Decided to jump this unit from another unit to eliminate having the TBG opened to the unit. After jumping it i was able to get the burner stared and then i checked the dumps, both dump displacers were froze in the unit. Started thawing on the shell of the vessel. First i did get the water displacer free. 165 well, found this well online with the unit warm but it is loaded and is waiting for the compressor to be stared. Compressor is down on low engine jacketwater level and possibly the batteries but i am charging them right now. This well will be RTP'd once i can get the compressor running. I need to come back to location tomorrow to get gas lift running and get it all back on. ",user_56,asset_546,48.224585,-103.8291059
7/20/2017,Flare System,Flare Header,Regulator,,,,"Relit ""C"" SCC. Pilot was extinguished after evening rain storm. ",user_41,asset_1761,48.20207628,-103.5975102
5/24/2017,Sales Valve (PV),Elec.System,,,,,"Fisher 6200f DVC failed because water got into communication terminals. This app is still missing the correct equipment for Wamsutter, and without that or an ""Other"" option it is impossible to put in an accurate surface failure, so what is the point here?",user_134,asset_1040,48.1470144,-103.6180489
5/31/2019,Automation,RTU,CPU,Schneider/Scadapack,Scadapack P4A,Wear,"NOT SCADAPACK!! PLEASE FIX DROPDOWNS. Yokogawa FCN PLC needed to be rebooted. Also, root cause is nonsense. Most likely cause of failure is Kelvin comms hogging bandwidth.",user_12,asset_1994,40.5262342,-113.8824849
4/4/2019,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,kimray fuel pot full of liquids ,user_56,asset_1713,48.1470144,-103.6180489
9/11/2019,Automation,RTU,Onboard Battery,Kimray,GFC,Wear,"cycled choke , dvc had it hung up. got it loose and. called optimizer, helped me out , surfaced plunger on its own, inspected and redrop, rtp well, optimizer watching",user_77,asset_1993,40.5262342,-113.8824849
5/6/2018,Compressor - Gas Lift,Compressor,Lubricator,Ariel,,Trash,"GL was down on compressor oil low level Day tank in compressor building was out and not feeding compressor. Day tank will need to be filled. Compressor will also need a PM, i will submit a TR to TL to get it scheduled with Fox services I was able to get low ash oil from WDW #1, got compressor filled with 5 gallons. RTP'd compressor",user_53,asset_1272,48.2669898,-102.8787701
8/21/2019,Site Power,Control Cabinet (MCC/PCC),,,,,Arrived To Location. Walked Down Pad And Noticed ESDs Were Closed. Contacted Optimizer. Optimizer Could Not Reset ESDs. Sending In WM To Automation To Look Further breaker was tripped,user_16,asset_1559,,
2/22/2017,Gas Scrubber,Other,Other,Other,Other,Other,Well hydrated off in choke causing unit to lose fuel gas burners eventually went out hi low shut. Broke freeze in choke. Opened by pass let pressure into unit until high low opened. Scrubber ball lodged up in pot. Bled pressure off of big joe. Snakes pot.,user_172,asset_42,48.20088601,-103.5384668
1/10/2019,Pipeline/Piping,Valves,,,,Corrosion (Internal),Hi-lo valve would not hold and failed. Well is shut in and tagged out. Work management in to have replaced. Informed Dean Kinsey. ,user_44,asset_1345,,
2/17/2019,Automation,Antenna,,Bluewave,,Loose Connection,"Bad temp sensor on bath, well is shut in and called out on high bath temp",user_77,asset_1747,48.10858943,-103.4912044
3/1/2018,Gas Scrubber Separator,PSV,Body,,,Weather,came on location and saw that the choke/ hi-low was frozen trap pressure caused it to burst ,user_110,asset_1321,36.2541889,-91.2478009
12/15/2018,Instrumentation,Lighting Arrestor,,,,,igniter was not sparkling. It was replaced.,user_83,asset_1302,48.1470144,-103.6180489
1/20/2019,Plunger System,Plunger,Plunger,PCS,,No Liquid,"Priority duel pad failed, spring tension on pads aren't great and don't hold a good seal compared to our older model duel pad plungers",user_25,asset_471,,
3/25/2018,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,"Knock out pots, to flare, fuel gas to flare, line heater, and line heater scrubber had liquids. Wells flowing over 110deg carries liquids through the gas stream which drop out in these pots and scrubbers.",user_58,asset_1823,48.41593731,-103.5769464
3/1/2019,Heater Treater,Vessel,Fuel Gas Scrubber,,,Weather,"regulators for line heater are out in the elements causing freezing, wo in to insulate",user_64,asset_1257,39.2506642,-92.4357879
5/16/2019,Tanks/Pits,Tank,Load Line,,,Empty,"when replacing leaking valves, we found all nipples into tank were corroded, very badly. we replaced all nipples on this water tank except the 4"" load line,nipples, will talk to team leader, we might want another W/M to replace the 4"" valves and nipples, i hAD TO MANY WORK ORDERS OPEN, FROM NEEDING FITTINGS, wanted to get it closed, ",user_77,asset_2268,40.5262342,-113.8824849
7/15/2018,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,Issue: well called out shut in alarm Root Cause: (INT) low unit pressure. found well was down on non arrivals. Fix: turned well back on paused open and got a good arrival then restarted the plunger cycles ,user_170,asset_557,48.2594901,-102.9011771
5/14/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,well was missing plunger arrivals,user_179,asset_778,48.1470144,-103.6180489
12/15/2017,Heat Medium,Furnace,Flow Controller,,,,"call out bath alarm-found t-12 turned down to low bouncing on 49 degrees-adjusted and stayed until temp was reached, also found 70 well down on low psi, RTP , done walk through ",user_131,asset_532,40.7126799,-114.1193569
2/1/2017,Wellhead,Cyclonic Valve,Actuator,Other,Other,Other,,user_134,asset_1664,48.1585692,-103.6168969
12/12/2017,Fuel Gas/Start Gas,Regulator,,,,,"Seperator A fuel gas pressure regulator and motor control valve that operate the vessel burner gas supply have failed, over pressuring the supply gas to the burner causing it to over pressure and ""woof"" the burner blowing out the pilot and making the burner unsafe to operate. Fuel gas has been identified and tagged out in the closed position. Parts have been ordered through a work request assigned to B. Grasse to complete maintenance once parts are available.",user_6,asset_1600,36.2541889,-91.2478009
2/10/2019,Dehy,Meter (BP Check),,,,,"sales meter was frozen and showing false flow, thawed meter and bleed off, not much liquid",user_31,asset_2120,43.56424,-91.351691
5/30/2018,Tanks/Pits,Tank Level,Probe,,,Calibration Issue,"Issue: well called out shut in alarm (INT) condo tank 2 Root Cause: looks like another tank switch is failing. This is the second tank on this location that is in an OOS state Fix: verified it was a false hi tank alarm, then i took the switch and level transmitter OOS force cleared the alarm. Then tagged out the tank and reported it to my superior and then turned the well back on",user_136,asset_1915,48.264955,-102.9008516
1/8/2018,Compressor,Compressor,Suction Controller,Ariel,,Liquid Carryover,,user_48,asset_2108,48.36316045,-103.789745
11/20/2017,Separator,Choke Valve/Loop,,,,Trash,"Issue: found the fed wells were down. this is a FED and FEE location and the FED side only has 3wells running in a 4pac Root Cause: the cycles keep shutting off at the same time and the unit runs out of pressure and shuts in. there is 2 glycol pumps, burner, methanol pumps, SCC's all running off the fuel gas so when all the wells go into off cycles at the same time there is only minutes before it shuts in. Fix: left one well running to keep pressured up. long term fix is a buy back meter",user_136,asset_854,48.2594173,-102.9010927
10/18/2017,Automation,RTU,Fuse,Kimray,Bristol 3310,Corrosion,cyclonic is bad will not turn ,user_110,asset_1822,36.2541889,-91.2478009
4/27/2019,Site Power,External Supply,,,,,"Location had a power bump. Had to restart PLC, and was able to RTP pump.",user_55,asset_2112,,
12/14/2016,Automation,Antenna,,,,,Water tank showing false high tank well is still flowing task request in,user_148,asset_1103,48.3357699,-103.5982326
8/3/2019,SWD System,Particle Filter,Element,,,,"Walk through, took readings, change filters due to high filter differential pressure. Greased motors and valves that I could. ",user_55,asset_2112,,
2/7/2019,Compressor - Gas Lift,Compressor,Cylinder,Frick,,Liquid Carryover,Compressor down on high temp,user_94,asset_910,40.5262342,-113.8824849
2/14/2017,Gas Scrubber,Other,Other,Other,Other,Other,Relit scc,user_100,asset_1929,48.11478852,-103.5977526
8/17/2019,Tanks/Pits,Flare Header,Regulator,,,,Location was shut in for high tank. Tank has been hauled. Rtp well on plunger cycles. Lifted plunger made its first arrival. Well rtp,user_120,asset_2034,,
3/29/2018,Dehy,Surge Tank,Regulator,,,,Doing my daily site visit checked dehy tub. One tub is around half full and the other is 75%-80% full. Turned in to fluid management to get hauled ,user_172,asset_2046,,
4/4/2018,Tanks/Pits,Valving/Swedges,Body,,,Corrosion,Opened all condo tanks to operate battery as facility to maximize condo capacity onsite and align with predictive dispatch tools. ,user_62,asset_873,48.1470144,-103.6180489
1/2/2017,Compressor,Compressor,Lubricator,,,Liquid Carryover,Compressor down on low oil psi. Wells 140&60 froze on discharge line rtp'd ,user_58,asset_910,47.99306933,-103.4221292
9/26/2017,Instrumentation,Controller,,,,,This is for the Asco solenoid valve controlling the pilot gas to the glycol bath heater burner. It was clogged and not allowing fuel gas to flow to the pilot.,user_134,asset_495,48.3619066,-103.2129855
7/12/2018,Separator,ESD Valve,Gas Supply Line,,,Calibration,well had lost unit pressure due to fisher controller have insufficient fuel gas psi. adjusted regulator test high low. rtp well,user_120,asset_278,43.252261,-115.0567324
9/12/2019,Pumping Unit,Engine,Water Pump,Waukesha,,Vibration,Water pump worn out from fan pulley vibration.,user_42,asset_588,48.1470144,-103.6180489
4/18/2017,Wellhead,Cyclonic Valve,Gate/Seat,Other,Other,Other,unknown,user_154,asset_1568,48.224585,-103.8291059
2/4/2018,SWD System,Particle Filter,Element,,,,Replaced filters because pump is down due to high filter differential pressure and restart pump,user_141,asset_2012,48.1470144,-103.6180489
12/4/2017,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Every end device and fuel gas regulators need drained constantly ,user_58,asset_1823,48.36654271,-103.5605372
12/23/2017,Gas Scrubber Separator,ESD,,,,,3 mile 15-pad down on low unit and valve fault. Installed jumper and RTP pad started cycles,user_71,asset_2224,48.1470144,-103.6180489
6/24/2018,Plunger System,Plunger,Plunger,Well Master,,No Liquid,I went to location surfaced plunger and put back on plunger cycles.,user_51,asset_1839,,
2/17/2019,Tanks/Pits,Flare/Combuster,,,,,"3 scc's out, didn't see any issues relit, probably due to high winds",user_31,asset_1406,46.2356189,-100.6010498
1/25/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Kelvin lost plunger arrivals, and loaded well by continuing adding off time and failing to surface plunger. vented well and put back on cycles ",user_53,asset_1056,40.7126799,-114.1193569
3/5/2019,Separator,Liquid Dumps,Controller,Norriseal,,Freezing,"arrived on location with steamer crew. found both HP vessels froze solid.was unable to move dis placers in vessels. attempted to get pressure in HP separators. coudnt get pressure into either vessels do to freeze in flowline. was unable to shut chokes on both line heaters do to freezes in choke/coils. attempted to thaw out fuel gas to fuel gas separator so we could at least get glycol pumps circulating heat. line is frozen solid. contacted team lead, and asked to get two heaters onsite and for them t be placed on each HP&LP. will return tomorrow with steamer crew. ",user_120,asset_580,39.2506642,-92.4357879
4/4/2018,Gas Scrubber Separator,ESD,,,,,Luman 10-45 Orin called and said he had fixed the allocation meter transmitter on B unit and it was ready to RTP. Went to location pressured up unit and reset interlocks and RTP. Ran all night everything looks OK.,user_71,asset_1323,48.1470144,-103.6180489
8/21/2017,Compressor,Compressor (Intergral),Process Gas Supply,,,,,user_71,asset_2262,48.3619066,-103.2129855
7/11/2018,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,"Divide 21-130 called out on high tank, #761364W at 17-1x16-4 shut in wellheads and seperators. Called IBEX.",user_37,asset_234,43.252261,-115.0567324
4/11/2018,Automation,Plunger Arrival Switch,,EDI,,,Found cyclops mso board detached from housing. Replaced with new cyclops,user_30,asset_458,47.89380937,-103.4995304
3/7/2018,Instrumentation,Transmitter,Tubing Pressure,Rosemount,1151,Temperature,"Tubing pressure transmitter was frozen, applied heat with thaw tube from truck, thaw and clear lines of liquids. No heat trace and insulation on this transmitter ",user_109,asset_725,48.141369,-103.4136746
10/30/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Dispatched to well, I had left well SIPB yesterday evening Got to location and found TBG with 512PSI and CSG with 793PSI with a load factor .35 Still decided to vent well, after an hour I got plunger to surface, shut TBG master and caught plunger Filled out SBA and sent it in for approval, once approved I inspected plunger Measurements are as followed Top 1.893 Middle 1.892 Bottom 1.894 Plunger is within reason to drop Installed plunger sign on lubricator cab Dropped plunger and coded to OPT to watch cycles and evaluate criteria RTP'd ",user_56,asset_76,48.2600967,-102.8982218
2/6/2017,Gas Scrubber,Shell,Body,Other,Other,Other,Relit both scc,user_100,asset_1646,48.11458258,-103.5980344
4/19/2019,Separator,Choke Valve/Loop,,,,Corrosion,Cleaned fire eye lens on scc B reset and verified eye was sensing flame,user_18,asset_89,,
2/7/2019,Separator Inlet Valve (XV),Pneumatic Control System,Hi/Lo Pressure Controller,,,,ESD won't stay open,user_94,asset_910,40.5262342,-113.8824849
11/14/2017,Instrumentation,Controller,,,,,I2P and realy in Fisher DVC 6000 plugged with condensate. The pad has the fuel gas reconfiguration. I don't know what condition the I2P and relay were in when the reconfiguration was done.,user_134,asset_1612,48.1602906,-103.6173979
11/28/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ajax,,Trash,There isn’t enough gas to keep compressor running and injecting need to either get buy back line or something needs fixed restarting 2 time a day,user_63,asset_757,48.30728987,-103.6409279
6/29/2018,Fuel Gas/Start Gas,Regulator,,,,,"big joe failure, very old, try to rebuild, may need replaced, will have parts in the morning to fix",user_88,asset_688,48.262822,-102.8996528
3/28/2018,Separator,Choke Valve/Loop,,,,Corrosion,choke seat was worn out causing choke to leak during off cycle. replace choke and seat submitted fieldbit ticket to automation to calibrate but he is currently busy but informed that he would swing by later to calibrate,user_11,asset_1249,40.7126799,-114.1193569
3/5/2018,Fuel Gas/Start Gas,Regulator,,,,,"burner blown out, bath 39 degrees, no issues found other than maybe high winds, burner sits in wind path..relit, brought bath up too temp",user_88,asset_536,48.2595038,-102.901041
11/22/2017,Separator,Choke Valve/Loop,,,,Freezing,Hi lo stuck,user_111,asset_1562,48.06791482,-103.3830955
8/10/2018,Separator,Choke Valve/Loop,,,,Trash,"ARROW PLUS 4PAK SEPARATOR DOWN #65 WELL SHUT IN FOR RIG WORK #40 DVC WAS STICKING IN THE CLOSED POSITION AND THE OTHER TWO WELLS COULD NOT SUSTAIN UNIT PRESSURE DURING OFF TIME DVC IS NOW WORKING, ALL WELLS RTP'D",user_34,asset_31,48.1470144,-103.6180489
3/13/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Had to RTP unit after flow line freeze broke,user_46,asset_292,48.0614644,-104.8417043
4/25/2019,Separator,Choke Valve/Loop,,,,Trash,"Tried to rtp well and found that the yoko choke on this unit was in IMAN and would not open / power cycled DVC and contacted Mike Edwards to try and reset the choke, he could not reset DVC and said that the DVC would need replaced before he could fix it . Automation my have to do more troubleshooting or replaced DVC",user_10,asset_739,40.5262342,-113.8824849
1/13/2019,Tanks/Pits,Flare/Combuster,,,,fuel gas freeze,"3 scc's out, 2 with frozen regulators",user_31,asset_1280,43.56424,-91.351691
2/15/2018,Chemical System,Pump,Diaphragm Gears,Texsteam,HBT2,Weather,"Gas lift compressor still running. Found methanol not pumping. Once I got it to pump 3 times the fuel supply pressure dropped down to 10#. Opened the main fuel supply line for methanol pumps, that line barely have any pressure. Tried another spot upstream from that and found the same thing. Poured 1 quart of methanol down the fuel supply line and let it sit for 15 mins. When I re-pressurized line the freeze broke. Went into the air compressor room, found the drying tower in a failure. Reset drying tower Got methanol pump again on all wells Tried breaking the freeze on the injection line on 120 well twice, not successful will leave methanol pump overnight ",user_53,asset_1945,48.2573957,-102.911502
1/17/2017,Instrumentation,Transmitter,3n1 MVT,,,,Williams meter lost power. Wasn't working. They corrected the problem. Should have data now,user_166,asset_1863,48.16032359,-103.6192751
4/14/2018,Gas Scrubber Separator,Dump Line,,,,Erosion,Luman 8-115 checked location drained scrubbers everything looked OK. Dropped flare pilot boom and relit pilot. ,user_71,asset_1317,48.1470144,-103.6180489
3/12/2017,Compressor,Engine,Other,Other,Other,Liquid,Low water jacket level. Was to low to start compressor. Archrock has filled reservoirs and RTP'd,user_141,asset_551,48.224585,-103.8291059
12/12/2017,Compressor,Motor,Windings,,,,"Motor removed and sent in for new windings,",user_84,asset_1466,48.0817546,-103.5597106
2/7/2019,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_101,,
8/8/2018,Amine,Reflux Accumulator,Mist Pad,,,,IGNORE. Start up of lateral compressor.,user_137,asset_1154,36.2527392,-91.2689312
12/11/2016,Gas Scrubber,,,,,,Supply gas to esd was frozen thawed and rtp well,user_100,asset_1746,48.13893557,-103.656688
11/16/2017,Separator,Liquid Level Control,,,,,"Unit was down, high tank alarm. ",user_48,asset_1998,,
1/29/2018,Compressor - Gas Lift,Engine,Bearing,Caterpillar,,Vibration,Installed rebuilt motor and hooked up to gas lift compressor ,user_161,asset_606,48.1587643,-103.6194633
4/3/2017,Wellhead,Other,,Other,Other,Other,Lost production and man hours,user_84,asset_2070,48.04257964,-103.5353847
5/1/2017,Gas Scrubber,Other,Other,Other,Other,Other,,user_88,asset_158,48.08486827,-103.6172187
12/5/2016,Compressor,Compressor,Scrubber Level,Other,,Freezing,Freeze in compressor dump line causing unit to go down on scrubber level,user_179,asset_1048,47.97172947,-103.5641525
4/1/2018,Instrumentation,End Device,Spa2,,,Wiring,Loose connection caused no power to SPA. No equipment issue. Works okay after wiring issue corrected.,user_134,asset_56,48.1470144,-103.6180489
1/24/2019,Separator,Fuel Supply System,Regulator,,,freeze,supply to chokes is outside cabinet and freezing. ,user_64,asset_1100,40.5262342,-113.8824849
12/8/2016,Heater Treater,Back Pressure Valve,Body,Other,,,"T12 on line heater froze, and motor valve froze . Due to liquid drop out in fuel gas with cold fuel lines, got line heater running but heater needs heat trace , insulation , an a building to keep wind off it ",user_122,asset_676,48.35936965,-103.7770899
10/28/2019,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,"Checked location, drained scrubbers and re-lit SCC's",user_63,asset_247,,
7/8/2019,Tanks/Pits,Liquid Level Control,,,,,Gasket on filter pot was is bad and needs to be replaced on the blue filter pot ,user_159,asset_101,43.56424,-91.351691
12/6/2017,Chemical System,Pump,Check Valve,Texam,HBC1,Air Locked,Sandpiper pump not moving glycol,user_50,asset_1406,48.33577187,-103.5982645
11/7/2017,Separator,ESD Valve,Actuator,,,Fouling,High tank shut in never reset. ,user_35,asset_377,48.18028744,-103.5361564
8/14/2019,SWD System,Tank,Shell,,,Weather,"Changed west filter, location checked, replaced 2"" gasket on leaking valve on 5K tank",user_31,asset_308,48.1470144,-103.6180489
3/17/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,Well is loaded couldn't get plunger to come in shut in for pressure build ,user_46,asset_535,48.0614644,-104.8417043
3/22/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Well had consecutive non arrivals I went to location and vented plunger to surface.,user_51,asset_1048,48.0614644,-104.8417043
4/28/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Drained all scrubbers while on location, no fluids present.",user_62,asset_293,48.1470144,-103.6180489
1/18/2019,Separator,Temp Control System,Heater/Burner,,,,"Snow drift had formed on flame arrestor starving the burner of oxygen and it went out. Shoveled out snow drift, cleaned flame arrestor and lit burner. ",user_15,asset_676,43.56424,-91.351691
3/31/2018,Separator,Dump Line,,,,Corrosion,While doing site vist noticed oil leakin at sep. the dump controller was leaking out of packing. Got permission to shut in well. Isolated well bled down unit. Changed out dump controller with a new one . Pressured up and tested my work with 100psi rtp well,user_172,asset_1760,,
5/20/2018,Compressor - Gas Lift,Compressor,Valves,Ariel,,Trash,"Injection line was froze, broke freeze and RTP'd",user_53,asset_910,40.7126799,-114.1193569
10/6/2017,Heater Treater,Vessel,Fuel Gas Scrubber,,,Weather,Fuel gas in heater treater has a lot of fluid in it. Drained scrubber ,user_172,asset_876,,
7/1/2018,Tanks/Pits,Flare/Combuster,,,,,SCC “B” pilot was extinguished after yesterday’s rain fall. ,user_41,asset_1363,48.02367627,-103.3638049
12/5/2018,Compressor - Gas Lift,Compressor,Scrubber Level,Ariel,,Freezing,could use a heater ,user_121,asset_296,48.3580576,-83.27272
8/1/2019,Chemical System,Piping,Supply Line,,,Connections,Maintenance crew went to location and the methanol line was already hooked up to the tank. Somebody performed the work and apparently forgot to close the WM in the system.,user_68,asset_602,48.1470144,-103.6180489
8/4/2019,Flare System,Flare/Combuster,,,,,"found pilot on scc north of location was plugged ,cleaned pilot and relit scc",user_144,asset_2001,46.2356189,-100.6010498
3/8/2018,Separator,Choke Valve/Loop,,,,Freezing,"hi/low was frozen when i pulled up on location, made sure i could shut the choke and thaw on the hi low safely. well is back up to temp and rtp ",user_110,asset_2171,,
8/1/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,well was losing arrivals due to worn plunger,user_179,asset_1801,40.5960545,-113.9323891
5/22/2019,Separator,rupture disk,,,,premature rupture,Ops site inspection found the wrong pressure rating on the separator. Rupture disk replaced with the right pressure rating.,user_21,asset_805,46.2356189,-100.6010498
3/19/2018,Wellhead,Cyclonic Valve,Gate/Seat,,,Corrosion,"Replaced 2"" 10k cyclonic blow down valve, re-insulated, and notified operator to RTP. ",user_161,asset_834,47.9545153,-103.3913019
7/31/2019,Chemical System,Containment,,,,Vandalism,The methanol tank secondary containment was missing the bird netting. Crew installed it over the tub.,user_68,asset_1127,48.1470144,-103.6180489
3/30/2018,Tanks/Pits,Liquid Level Control,,,,,False high tank 13'8 highest tank level and had already been switched,user_163,asset_63,48.1470144,-103.6180489
3/9/2019,Separator,Liquid Dumps,Controller,Nalco,,Freezing,surface piping freeze issues due to cold weather,user_17,asset_1428,,
3/15/2019,Separator,Dump Line,,,,Freezing, +WATER DUMP LINE FROZEN- NOW SHUT IN AT SEPARATOR RCFA FREEZING? LOOK TO THE PUMPS,user_34,asset_1206,43.56424,-91.351691
9/14/2019,Flare System,Flare Header,Regulator,,,,Well load and needs a vent also replaced two fuel gas regulators on the fuel gas system and re lit 3 scc's,user_10,asset_477,40.5262342,-113.8824849
12/19/2016,Wellhead,,,,Other,Other,Unable to proceed with wellhead reconfiguration. ,user_161,asset_2029,48.26485258,-102.9262409
5/22/2019,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Plunger wouldn't surface.,user_94,asset_1270,48.1475232,-103.6191904
1/13/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_2012,48.1470144,-103.6180489
11/15/2017,Compressor,Intrumentation,,,,,"Issue: found the compressor was down on the HMI Root Cause: when I got there it was down on ECIS. Restarted but went back down again on D-EGF fuel pressure, restarted again and went down on another alarm. The compressor would only run at 300RPM and then went back down. Fix: notified Archrock to come look at it",user_136,asset_695,48.1470144,-103.6180489
3/22/2018,Compressor - Gas Lift,Compressor,Valves,Ajax,,Freezing,"valve outside cabinet freezing, we have talked about removing trims in these valves before but never got ok to do it",user_87,asset_271,40.7126799,-114.1193569
9/15/2019,Gas Scrubber Separator,Dump Line,,,,Trash,"Drained all scrubbers, fuel pots, dezi, and regulators. All had fluid and paraffin. Choke is operating properly. RTP'd well",user_55,asset_1075,,
2/8/2017,Gas Scrubber,Other,Other,Other,Other,Other,Relit scc pilot,user_100,asset_356,48.12562829,-103.6165974
3/20/2018,Wellhead,Wellhead Piping,,,,hydrate,well was in int didnt give a reason. looked over t-pack kicked well on achieved plunger arrival. cycles resumed,user_11,asset_2155,40.7126799,-114.1193569
3/18/2019,Surface Location,Lease Road,,,,Weather,Location drifted shut. 3-18-19 Plowed location access road & turnaround. ,user_42,asset_1937,46.2356189,-100.6010498
12/9/2017,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,"Issue: found whole pad was down Root Cause: all the well going into off cycles at the same time and then the 2 burners, 4 glycol pumps, 4 SCC's use up all the unit pressure and then the pad shuts in Fix: turned pad back on and left one well flowing to keep the pad up while all the other wells go into there off cycles. Long term fix: is to adjust the cycles so there not all shutting in at the same time or putting the buy back meter into service. ",user_136,asset_967,48.2591046,-102.9021856
10/15/2019,Fuel Gas/Start Gas,Regulator,,,,,"automation working on tank switches, shut pad in and knocked compressor down, had to wait for them to finish job to bring back on line. Flowed well out and brought compressor back on, not flowing, seems to be a freeze, injecting but not building any tubing pressure, needs to be blown to tank, but automation is working on top of the tanks and I cannot blow down now. Will need to re visit tomorrow",user_106,asset_1359,48.1470144,-103.6180489
11/6/2019,Chemical System,Pump,Valves,Texam,HBC1,Set Screw,found meth pump unable to control discharge due to removal of downstream thumb valve. added correct valve and rtp pump to service. ,user_17,asset_714,,
4/9/2018,Tanks/Pits,Flare/Combuster,,,,,Found SCC main and pilot out. Checked pilot pressure against new gauge and found it to be within specc. Checked fuel gas for pilot for fluids and supply is dry. Tested regulator functionality against closed valve and PSI does not creep. Tip of pilot is not deformed or plugged. After re-lighting pilot the tip turned red and should create a hot enough surface for auto ignition should the pilot go out due to wind. Possible RCFA is precipitation overnight fell onto pilot tip and knocked out the flame and cooled off the tip to where auto-ignition was not possible. Possible re-design by engineering needed to alleviate this issue.,user_6,asset_793,48.0831088,-104.8694982
9/22/2019,Chemical System,Pump,PSV,Goulds,HBC1,Wear,"Methanol pump had a rupture disc that was blown, replaced with a psv and working good now.",user_22,asset_1109,46.2356189,-100.6010498
3/13/2018,Compressor,Engine (Gas),,,,,"Compressor was shut of for production test, Engineering team requested that the compressor be re-started. Arrived on location and found compressor off, inlet shut and tagged and batteries shut off. walked through all piping and made sure all valves were in proper order to start and run compressor. Started and warmed compressor, loaded compressor and am watching wells to see if any need unloaded to tanks.",user_62,asset_857,48.1470144,-103.6180489
11/5/2017,Tanks/Pits,Flare/Combuster,,,,,Pilot lines filled with fluid regulator on scc B leaking out of weep hole. Took line apart and replaced regulator. Couldn’t get scc A to lit. Selnoid needs to be replaced ,user_172,asset_1276,,
11/3/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Relit flare keeps blowing out with pilot running. Relit dvc. Drained scrubbers. Opened choke 1/64,user_172,asset_2069,,
1/15/2018,Compressor,Compressor (Recip),Lubricator,,,,"Compressor went down on low compressor oil pressure, everything looked good restarted compressor let it run and it ran good. RTP'd well ",user_53,asset_600,48.1602349,-103.6171353
9/26/2019,Fuel Gas/Start Gas,Regulator,,,,,Needs new Dixon regulator.,user_98,asset_1850,48.1603503,-103.6188405
9/26/2019,Tanks/Pits,Berm,Gravel,,,Erosion,"After dump line repaired, crew raked around tanks",user_21,asset_450,46.2356189,-100.6010498
3/24/2018,Chemical System,Piping,Discharge Line,,,Debris,"Removed thumb valve on pump exhaust, cleaned and reinstalled. Pump is working",user_141,asset_817,48.1470144,-103.6180489
3/28/2017,Tanks,Other,Other,Other,Other,Other,Burner out,user_138,asset_1237,48.17281702,-103.4318953
1/17/2018,Gas Scrubber Separator,Dump Line,,,,Freezing,Drained desi dryer while on location working on well 90.,user_62,asset_776,48.1470144,-103.6180489
3/9/2017,Wellhead,Primary Choke,Other,Other,Other,Other,,user_134,asset_1938,48.224585,-103.8291059
1/5/2018,Wellhead,Tubing,,,,,"Inlet froze, brake it and send it to the tank",user_116,asset_2261,47.941946,-103.6974949
12/13/2017,Gas Scrubber Separator,ESD,,,,,Lost fuel gas due to all wells in off cycle at the same time,user_126,asset_680,,
3/10/2018,Compressor,Compressor,Regulator,Ariel,,Vibration,Issue: called out compressor down alarm Root Cause: went down on hi discharge pressure. is acting like the hi pressure recycle valve isn't working Fix: restarted and returned to service. made sure was injecting into one well so wouldn't over pressure ,user_136,asset_1452,48.1470144,-103.6180489
11/10/2017,Separator,Temp Control System,Fuel Gas Supply,,,,"Find 4-PAC unit down on low unit. Zero vessel pressure. SCC's down as well. Jump gas to unit. Begin returning well to production after breaking freeze in fuel gas header. Could not break freeze with first well jumped. Had to move jumper to another well to break freeze. All wells were in an off cycle at same time with pumps, burners and SCC's running dropped pressure enough to trigger ESD's. Buy back schedule dated 10/6/2017 shows buy back meter installation scheduled for the week of 11/13/2017. Return well to operation. Continue with other wells on pad. Relight SCC's and bath. Drain desi of minimal fluid. Longer wrench time due to having to break fuel gas freeze. ",user_75,asset_1122,,
11/9/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_2012,,
3/3/2018,Tanks/Pits,Flare/Combuster,,,,,Liquid on regulator. Rtp scc,user_153,asset_1232,48.17178954,-103.5941483
2/8/2018,Sales Valve (PV),Sales Valve,Body,Valvcon,,End Of Useful Life,Salesline cyclonic valve leaking out the stem bleeding off unit pressure. Task request has been submitted to have it replaced. ,user_41,asset_714,48.20684273,-103.5352995
3/5/2018,Separator Inlet Valve (XV),Pneumatic Control System,Vent,,,,"Thawed DVC and checked operation of choke. Vented well due to being loaded. Plunger arrived, RTP'd well, started cycles, and return to optimizer.",user_141,asset_905,40.5960545,-113.9323891
11/17/2017,Compressor,Compressor,Suction Controller,Ariel,,Liquid Carryover,Compressor down on hi suction pressure. ,user_48,asset_1675,,
4/2/2017,Sand Separator,Other,,Other,Other,Other,no sales,user_39,asset_554,48.224585,-103.8291059
10/16/2019,Separator,Choke Valve/Loop,,,,Corrosion,The choke was leaking by loading up the well. All internal parts were replaced but the choke couldn't be calibrated due to the pad is down and no fuel gas to the choke controller.,user_68,asset_1337,36.247824,-91.2533664
12/5/2016,Wellhead,Primary Choke,,,,,"Found choke fuel supply was froze off, traces back fuel gas system found 1"" check valve installed backwards not allowing fuel gas to go to desi drier, which allowed fuel gas to carry over enough liquids over to freeze of fuel supply to choke, repaired/rtp",user_115,asset_1142,48.16024159,-103.6171467
7/29/2019,Pipeline/Piping,Valves,,,,Corrosion (Internal),Replaced Blow down valve,user_157,asset_1488,46.2356189,-100.6010498
7/11/2018,Plunger System,Plunger,Plunger,PCS,,Scale,RD 5-160 changed out venture plunger with a spiral bar. RTP Travis started cycles.,user_37,asset_1092,43.252261,-115.0567324
3/30/2019,Wellhead,Tubing,,,,,tubing master valves were not holding had crew grease both valves on tubing,user_28,asset_471,48.1511877,-103.6265331
2/2/2017,Heater Treater,Other,,Other,Other,Other,Relive scc's,user_156,asset_235,48.14022425,-103.6809545
3/25/2019,Flare System,Flare Header,Regulator,,,,"froze regulator on #1 scc, shut off supply psi to regulator and letting warmer weather thaw it out , due to no access by vehicle to scc's",user_144,asset_793,48.1470144,-103.6180489
1/8/2019,Separator,Temp Control System,Fuel Gas Supply,,,,"fuel gas is frozen and full of water, probably from vessel being full of ice",user_31,asset_1291,43.56424,-91.351691
3/16/2019,Separator,Temp Control System,Thermostat,,,,"After I got the bath heater lit, i checked to see what the set point of the T-12's were. Found the glycol bath to be set at 125 and the gas temp T-12 set at 85. Turned gas T-12 down to 70. The higher gas temp causes it to carry more liquids and then it drops out in the fuel gas line to the SCC's and line heater as it cools off. ",user_15,asset_1220,49.5499678,-102.9290839
1/27/2017,Gas Scrubber,Dump Line,Dump Line,Other,Other,Trash,No circulation ,user_138,asset_1476,48.18402736,-103.4263904
3/27/2017,Gas Scrubber,Back Pressure Valve,Seat/Ball/Piston,Other,Other,Other,Potential for fuel scrubber over pressure,user_60,asset_140,48.30946413,-103.6584993
1/24/2019,Separator,Liquid Dumps,Body,Nalco,,Freezing, +CONDENSATE AND WATER DUMPS FROZEN DUE TO NO HEAT TRACE- *HEAT TRACE NOW WORKING **SHUT IN LIQUID LINES AT VESSEL UNTIL THAWED ***SHUT IN SALES LINE TO PREVENT PRODUCING WELL UNTIL LIQUID DUMP LINES ARE THAWED. ******VERIFIED INLET VALVE IS HOLDING,user_34,asset_811,43.56424,-91.351691
9/25/2019,Plunger System,Plunger,Plunger,IPS,,Corrosion,"Was able to kick well on and bring in plunger without venting. Removed and inspected plunger, failed inspection. Worn divots down. Replaced with new 2 3/8 dual pad. ",user_55,asset_553,,
4/1/2018,Separator,Temp Control System,Pilot,,,,"SCC lost pressure due to frozen big joe at the separator. The big joe was frozen due to the bath heater and pilot blowing out, and multiple end devices pulling cold gas off of the separator through the big joe orifice with no bath heat froze off end device fuel gas. Separator burner pilot went out due to wind and improper oxygen mixture causing the main burner to woof when it came online. Checked and cleaned pilot orifice, re-lit and cycled main burner on and off 5 times after adjusting fuel/oxygen mixture and found it to be functional.",user_6,asset_1523,36.2541889,-91.2478009
2/3/2018,Separator,Temp Control System,Pilot,,,,Pilot was plugged ,user_48,asset_1029,48.35296935,-103.7748608
3/20/2017,Gas Scrubber,Pnumatic Dump Valve,Controller,Other,Other,Other,,user_87,asset_1736,47.9934026,-103.4437018
3/12/2018,Plunger System,Plunger,Plunger,Trip Mate,,Not Optimized,Well is very loaded because of higher line pressure on this pad will need multiple vents / Vented plunger to surface,user_100,asset_1766,48.1470144,-103.6180489
12/23/2017,Separator,ESD Valve,Gas Supply Line,,,Freezing,Esd on valve misalignment. Fuel gas to esd and kimray catch pot both froze. The reason this happens is because we work with wet fuel gas and it is 5degrees outside. Thawed out lines rtp well on plunger cycles ,user_172,asset_1875,,
2/3/2017,Chemical System,Piping,Discharge Line,Other,Other,Other,Fittings and tubing,user_156,asset_58,48.20190722,-103.7919816
12/4/2017,Heat Medium,Pump,Plunger,Texsteam,113,Air Locked,Pump for supply gas stalled,user_111,asset_708,48.03758076,-103.3453799
10/14/2018,Separator Inlet Valve (XV),Pneumatic Control System,Hi/Lo Pressure Controller,,,," Found fisher block and bleed to be mafunctioning due to lost of seal on plastic body, due to weathering/use/cracking. OPS replaced and verified functionality. ",user_54,asset_1969,36.2551968,-91.268112
8/4/2017,Instrumentation,Controller,,,,,This is for a failed Fisher I2P100. Cause of failure unknown,user_134,asset_2055,48.1584072,-103.6173515
1/26/2019,Instrumentation,Transmitter,Unit Pressure,Rosemount,1151,Weather,"unit transmitter was froze showing a false reading, thaw tubed transmitter and RTP unit",user_37,asset_1323,43.56424,-91.351691
10/11/2017,Compressor - Gas Lift,Compressor,Suction Controller,Ariel,,Vibration,"Jam nut on suction controller was not locked down. Vibration caused the suction controller to back itself off, compressor went down on low suction. Restarted compressor and set suction controller to 70 PSI, set jam nut.",user_62,asset_794,40.5262342,-113.8824849
2/17/2019,Heat Medium,Pump,Valves,Sunpumper,HBC1,Weather,"Bath temp was good, but pump wasn’t stroking, froze cyclonic valve, got pumps going and will warm up, not enough thaw tubes to reach, unit psi has come down,",user_77,asset_890,47.99184775,-103.5950995
2/21/2017,Wellhead,Cyclonic Valve,Gas Supply Line,Other,Other,Freezing,"Flow line partially froze, popped to tank and cleared freeze, rtp well",user_84,asset_592,48.15473353,-103.5405951
3/22/2018,Separator,Choke Valve/Loop,,,,Corrosion,Choke failed to open and close properly. Stem slightly bent,user_105,asset_501,48.03767711,-103.3447712
3/22/2019,Surface Location,Lease Road,,,,Weather,3/22/19 Plowed location access road & turnaround. Well is ready for ops to attempt to RTP.,user_42,asset_1784,46.2356189,-100.6010498
1/2/2019,Separator,Fuel Supply System, Big Joe Regulator,,,freeze,"big joe frozen, probably from burner being out and glycol cold",user_31,asset_484,48.257296,-102.8606112
4/17/2019,Instrumentation,Meter,Orifice Plate,Control Micro,4203DR,Weather,"Found Liquids in Sensing Lines, Blew down Lines and check zero Meter back in service; Test through Sams",user_139,asset_1544,,
12/7/2016,Gas Scrubber,,,,,,Scrubber pot was full and the drain was froze thawed scrubber drain line and got supply gas running,user_100,asset_12,48.09992917,-103.6536052
5/30/2017,Wellhead,Tubing,,,,,"Still froze down hole, equalized and left meth going, turned up heat on heat trace will have to come back later to let this work awhile ",user_131,asset_202,48.01297614,-103.7328962
6/4/2019,Wellhead,Plunger,Lubricator Top,Trip Mate,,Corrosion,"wasnt corrosion, but lack of lube, when screwing cap on, lubricator, cut the o-ring, causing a leak, of paraffin, and grease.",user_77,asset_2010,40.5262342,-113.8824849
8/27/2019,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue," CL 32-45 was down on high tank when I got here, water tanks #02,#03,#04 at 18-1x15-0 called ibex and got them to haul tank, RTP site had to vent well for an hour but it unloaded and I sent back to sales. ",user_37,asset_796,48.2712224,-102.8704416
12/25/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced and pit water,user_141,asset_1633,48.1603927,-103.6171977
4/24/2019,Separator,Liquid Dumps,Controller,Norriseal,,Liquid, +LIQUIDS IN MANY OF THE DUMP CONTROLLERS- CHECKED ALL DUMP CONTROLLERS. * DRAINED LIQUIDS AND ADJUSTED WHERE NEEDED,user_34,asset_1404,43.56424,-91.351691
1/4/2019,Separator,Manual Drain Valves,Body,,,Freezing,"scrubber was full of liquid, drained scrubber",user_31,asset_2135,48.257296,-102.8647072
12/10/2016,Tanks,Valving/Swedges,Seat/Ball/Piston,,,,"4"" load line frozen on water tank ",user_23,asset_1578,48.05397681,-104.8582439
2/28/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"Well logged off, vented for 118 min, got on slug out of well, shut in for pressure build will reset cycles and watch if plunger makes an arrival all is good if it struggles will vent for the 2nd time and reset cycles if DP is good, could not find any reason well logged off, no issue with leaks.",user_115,asset_1793,,
3/13/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Lost plunger arrivals, needed a vent.",user_95,asset_1646,48.11406143,-103.5972198
2/15/2017,Tanks,Manway,Gasket,Other,Other,deterioration,"Man-way is seeping oil. I have a full load of oil called in, so I can start prepping tank to be worked on once load has been hauled off. ",user_117,asset_1032,55.3918883,-118.3834219
6/16/2019,Separator,Liquid Level Control,,,,,"leaking condo dump blowing gas, adjusted so it quit",user_31,asset_1753,43.56424,-91.351691
4/21/2018,Fuel Gas/Start Gas,Regulator,,,,,Issue: well shut in alarm. (INT) valve fault Root Cause: found the fuel gas to the desi and back was lined up wrong and the big joe froze from getting wet gas Fix: broke big joe freeze relined up the valves to properly go to the desi and get dry warm gas back to the scrubber ,user_136,asset_612,48.1470144,-103.6180489
6/6/2019,Automation,Cyclonic Valve,Actuator,,,Freezing,Wyolectric found the actuator burned up. Replaced actuator and verified operation.,user_108,asset_316,,
9/3/2019,Flare System,Flare Header,Regulator,,,,"scc out found low psi on regulator, adjusted and lit scc",user_144,asset_2053,48.1470144,-103.6180489
12/9/2017,Separator,Choke Valve/Loop,,,,Freezing,,user_126,asset_814,,
2/8/2017,Wellhead,Other,Other,Other,Other,Other,"Tubing flow path hydrate, Tubing was blocked by a hydrate. Meth was pumped over night and heat was aplied directly to the tubing. ",user_130,asset_1337,48.05468374,-103.5590603
12/7/2017,Tanks/Pits,Flare/Combuster,,,,,"SCC ""A"" Pilot Burner extinguished due to Low pressure Regulator Freeze. Design goes from 1"" Pipe to 1/4"" pipe, back to 1"". Thawed manually with Thaw Tube and Relit.",user_138,asset_855,48.16968647,-103.4459538
4/1/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Well was loaded I vented plunger to surface and put back on plunger cycles.,user_51,asset_2215,48.1470144,-103.6180489
8/27/2019,Plunger System,Plunger,Plunger,PCS,,Corrosion,Well was missing plunger arrivals and needed a vent and inspection. Vented plunger to surface and inspected and replaced plunger. Rtp'd,user_10,asset_1746,48.224585,-103.8291059
11/17/2017,Automation,Battery,Battery,Universal,Blue Top,End Of Useful Life,"Was contacted by water haulers that heater in hand scan building at offload site wasn't working. Stopped by to look at it, see if we needed an automation tech, and found the batteries in the thermostat where dead. Got some batteries from the warehouse and replaced them. Heater is working now.",user_141,asset_987,48.1004946,-103.5858917
10/23/2017,Compressor - Gas Lift,Compressor,Panel,Ajax,,Electrical Short,"Compressor went down on high discharge pressure. discharge pressure was fine, compressor RTP'd",user_24,asset_387,40.5262342,-113.8824849
1/7/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"Vented well due to being loaded. Plunger arrived, RTP'd well, started cycles, and return to optimizer.",user_141,asset_1388,48.1470144,-103.6180489
2/11/2018,Gas Scrubber Separator,ESD,,,,,Issue: well is down and ESD wont open Root Cause: the packing in the actuator body went bad and is allowing the gas to blow buy and out the vent causing the valve to not operate Fix: wrote a work order for automation to replace the top works ,user_136,asset_661,48.2595091,-102.9010563
1/6/2019,Heat Medium,Pump,Cam,Goulds,HBC1,Electrical Wiring,"Scrubbers and dump lines frozen due to no glycol heat trace. Solar glycol pump down on speed controller fault. Post conversation with AUTO tech decision was made to code to maint to troubleshoot and RTP pump then verify circulation to front end of units/wellheads and ensure warm circulation to compression, troubleshoot circulation issues. WM created.",user_54,asset_1174,40.5262342,-113.8824849
10/10/2019,Separator,Fuel Supply System,Regulator,,,wear,"Well call out/ shut in on low unit pressure . Jumped ad pad up and installed burp setting in the front end choke to help keep the pad up. This pad would benefit from a down stream valve on the 120 well, work order has already been turned in. Rtp'd wells",user_10,asset_478,40.5262342,-113.8824849
10/7/2018,Separator,Temp Control System,Thermostat,,,,glyol level too low to have correct temp control- order glycol,user_31,asset_1405,43.252261,-115.0567324
12/7/2017,Tanks/Pits,Tank Level,Sensing Cable,,,Weather,True high tank needs to have a pull bottom done and transfer,user_51,asset_1970,48.1470144,-103.6180489
6/2/2019,Instrumentation,Controller,,,,,Fisher DVC6200. Positioning slide out of adjustment. Device tests okay after correction.,user_12,asset_1139,40.5262342,-113.8824849
7/3/2019,Chemical System,Pump,Check Valve,Texam,HBC1,Wear,small check bad on pump,user_64,asset_909,38.4425988,-95.5406131
4/1/2017,Gas Scrubber,Other,Other,Other,Other,Other,Loss of production ,user_175,asset_1403,47.96337372,-103.6986715
4/15/2018,Tanks/Pits,Berm,Steel,,,Erosion,Pit fence need repairs or replaced due to erosion and water haulers hoses made some bad spots. ,user_58,asset_876,48.41610629,-103.5771844
2/16/2018,Fuel Gas/Start Gas,Regulator,,,,,"freeze in hi/lo bypass valve, took unit dow, thawed and RTP",user_88,asset_1819,48.2575134,-102.9115358
11/6/2019,Chemical System,Pump,Packing,Texsteam,HBC1,Air Locked,"low glycol, pumps shut off til bath gets topped off. glycol ordered",user_17,asset_1274,,
8/19/2019,Separator Inlet Valve (XV),Valves,,,,End Of Design Life,The Hi/Lo body was washed out and was replaced with a complete new assembly.,user_68,asset_2075,40.5262342,-113.8824849
6/24/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Brought up plunger ,user_86,asset_1225,,
2/9/2018,Flare System,Flare Header,Instrumentation,,,,Issue: flare down Root Cause: Hi winds blew pilot out and the sparker isn't working Fix: took flare down relight and then put back up and returned to service ,user_136,asset_705,48.1603196,-103.6176623
9/7/2019,Tanks/Pits,Flare/Combuster,,,,,"relight scc, adjust pilot psi, no igniter or esd. scc out due to wind/rain",user_64,asset_1772,40.5262342,-113.8824849
12/13/2016,Wellhead,,,,,,"Plunger loaded off,vented and RTP'd optimizer looking at cycle times",user_115,asset_1961,48.10275299,-103.6773831
3/22/2019,Surface Location,Lease Road,,,,Weather,3/22/19 Plowed location access road & turnaround. Well is ready for ops to attempt to RTP.,user_42,asset_1824,46.2356189,-100.6010498
5/8/2019,Wellhead,Wellhead Piping,,,,,2 inch valve off well head piping leaking. Shut well head in blew down line ,user_19,asset_1467,46.2356189,-100.6010498
1/6/2018,Tanks/Pits,Flare/Combuster,,,,,B scc pilot out. Relit. Not sure why this one went out ,user_156,asset_21,48.18123413,-103.6144952
7/13/2019,Automation,Radio,,Cambium,,End Of Useful Life,Cambium PMP-100 radio failed.,user_12,asset_562,46.2356189,-100.6010498
5/7/2019,Chemical System,Pump,Diaphragm Gears,Goulds,HBC1,Weather,"lightining, caused us to stop the job, until management approved , to continue.",user_77,asset_1435,40.5262342,-113.8824849
12/16/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Well was down for non arrivals. Kicked well on and paused it open. Plunger arrived, returned well to production.",user_141,asset_436,48.1470144,-103.6180489
7/9/2019,Pumping Unit,Liquid Level Control,,,,,"Rod pump down on E-pot full, appears to be rain water, rtp pump and checked location",user_63,asset_705,,
2/17/2019,Separator,Fuel Supply System, Big Joe Regulator,Fisher controls,,freeze,"Burner out, froze fuel gas, will try to get burner lit, and pump going, just got another call out on a different well, same thing I think ?",user_77,asset_61,47.99935496,-103.6408992
2/3/2019,Separator,Fuel Supply System,Regulator,Fisher controls,67CR-206,overpressure,"OPS found line heater @ 120 site down and shut in with no tags. OPS Thawed fuel gas system and RTP'ed burner, found pressure regulators to T-12's, motor control valve and main burner fuel gas supply over ranging end devices. Regulators failed likely due to a freeze in the past. OPS replaced both regulators and RTP'ed burner. Set pilot PSI to 5, burner main to 8 and T-12's to 25. Verified bath came up to temp and was able to shut off. Left setting @ 140 F. ",user_54,asset_599,40.5262342,-113.8824849
4/4/2017,Heater Treater,Other,Other,Other,Other,Other,"No damages,",user_84,asset_1169,48.06007322,-103.5123125
5/1/2019,Plunger System,Plunger,Plunger,IPS,,Not Optimized,"well was logged off and had a large deferral. went had originally loaded up due to a lateral freeze and the downstream kimray was not shutting in an off cycle. started troubleshooting downstream valve. valve was 100% open in an off cycle and was still open when you sent it a shut in command. has sufficient fuel gas and was dry. could not find any issues with valve. contacted automation to help troubleshoot over the phone.started looking through valve open criteria and found the burp setting on the valve was set at 100psi. with this setpoint entered in this valve would never close unless unit pressure dropped below 100psi. adjusted burp setting and function tested valve. valve is now working normal. vented well for around 54minutes. plunger came and differential pressures look good. 780 on tubing 841casing. put well in an off cycle, let plunger drop. well has a bypass plunger but we are running 60 minutes of off time for some reason. well made its last three arrivals. coding over to optimizer to cut down on some of the off time. if we are unable to cut down from the 60 minutes. i recommend removing bypass and running a bar. was unable to relit flare due to the ceramic insulator on igniter being cracked. verified glycol pumps are circulating heat. relit all abutec sccs.gauged tanks. water tank at 13' turned into fluid management. tested surface equipment for leaks. did not find any issues.",user_120,asset_2069,40.5262342,-113.8824849
4/11/2017,Gas Scrubber,Other,Other,Other,Other,Other,Na,user_166,asset_1707,48.11118673,-103.6455892
2/21/2019,Fuel Gas/Start Gas,Regulator,,,,,"DVC frozen cannot get choke to open up and sell. Cannot get close to quad packs at all to thaw on the front end fuelgas. Turnaround has been plowed but not access to equipment, put in a work order to plow a path and hand dig the first quad pack that has 5' snow drifts in front of it. Baths are up and warm and 3 wells are flowing good",user_106,asset_197,48.1470144,-103.6180489
12/19/2017,Compressor - Gas Lift,Compressor,Process Gas Supply,Ajax,,Vibration,"Compressor B down due to hot gas fitting failure. Arrive on location and inspect. Determine the 1/4” By 1/2” NPT fitting failed due to vibration within system that caused the pipe racks for the suction, discharge recycle and fuel gas lines to settle pulling the fitting until it failed. Contacted and informed engineering. Approval received to repair and add support under hot gas supply line to prevent another occurrence. 30 and 90 well fed by compressor A down during this repair for <2 hours due to fuel gas lock out for repair. Leak test repair. Good. Begin unloading operations. Start and warm compressors. Begin injecting gas to start unloading wells. 30, 90, and the 120 unload to sales and show signs of pumping off near or to orifice valve. 30 injecting at .75 mmscfd at 779 psi. 90 injecting at .72 mmscfd at 825 psi. 120 injecting at .51 mmscfd at 762 psi. The 150 well began to unload at 954 psi csg and is currently injecting at .72 mmscfd at 962 psi. Csg pressure climbing slowly. Will continue to monitor the 150 for signs of continued unloading. ",user_75,asset_1452,,
4/9/2019,Chemical System,Pump,Check Valve,Sunpumper,HBC1,Air Locked," 4/9/2019 110 well froze in wellhead again, solar glycol pump was fixed and now both solar pumps aren't pumping, possible low level in line heater so ordered glycol. All of the methanol pumps were air locked again, took apart at wellhead and verified that check valves were good and getting methanol at tree, found a bad check valve on the 110 well so replaced it and got pumping again. ",user_31,asset_2040,43.56424,-91.351691
3/9/2019,Wellhead,Manual Valve,Master Valve,,,Freezing,,user_34,asset_1078,48.1470144,-103.6180489
1/8/2017,,,,,,,Returned well to production after pressure build,user_35,asset_54,48.09248139,-103.4977354
10/9/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,Load line valve found leaking on tank,user_150,asset_2121,40.5960545,-113.9323891
2/13/2018,Separator,Choke Valve/Loop,,,,Corrosion,Root cause not listed. Choke found pinched on plunger cycled well with downstream rate control. Opened choke to 64/64”. See full resolution comments below. Arrow dispatch for Fed based gauge. Gauge oil and water tanks. No hauler action requested. Pull graphs while on location. Find plunger missing arrivals. Graph indicates the plunger is freezing in lubricator. Pull coding history to find out if well has had this failure in the past. Confirmed well has a history of hydrate hanging plunger in lubricator. Check methanol. Tank over 90% full. Find methanol pump stalled out. Regulator backed off due to vibration to 20 psi. Increase back to 30 psi and methanol begins injecting. Find choke at 30/64”. Rate is controlled on this site by the cyclonic downstream. Open choke to 64/64”. Well head recently re insulated. Valve access on tbg and csg sweep not cut back to access for actuation. Cut insulation back for valve access. Dig out dirt accumulation on berm stairs to tank. No further action needed. ,user_75,asset_494,,
6/17/2019,Instrumentation,Controller,,,,,Fisher DVC6200. Magnetic position feedback slide had fallen off.,user_12,asset_370,40.5262342,-113.8824849
1/12/2018,Tanks/Pits,Flare/Combuster,,,,,3 of 4 SCCs out due to high wind. Relighted,user_163,asset_1339,48.1470144,-103.6180489
11/21/2018,Separator,Temp Control System,Fuel Gas Supply,,,,"burner was shut off, started burner",user_31,asset_696,43.252261,-115.0567324
5/24/2019,Instrumentation,Meter,Orifice Plate,Control Micro,4203DR,Passed Function Test,Found that the meter shows both Volumes for Luman 17-1 and 17-80 but only on 17-80. The PLC can only control on the Luman 17-80. The Luman 17-1 Volume will not show in SAMS. I will sent email to Trevor to show communications on that control Configuration.,user_139,asset_398,,
3/30/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,fluid,The scrubbers on separator A had a significant amount of fluid drain from it. We are using such a high volume of supply gas on this pad that there is limited retention time for fluid to drop out of the supply gas. I think this pad would benefit from cold fingers. ,user_50,asset_1393,47.95035331,-103.3856641
9/7/2019,Automation,Antenna,,Bluewave,,Loose Connection,"Wells called out on high tank and are shut in / gauged condo tank 18ft 4in x 10ft 4in called to have tanks hauled . This pad is also in comm error so I just not get the interlocks to clear when the condo tank does get hauled, w/o turned in to automation. Live reads on this location are not working looks like work order to already been turned in.",user_10,asset_863,40.5262342,-113.8824849
3/21/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Attempt to vent up plunger, non surface due to downhole issues. Request wireline to pull and engineer evaluation on tubing issues",user_35,asset_76,48.185059,-103.5003089
2/24/2018,Separator,ESD Valve,Gas Supply Line,,,Freezing,Scrubbers are ball checked lossy fuel gas. Supply line to esd froze. Baths are cold. Thawed out fuel gas got esd open and well rtp on plunger cycles,user_172,asset_113,,
11/14/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Desi and fuel gas of liquids ,user_109,asset_1676,48.3272265,-103.6564851
3/21/2017,Tanks,Shell,Body,Other,Other,Other,Corrosion in tank bottom led to hole and contents of tank spilled out. Turned in to team lead to get fixed,user_35,asset_285,48.36384056,-103.6043183
10/27/2018,Separator,Choke Valve/Loop,,,,Corrosion,2'' 10M CYCLONIC AT BLOW DOWN IS LEAKING THROUGH THE STEM AREA. WM ENTERED,user_34,asset_1442,48.1470144,-103.6180489
3/21/2019,Sales Valve (PV),Sales Valve,Pie Disks,Automax,,Washed Out,"Automated valve was 10% open I had Travis close it and I closed both block valves before and after it and blew vessel down to 0, it slowly pressured back up to 200 psi, I believe all three valves are washed out and need replaced or repaired. left automated valve closed and block valves open",user_22,asset_2271,46.2356189,-100.6010498
3/20/2019,Fuel Gas/Start Gas,PSV,Body,,,Weather,"scrubber psv releasing gas at 20#. able to reset. will need tested or replaced prior to rtp. probable cause big joe freeze and scrubber initial overpressure, then froze",user_17,asset_2096,,
11/20/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,NO fluid in system. it was dry RTP'd well after construction worked on buy back meter.,user_0,asset_764,48.1470144,-103.6180489
3/9/2017,Automation,Solar Panel,Other,Other,Other,Other,none ,user_65,asset_1047,48.224585,-103.8291059
8/11/2017,Wellhead,Choke Valve,Body,,,,started cycle found that dvc was not opening choke. i gave the dvc with a tap and it started controlling choke i paused cycles till plunger arrived then resumed cycles after plunger arrived.,user_11,asset_1868,,
11/17/2016,Gas Scrubber,Shell,Body,Other,Other,Corrosion,"Found fuel gas supply that feeds line heater froze at line heater. Also found scrubber pot full of liquid and float inside scrubber froze off. Thawed, drained and RTP'd. ",user_62,asset_1323,,
10/5/2018,Heat Medium,Surge Tank,Instrumentation,,,,"found a hammer union on #110 well that was leaking glycol, contacted TL about spill, tagged out burners to put bath in bypass to RTP wells on site",user_37,asset_1581,43.56424,-91.351691
7/26/2017,Instrumentation,Transmitter,3N1 MVT,ABB,3051,Recalibrated,"Wonder card not working. Reloaded program, verified production data updating in JSAMS",user_99,asset_604,40.5960545,-113.9323891
9/16/2018,Dehy,WFS Issue,,,,,"Well is down, well does not do well with high line pressure. SIPB overnight can be RTP'd on 17SEP18",user_56,asset_1441,48.2651462,-102.8788038
8/6/2018,Tanks/Pits,Shell,Body,,Steel,Corrosion,"Hole in lower side of shell about 4"" off the ground on the Water Tank / Blowdown tank",user_5,asset_1916,48.3619066,-103.2129855
7/24/2019,Separator,Choke Valve,Seat,,,,The automated choke was leaking by. The internal parts were replaced and is ready for calibration.,user_68,asset_583,48.1511815,-103.6272739
9/11/2019,Compressor,Engine,Battery,Ajax,,Weather,"Comm error got fixed. Dispatched to well, entire pad was down. Started by jumping the pad on and then allowed allowed baths A&C to warm up. Bath B needs a top off. RTP'd well Had to jump compressor and then got it warmed up and loaded RTP'd compressor",user_56,asset_1996,48.1470144,-103.6180489
5/22/2018,Tanks/Pits,Piping,Load Line,,,Corrosion,4” Load line valve on water tank found leaking through inner valve and tee on load line was found to be cracked and leaking,user_150,asset_535,,
10/30/2017,Compressor,Compressor,Process Gas Supply,Ajax,,Freezing,Lack of wells flowing to compressor resulted in low suction pressure set point to kill compressor. 3 of 5 well flowing. 2 awaiting swab. ,user_75,asset_998,,
4/20/2019,Sales Valve (PV),Sales Valve,Body,Valvcon,,End Of Useful Life,Salesline cyclonic valve was leaking around the stem. The valve was replaced.,user_68,asset_662,48.1470144,-103.6180489
6/17/2019,Separator,Choke Valve,Stem,,,,Replaced leaking choke,user_21,asset_669,40.5262342,-113.8824849
3/5/2018,Separator,Dump Line,,,,Freezing,Lost unit pressure. Below 0 temps. No heat all dump line froze. No fuel gas buyback. ,user_156,asset_2151,48.27159033,-102.8691265
1/19/2019,Surface Location,Well Pad,,,,Weather,surface equipment inaccessible due to large amount of drifted snow,user_17,asset_704,,
11/28/2017,Pipeline/Piping,Pipe/Components,,,,Human Error,Wellhead heat trace was not re-installed and wellhead was not re-insulated after well work. Both completed now.,user_161,asset_847,40.5262342,-113.8824849
5/22/2018,Sales Valve (PV),Sales Valve,Body,Automax,,Wiring,While rtp a well could flow in off cycle. After troubleshoot determined sales line cyclonic valve body stem flow direction was stamped backwards. Well flowing normal now,user_35,asset_2003,48.17917822,-103.4307652
10/22/2018,Separator,Temp Control System,Coils,,,,"Separator inlet on flowline by blowdown valve, insulation had holes from animales and hail damage, flowline was exposed, repaired insulation",user_31,asset_1497,43.252261,-115.0567324
12/5/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,Load Line Valves on Condensate Tanks Found Leaking,user_150,asset_1060,40.5262342,-113.8824849
1/18/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,Well was knocked odwn due to the local line pressure spike experienced. Plunger was vented up and RTP'ed. OPS adjusted high line PSI set-point for the this well to accommodate any future line psi spikes. ,user_6,asset_1401,,
10/25/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,4” Load line valve on both water and condo tank found leaking.,user_150,asset_27,,
2/27/2018,Compressor,Compressor,Valves,Ariel,,Trash,"Discharge temp too high, opened doors to allow better cooling.",user_95,asset_524,48.09528463,-103.6432061
9/20/2017,Compressor,Compressor,Suction Controller,Ariel,,Freezing,compressor down on low second stage interstage pressure. blew out suction control valve to check for freeze there was none. i do have the 70 well shut in waiting on choke parts. this well has a ten min off time so im thinking the compressor went down due to excessive off time with the other wells maybe should look into a better recycle valve,user_11,asset_1154,48.3619066,-103.2129855
5/13/2019,Fuel Gas/Start Gas,Valves,,,,human error,"pad went down on lolo psi and esd valve miss alignments, found only 20 psi supply psi to esd valve, checked cold finger and regulators , no liquids found , found only 50 psi at scrubber and scrubber was dry, found 1'' valve to supply gas big joe was closed and no tag, opened valve and got 100 psi to scrubber, verified big joe is set correctly ",user_144,asset_1642,40.5262342,-113.8824849
4/9/2018,Dehy,WFS Issue,,,,,lateral freeze broke by williams operator. put well back into service.,user_11,asset_1723,40.7126799,-114.1193569
11/28/2017,Compressor,Intrumentation,,,,,"Down 3rd part, Williams plate change knocked down pad and compressor ",user_109,asset_1401,48.3534609,-103.6555327
9/8/2019,Separator,Liquid Dumps,Controller,Norriseal,,Improper Adjustment,"dispatched to location for low production, pulled graphs and found yesterday tubing psi dropped , showing signs of a stuck dump or valve left open, got to location and found stuck condo dump, found controller was set to sensitive , adjusted controller and got dump working properly,",user_144,asset_756,40.5262342,-113.8824849
1/24/2018,Tanks/Pits,Flare/Combuster,,,,,Relit all SCC's. Pilots were extinguished after losing fuel gas supply pressure. Whole pad went down. Sacraficial well not supplying enough gas to keep the pad up. ,user_41,asset_1892,48.21017269,-103.6495084
3/17/2018,Tanks/Pits,Liquid Level Control,,,,,"Issue: called out hi tank alarm Root Cause: Human Error/Dispatch, real hi condo tank Fix: got a hold of dispatch and got the tank pulled and turned the well back on",user_136,asset_1212,48.1470144,-103.6180489
7/26/2018,Flare System,Flare Header,BMS,,,,Issue: Called out SCC alarm. (INT) SCC (A) down no pilot flame Root Cause: a ground pounding rain storm came through and flooded out the pilot knocking down the SCC Fix: i was able to relight remotely. May look into putting the pilot horizontally instead of vertically and may not get flooded out as often ,user_170,asset_103,48.224585,-103.8291059
2/4/2017,Compressor,Compressor,Process Gas Supply,Other,Other,Other,Compressor won't push against it ,user_175,asset_934,47.8645424,-103.5280916
1/31/2019,Separator,Liquid Dumps,Seat/Ball/Piston,Norriseal,,Erosion,"condo dump was blowing a full stream of condo, replaced packing and trim set",user_31,asset_1892,43.56424,-91.351691
2/8/2018,Flare System,Flare Header,Regulator,,,,"adjusted reg. and relite,",user_84,asset_1803,48.1470144,-103.6180489
3/29/2018,Tanks/Pits,Valving/Swedges,Body,,,Trash,Opened all condo tanks on location to operate battery as facility to maximize condo capacity onsite and align with predictive dispatch tools. ,user_62,asset_425,48.1470144,-103.6180489
3/14/2018,Separator,Choke Valve/Loop,,,,Freezing,Freeze in the flow line and choke.,user_130,asset_700,47.87558179,-103.5256012
1/20/2019,Wellhead,Manual Valve,Master Valve,,,Erosion, +SEPARATOR AT 819 PSI +WELLHEAD SHUT AND TAGGED AT THE TUBING MASTER AND WING VALVE *** I WAS ABLE TO GET THEM A LITTLE TIGHTER AND MOSTLY STOP THE PRESSURE BLEED THROUGH FROM THE TUBING ** STILL NEEDS THE VALVES GREASED. **WM IS IN PLACE,user_34,asset_1026,43.56424,-91.351691
11/4/2019,Separator Inlet Valve (XV),Pneumatic Control System,Spring,,,,Inlet to separator was froze,user_97,asset_713,46.2356189,-100.6010498
4/5/2017,Instrumentation,Tank Level,Other,Other,Other,Other,i switched over to other circuit inside high tank switch,user_92,asset_380,48.0614644,-104.8417043
5/11/2019,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,High tank alarm I went to location and 40874c 3ft 7in x 0ft 4in 40874w 6ft 10in x 3ft 8in FALSE ALARM it dose not appear to have spiking live reads I went to so I think the HLA switch is faulty.,user_159,asset_2205,43.56424,-91.351691
12/7/2016,Compressor,Compressor,Instrument Gas Supply,,,Freezing,"Compressor down on low suction, found fluid in lines to control panel, starter button was also froze. Thawed lines and drained fluid, hopefully this fixes it.",user_148,asset_1124,48.32432663,-103.6004106
12/21/2017,Separator,ESD Valve,Gas Supply Line,,,Freezing,,user_48,asset_385,48.21154443,-103.638478
10/7/2018,Separator,Choke Valve/Loop,,,,Freezing,"Froze, blew backwards and rtpd",user_94,asset_530,,
1/3/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,"4"" Load Line Tee froze and broke",user_5,asset_2266,49.3189309,-101.9779473
7/25/2019,Pipeline/Piping,Piping,Connections,,,Connections," Production line over by wellhead has a gas leak. Driving by today leaving the 23 10 dog house, I noticed some condo on the ground puddled up, so I went and investigated and noticed that there was a gas leak, and spitting condensate out as well. So instantly shut well head in, and then secured location and contacted TL, shut in rest of location. Going to code and turn into maintenance to inspect and fix. DUPLICATE WORK MANAGEMENT ",user_68,asset_1099,48.1470144,-103.6180489
5/27/2018,Pumping Unit,Engine,Plugs,Ford,,Corrosion,Replaced all 6 spark plugs in attempt to RTP pumping unit. Spark plug #6 was heavily oil fouled & corroded.,user_161,asset_1658,40.7126799,-114.1193569
4/2/2018,Compressor,Compressor (Intergral),Process Gas Supply,,,,"MC 3-pad down on valve fault, comp down on low discharge. when comp went down pad didn’t have enough fuel gas because most of the wells are pulled down below 90psi. jumped pad on and restarted comp ran the rest of the night.",user_71,asset_2148,48.1470144,-103.6180489
7/17/2018,Gas Scrubber Separator,ESD,,,,,Issue: called out shut in alarm Root Cause: found the buyback gas is shut off and the compressor is using up all the pad gas recycling. Fix: i opened up the buyback gas and watched it for a while to make sure it wasn't just gonna flood out the fuel gas. was doing good so i turned the well back on and returned to service ,user_170,asset_1193,48.1470144,-103.6180489
1/15/2019,Pipeline/Piping,Pipe/Components,,,,Human Error,the pump building was not properly insulated for winter conditions,user_28,asset_523,48.1602754,-103.6180351
4/25/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,Issue: open choke up more Root Cause: well just came back on so its flowing on a pinched choke Fix: opened choke to a 27/64 and that's about as much as the dumps can handle without carry over ,user_136,asset_1345,48.2595694,-102.9009394
12/3/2018,Compressor,Compressor (Intergral),Battery,,,,Battery low ,user_94,asset_459,,
9/29/2019,Fuel Gas/Start Gas,Regulator,,,,,"units are flooding out fuelgas with condensate, both desi's had a lot of fluid in them and the scrubber pots did as well. Went through the units and separators one by one in cycles and found several dumps not dumping soon enough and flooding units. Did not make it through all separators and will need to go back and do some more adjusting. ",user_106,asset_18,46.2356189,-100.6010498
4/4/2017,Instrumentation,Other,,Other,Other,Other,,user_58,asset_616,47.93417615,-103.4061217
1/3/2017,Pumping Unit,Engine,Battery,Other,Other,Weather,Cold temp and engine not running drew the battery down ,user_74,asset_599,48.40985331,-103.585019
3/13/2018,Compressor,Engine (Gas),,,,,"Compressor was shut of for production test, Engineering team requested that the compressor be re-started. Arrived on location and found compressor off, inlet shut and tagged and batteries shut off. walked through all piping and made sure all valves were in proper order to start and run compressor. Started and warmed compressor, loaded compressor and am watching wells to see if any need unloaded to tanks.",user_62,asset_1905,48.1470144,-103.6180489
1/20/2019,Heat Medium,Pump,Process Indicator,Texam,HBC1,Power Supply,"regulator to both glycol pumps on the 10 well were frozen, thawed and started pumps",user_31,asset_674,43.56424,-91.351691
11/21/2017,Tanks/Pits,Flare/Combuster,,,,,Relit SCC. Pilot was extinguished after fuel gas pressure was lost. ,user_41,asset_333,48.20713337,-103.6133589
10/2/2017,Chemical System,Tank,Sight Glass,,,Weather,Sightglass plugged with garage ,user_156,asset_1496,48.19305831,-103.6413694
3/20/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,hydrate,Pad well called out on bath heater alarm and valve fault . Found that the solenoid for the main on the bath heater would not seal thawed valve and got valve to seal. The fuel gas to the esd had a freeze between the glycol bath and the unit . Thawed supply line and broke freeze rtp well/ bath heater,user_100,asset_2053,48.1470144,-103.6180489
1/17/2017,Compressor,Compressor,,,,,When trying to crank engine batteries were spewing out liquid. Shut down and called JW,user_88,asset_1154,,
4/11/2019,Heat Medium,Pump,Instrumentation,Texam,HBC1,Air Locked, • Skid B ? Found no power on motor controller ? Found low battery voltage at 23.9 Vdc ? Found prostar shorted out due to water damage ? Removed failed prostar ? Cleaned all wiring that went to prostar due to water causing electrical shorts ? Installed new prostar ? Tested and verified Prostar functioning correctly ? Tested and verified pump functioning correctly ? Left pump running at 2 Amps ,user_38,asset_2256,40.5262342,-113.8824849
9/11/2019,Pumping Unit,Engine,Clutch,Cummins,,Wear,"Arrived onsite to troubleshoot pump / clutch issue. Chain lakes 29-155H. Pumping unit is rtpd in automatic at 3.76 spm. I tightened the clutch 8 notches and adjusted the clutch actuator to extend 2 ""wheel widths"" further out. I noticed the jack shaft bouncing, so I tightened all 8 bolts that mount the jack shaft horizontally to the tilt control and the horizontal mounting plate welded to the engine. I used a 12"" crescent and 1/2"" drive socket as this was all I had. I did ask Weatherford mechanic to double check the tightness when he services the engine tomorrow. I feel the power band is slightly loose, but not slipping it has a brief struggle to lift the weights from 7 to 9 o'clock then it's good. I verified that a slightly loose power band is acceptable to operate with Mr Hoffman. I'm planning on having Weatherford crew out to annual PM the units on 9/24, so we will tighten power band then if not before. Entered surface failure & observation in Safety 3.0.",user_42,asset_1823,46.2356189,-100.6010498
10/16/2019,Gas Scrubber Separator,Dump Line,,,,Freezing,"Drained the Dezi took about 12 seconds, drained the scrubbers both to about 2 seconds, drained all the drip pots, and all the pressure regulators.",user_76,asset_386,46.2356189,-100.6010498
7/23/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_1489,40.5960545,-113.9323891
9/21/2019,Tanks/Pits,Shell,Body,,Steel,Corrosion,Steamed washed the tanks and found a tank leak. Turned in for tank replacement.,user_21,asset_2087,46.2356189,-100.6010498
11/8/2017,Compressor,Compressor (Intergral),Process Gas Supply,,,,compressor called out and showeed down on Emerson. was running when i arrived. day shift operator must have started at end of shift and not been able to answer callout?,user_71,asset_1675,48.1470144,-103.6180489
6/15/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_1489,48.1001903,-103.5869983
9/11/2018,Tanks/Pits,Flare/Combuster,,,,,"A scc out. Took apart and cleaned a moth out of pilot tip, relit",user_31,asset_1493,,
2/13/2019,Separator,Temp Control System,Flame Arrestor,,,,"arrestor completely covered in snow drift causing burner to go out, also arrestor housing packed with ice. try to dig out and chip away ice.",user_64,asset_376,40.5262342,-113.8824849
9/21/2019,Wellhead,Manual Valve,Master Valve,,,Fouling,"Replaced bad grease fittings on the valves, re greased valves and worked them to hold pressure. Returned them to service",user_21,asset_2245,46.2356189,-100.6010498
2/28/2019,Fuel Gas/Start Gas,Regulator,,,,,"Pad has been down since January 27th. Went down i'm assuming in one of our winter storms, there is a lot of fluid in the fuelgas system, guessing burners went first then the freezing and flooding. Pad was inaccessible for quite some time due to weather. Was able to isoalte, blow down and drain scrubbers, got fuelgas to the front end and scrubbers and was able to get burners to both quad packs up and going. All water dump lines are frozen and some of the condo dump lines. Checked tanks, condo tanks are not frozen and was able to get to the bottom, Water tanks have ice shlelves and are frozen around 5', hoping with warmer temps and warm glycol we can thaw these over a couple of days if not a steamer and or hot oiler may be needed. the Glycol path to water and condo tanks had caution tags on them and were shut off. Talked with Cragoe who had put them there and they were only supposed to be pinched on both sides from when we were having difficulty getting eat trace to compressor, they now have an additional pump for that when it is up and running. Opened up the water side completely to get good heat trace going, all glycol pumps are functioning and getting warm as bath temps come up. Open up this well with a burp setting to keep the pad up and the heat going, re-evaluation needed in a day or 2 to check the dump lines and see if we are clear or if we need additional resources. Whoever comes back will need to check the water tanks and see if we are thawing out. Will code this well as waiting on operations. ",user_106,asset_1239,39.2506642,-92.4357879
5/24/2019,Automation,Sensor,,,,,Driver has not been able to hand scan in since original hand scan done at office. Have had difficulty catching up to see exactly what has happening. Contact Justin R with Automation. Gave him drivers name and login password. He found the issue. Verified driver is able to hand log in. All good.,user_55,asset_2012,,
3/3/2019,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Well loaded up due to fuel gas usage. Attempted to vent with no luck. SIPB for vent at a later date,user_147,asset_1615,,
6/26/2017,Wellhead,Cyclonic Valve,Actuator,,,Freezing, 2. West Wamutter 33-140 - Cyclonic stuck at 5% (Deferral) • Found cyclonic actuator stuck at 5% • Found blown relay and cyclonic fuses • Replaced fuses • Verified actuator now working correctly ,user_92,asset_1690,48.1470144,-103.6180489
8/27/2019,Fuel Gas/Start Gas,Regulator,,,,,Block and bleed leaking. Also found spring off. Replaced block and bleed and reinstalled spring,user_55,asset_1748,,
5/31/2019,Pumping Unit,Pumping Unit,Bridle,Weatherford,Model 912,Improper Installation,"Replaced pumping unit engine battery. Weatherford crew attempted to install load cell, but rig did not have pump set anywhere close to tag, and Weatherford crew did not have any ponies so we could not space pump and install load cell. Stop the job today, Weatherford is hot shotting ponies and work will continue tomorrow 6/1/19 per PTL directive. Surface failure and STJ observation entered.",user_42,asset_298,46.2356189,-100.6010498
7/1/2018,Wellhead,Casing,Intermediate Casing Head Valve,,,,WWD 12 casing was at 188psi at 11:00 got to location at 11:40 it was at 238psi shut down injection pump and notified TL. Blew down casing at no shock valve bleed just before transmitter to 6.1psi had about 12 gal of water in it finished at 12:30. ,user_71,asset_523,48.1470144,-103.6180489
4/1/2017,SWD System,Other,Other,Other,Other,Other,,user_117,asset_1633,40.7126799,-114.1193569
7/30/2019,Instrumentation,Meter,Orifice Plate,Control Micro,4203DR,Recalibrated,Complete Scheduled calibration ,user_139,asset_734,48.16031274,-103.6183828
1/8/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Plunger vented in. During discussion with OPT, found max flow setting to be 1.1mmcf (set there during compression operations) and should be set @ 2.2 MMCF since the compressor was shut down. This casuing slow arrivals and even non-arrivals. OPT reset sales valve set points and reset cycles.",user_6,asset_695,36.2541889,-91.2478009
4/22/2018,Flare System,Flare Header,Process Indicator,,,,Flare out relit and returned to service ,user_58,asset_1417,48.37291744,-103.5169273
11/5/2019,Chemical System,Pump,Instrumentation,Goulds,HBT2,Power Supply,"drained scrubbers, walked down pad, looking for closed glycol valves, found no closed valves, turnened in a W/M to have pressure washer crew hook up to pump discharge lines and pressure them up to see if we get return flow, possible kink or freeze, or just cold glycol causing pumps to overload on start up. and blow fusses, bath temp is good, but lines are starting to freeze, as well a water tanks, put it as priority 1, and called scott schmidt, to try and get a crew asap. ",user_77,asset_943,39.2506642,-92.4357879
3/27/2017,SWD System,SWD Pump,Other,Other,Other,Other,Pump down due to plugged filters,user_141,asset_1918,48.224585,-103.8291059
12/10/2018,Pipeline/Piping,Pipe/Components,,,,hydrate,Frozen dump line on WFS dehy parted at hammer union,user_61,asset_1383,48.2616379,-102.8778605
3/16/2018,Heater Treater,Burner,BMS,,,Corrosion,Issue: found the bath was 110deg on the HMI with wells flowing 90deg+ Root Cause: found the T-12s had fluid in the fuel gas. that comes from the wells flowing to hot and carrying fluid in the fuel gas Fix: drained the fluid out and turned the T-12 down,user_136,asset_592,48.2594738,-102.9011108
11/9/2019,Separator,Choke Valve/Loop,,,,Trash,"Choke wouldn't open. Blew down fuel pot, had some moisture in it. Tapped on DVC, started working. Opened and closed choke a few times to verify operation. RTP'd well",user_55,asset_627,,
1/14/2019,Heat Medium,Furnace,Process Indicator,,,,"burner is out on 4 pack and T pack, both got ball checked on scrubber being full of liquid",user_31,asset_1423,43.56424,-91.351691
3/16/2018,Wellhead,Wellhead Piping,,,,,Shoot fluid level down casing of well. 314 foot of fluid above end of tubing. Information sent to engineer for review.,user_62,asset_1782,48.1470144,-103.6180489
2/28/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Vented plunger to surface,user_84,asset_5,48.15477644,-103.5407908
4/5/2018,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,"Issue: called out well shut in alarm (INT) low MVT pressure Root Cause: wells stayed shut in to long and the 4glycol pumps, 2 burners, 4 SCC's and methanol pumps used up all the unit pressure and the wells shut in on low unit pressure Fix: jumped location back on and left one well flowing to keep the pad up. Long Term Fix: pad is grosley over sized for the wells on this location. Engineering really should review the location and see if we really need all the equipment and review the amount of fuel gas it uses for the amount of wells we have on location ",user_136,asset_1897,48.2593797,-102.901033
1/9/2017,Instrumentation,Transmitter,Tubing Pressure,Rosemount,,Installation Design,Tubing transmitter freeze,user_50,asset_601,47.99335943,-103.4436681
5/7/2018,Flare System,Flare Header,Process Indicator,,,,"Scc out, attempted to adjust igniter and eventually relit manuely and returned to service ",user_58,asset_580,48.37291283,-103.5168232
4/14/2019,Tanks/Pits,Tank Level,Sensing Cable,,,Weather,Well was shut in on high tank I went to location and gauged tank it was pulled down to 8ft 5in I brought the well back online and restarted plunger cycles relit the burner and SCC ,user_159,asset_409,43.56424,-91.351691
5/26/2018,Tanks/Pits,Flare/Combuster,,,,,"Did location walk down, appears SCC was shut off to have sump pulled. Pilot and main were closed with no tags and I could see hose marks and tire tracks by sump. Lit SCC.",user_62,asset_1274,40.7126799,-114.1193569
5/9/2018,Pumping Unit,Engine,Crank Shaft,Ford,,Wear,Replaced pumping unit engine rear main seal and RTP'd.,user_161,asset_1658,48.267245,-102.9231841
7/28/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Checked for fluids in green complete separator. No fluids present. ,user_15,asset_1383,48.1470144,-103.6180489
10/28/2019,Separator,Temp Control System,Coils,,,,"NBU PI showed separator temp at 32 degrees, When I arrived on location the bath temp was 100 degrees and the separator temp was 70 so I left these alone, the glycol pumps were stroking way too fast so I cut back on the fuel gas going to them to slow them down. Looking at the graphs on Kelvin the well isn't cycling correctly because the plunger stopped making arrivals, might be hung up in cap, there is no methanol on location???? The valves for the glycol at the well head were also shut in, not allowing warm glycol to the well head.",user_22,asset_1545,46.2356189,-100.6010498
3/7/2017,Gas Scrubber,Pnumatic Dump Valve,Seat/Ball/Piston,Other,Other,Other,Fuel supply shut off to three esd's/wells down,user_131,asset_1464,47.95107457,-103.5791599
4/29/2019,Separator,Choke Valve/Loop,,,,Trash,Choke leaking profusely to atmosphere. Packing in choke was in the wrong way and no lubricated. Replaced properly and no longer leaks,user_147,asset_609,,
2/5/2018,Wellhead,Manual Valve,Ball,,,Trash,End Of Life on old KF valves,user_119,asset_285,48.1470144,-103.6180489
5/24/2018,Tanks/Pits,Piping,Load Line,,,Corrosion,4” Load line valve on Condo tank found leaking with steady drip,user_150,asset_860,,
9/12/2019,Plunger System,Plunger,Plunger,IPS,,Corrosion,Well was shut in for non arrivals rtp'd well and got a plunger arrival. Inspected and replaced bar plunger and rtp'd,user_10,asset_1069,40.5262342,-113.8824849
10/10/2017,Plunger System,Plunger,Plunger,PCS,,Not Optimized,well lost plunger arrivals and loaded up and died,user_179,asset_372,40.5960545,-113.9323891
1/30/2017,Gas Scrubber,Dump Line,Dump Line,Other,Other,Corrosion,"The fuel gas line froze off to all the scc' they have a 1"" carbon steel bare riser to each one that always freeze off ",user_131,asset_633,47.86365991,-103.5284394
3/1/2018,Tanks/Pits,Flare/Combuster,,,,,"**SCC B** WFS line freeze had well shut in. High low closed causing pumps and burners to use up all fuel gas and the location to go down. Opened high low bypass and go pressure into the unit, pinched choke to a 8/64 to allow high low to burp and allow units to stay on line in anticipation of WFS getting line freeze broke today. Lit HP unit burner #1 and HP unit #2 burner. Checked all dumps for freezes, all were clear. Checked all scrubbers across location, all were clear. Lit both sides of line heater and walked location making sure the heat trace is warm across location, all was good. Lit SCC B.",user_62,asset_1212,40.5960545,-113.9323891
2/12/2018,Separator,Choke Valve/Loop,,,,Freezing,"Thawed DVC. Had to thaw on blow down valve also. Vented well due to being loaded. Plunger arrived, RTP'd well, started cycles, and return to optimizer.",user_141,asset_220,48.1470144,-103.6180489
3/10/2018,Flare System,Flare Header,BMS,,,,"Issue: found SCC (B) down on the HMI Root Cause: found Teflon in the pilot tip Fix: cleaned out pilot tip relight and returned to service Along with the warmer weather i was able to drain all the ESD filters and blew all of them dry, Choke filters drained and blew all of them dry, drained desi, drained all three separator scrubbers and drained comp scrubbers as well ",user_136,asset_146,48.1470144,-103.6180489
12/21/2017,Compressor - Gas Lift,Compressor,Suction Controller,Compressco,,Freezing,methanol off to casing opened and vented casing breaking freeze and rtp'd compressor,user_176,asset_1707,48.1470144,-103.6180489
11/11/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Issue: Arrow Dispatch for well Deferring Root Cause: cycles are bad, well is just bumping on to repressure the unit trips the meter and shuts right back in. The well has been coded to optimization twice but nothing has changed Fix: recoded the well again and will get a hold of an optimizer to look at the cycles ",user_170,asset_694,48.1470144,-103.6180489
2/28/2017,Gas Scrubber,Other,Other,Other,Other,Other,Gas supply to T-12 on line heater was froze. Thawed and relit line heater and got heat trace going again.,user_62,asset_1522,48.224585,-103.8291059
3/20/2018,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,"Knock out pots, to flare, fuel gas to flare, line heater, and line heater scrubber had liquids. Wells flowing over 110deg carries liquids through the gas stream which drop out in these pots and scrubbers.",user_58,asset_1915,48.37289758,-103.5167781
7/27/2017,Automation,Plunger Arrival Switch,,EDI,,, 5. Five Mile 31-130 - MSO problem • Found Cyclops board burnt up • Replaced Cyclops • Found wiring issue that was created when ever the hooked up the gas lift compressor on this site • They removed all negative wires for Cyclops in the front end J-box • Corrected wiring issue • Tested and verified Cyclops now working correctly ,user_92,asset_296,40.5960545,-113.9323891
1/16/2018,Compressor,Compressor,Dump Valve,Ariel,,Freezing,"Found compressor down, comp was down on high liquid level 1st stage , found dump line froze off, found sandpiper pump stalled out, adjusted regulator and pump is working fine, got dump line opened back up an compressor started an loaded",user_122,asset_1196,48.35744013,-103.7791556
12/8/2017,Fuel Gas/Start Gas,Regulator,,,,,lost fuel gas ,user_53,asset_451,48.1602922,-103.6173872
2/13/2019,Separator,Liquid Dumps,Seat/Ball/Piston,Kimray,,Erosion,"checked location, everything looked good except for the green complete dump trims were leaking bad, all fluids were going out of water dump to pit, called TL and discussed plan of action was able to find a 2 in kimray dump trim and replace the water dump trim to keep unit running without sending condo to pit. condo dump trim in green complete will need to be replaced but production rate is enough that more condo is coming in than is leaking by trim, ",user_37,asset_796,43.56424,-91.351691
3/24/2018,Chemical System,Tank,Shell,,,Empty - Methanol,Had methanol tank refilled. ,user_141,asset_817,48.1470144,-103.6180489
8/28/2019,Flare System,Flare Header,Regulator,,,,"adjusted regulator , was low on supply psi",user_144,asset_527,40.5262342,-113.8824849
11/17/2017,Tanks/Pits,Tank Level,Sensing Cable,,,Weather,Issue: callout hi water tank alarm Root Cause: as the weather changes and it starts freezing when the equipment dumps to the tanks is causes a fog and gives a false hi tank level. Fix: alarm usually clears itself like it did. not sure what the long term fix is unless we look at another type of tank level,user_136,asset_1716,48.0614644,-104.8417043
8/25/2019,Surface Location,Well Pad,,,,Weather,Lot of weeds on location. Will write a work order to have them sprayed,user_55,asset_324,,
9/30/2017,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water,user_141,asset_2012,48.1470144,-103.6180489
10/10/2018,Site Power,External Supply,,,,,Had a power bump last night. Pump was down for approximately 4.6 hours. It only shut off the injection pump itself.,user_55,asset_2012,,
11/10/2017,Dehy,WFS Issue,,,,,Frozen in contactor tower. All BP equipment on site operational and up to temp. Dumps actuating properly. Dehy is off ,user_107,asset_1205,47.96750604,-103.4070054
4/13/2019,Pipeline/Piping,Valves,,,,End Of Design Life,"valves wouldn't hold, replaced them, ",user_77,asset_1419,46.2356189,-100.6010498
6/14/2018,Separator,Liquid Level Control,,,,,"Bad bottoms in condo tank, replaced dump trim sets, and verify no leaks",user_84,asset_1225,48.02934474,-103.5158686
2/14/2018,Compressor,Compressor (Recip),Scrubber Level,,,,"call out compressor down- went down on high 1st stg scrubber liquids, I adjusted the dump control, drained scrubbers & control valves, they had a lot of liquids in the control valves, drained the desi, rtp comp/wells, checked dumps on seps-good",user_131,asset_1346,40.7126799,-114.1193569
8/25/2017,Pumping Unit,Pumping Unit,Hall Effect,Weatherford,Model 320,Water Level,Pumps off immediately ,user_111,asset_1789,48.03612164,-103.3804393
1/8/2018,Compressor,Compressor,Process Gas Supply,Frick,,Trash,Compressor down on low discharge pressure to many wells in an off cycle at the same time ,user_172,asset_337,,
8/6/2018,Sales Valve (PV),Sales Valve,Body,Valvcon,,Washed Out,Top of cyclonic was showing closed. Valve body at 50%. Someone had it set wrong. ,user_31,asset_438,48.42236782,-103.6425499
2/11/2018,Gas Scrubber Separator,Back Pressure Valve,Top Works,Taylor,,Freezing,"Ball in scrubber was floated and froze. Thawed on scrubber, ball dropped. RTP'd well.",user_141,asset_420,48.1470144,-103.6180489
4/28/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Drained desi while on location. location runs off WFS buy back gas. No fluids present.,user_62,asset_2051,48.1470144,-103.6180489
2/10/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Supply pressure to esd was low not allowing it to open. Adjusted pressure to 100 in scrubber and 90 to esd. Rtp well,user_153,asset_333,48.20752965,-103.6138495
9/6/2018,Compressor - Gas Lift,Compressor,Valves,Ariel,,Freezing,"Compressor down on high discharge frozen in the casing close to the surface meth. is injecting , broke freeze and rtp'd compressor rpms set at 980 injecting 700 down the casing ",user_10,asset_2055,48.1470144,-103.6180489
11/4/2019,Automation,Solar Panel,Glass,BP Solar,,End Of Useful Life,"Replaced Battery box stand, battery box, 4 batteries, 2 solar panels, and fuses. Rebuilt solar panel stand and terminated wiring. Completed termination of batteries and verified that solar panels were charging batteries and that batteries were powering RTU. Verified that all end devices on wellhead were operational. ",user_44,asset_2182,46.2356189,-100.6010498
3/27/2019,Separator,Temp Control System,Pilot,,,,"pilot plugged, cleaned out and relit",user_31,asset_648,43.56424,-91.351691
6/14/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Inspect plunger, non arrivals, try a dual pad",user_84,asset_1225,48.02990352,-103.515384
11/10/2017,Compressor,Compressor,Suction Controller,Ariel,,Freezing,compressor down on low 2nd stage inter stage pressure. 125 psi. restarted compressor and put back into service. called bob with jw to see if we can lower the top governed speed from 1700 to 1650 and lower the first stage percentage load from 85% to 60%,user_11,asset_1154,48.1470144,-103.6180489
6/13/2018,Wellhead,Casing,Intermediate Casing Head Valve,,,,SHot fluid level down casing of well. Hit fluid level or hydrate at 732 feet from surface. Sent results to engineer for review.,user_62,asset_1083,48.1470144,-103.6180489
3/26/2018,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,"Knock out pots, to flare, fuel gas to flare, line heater, and line heater scrubber had liquids. Wells flowing over 110deg carries liquids through the gas stream which drop out in these pots and scrubbers. ",user_58,asset_1915,48.37143892,-103.5201341
5/29/2018,Flare System,Flare Header,Instrumentation,,,,Luman 9-pad SCC callout relit SCC 2. ,user_71,asset_226,48.1470144,-103.6180489
11/14/2018,Compressor,Compressor (Recip),Scrubber Level,,,,"Dispatched to well due to its deferment Got to location and found ESD was closed as well as the compressor was down Found compressor down on high 2nd stage scrubber level Drained compressor and restarted Allowed compressor to warm up, while compressor was warming up i drained the desi Desi was full liquids Started cycle then loaded compressor Sat with compressor and made sure it stayed online RTP'd well and compressor ",user_56,asset_1548,48.259175,-102.9017971
1/25/2017,Gas Scrubber,Shell,,Other,Other,Erosion,Na,user_156,asset_180,48.1601953,-103.6171451
12/7/2017,Gas Scrubber Separator,Dump Line,,,,Freezing,Thawed and drained desi drier ,user_62,asset_1043,48.1470144,-103.6180489
8/29/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,well lost plunger arrivals and was deferring production,user_179,asset_359,48.3619066,-103.2129855
6/5/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,"Issue: well just came back on request to check Root Cause: checked to make sure the dumps were open, and there was a good flow rate. i also performed a walk around Fix: looked good flow rate down finished opening the choke up",user_136,asset_2019,48.2594698,-102.900849
5/23/2018,Instrumentation,End Device,Moore,,,Installation Design,"Issue: called out LP unit fuel gas issue Root Cause: the only time this alarm should go off is if the liquid level drops and the float shuts off the fuel gas. but instead it calls out randomly and every time i am there the levels are about 4"" higher than the float Fix: left as is, poor callout design ",user_136,asset_1915,40.7126799,-114.1193569
1/23/2018,Compressor,Compressor (Recip),Scrubber Level,,,,"Compressor was down on HI 2nd stage scrubber level. scrubber was froze, finally got it to break free. warmed up compressor and RTP'd well ",user_53,asset_879,48.1602435,-103.6172092
1/25/2017,Wellhead,Primary Choke,Body,Other,Other,Other,no issue found,user_92,asset_1347,48.160325,-103.618612
1/21/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,I vented plunger to surface and put back on plunger cycles.,user_51,asset_1597,48.1470144,-103.6180489
7/31/2018,Compressor,Engine,Governor,Ajax,,Controller Failure,Wasn’t revving up,user_94,asset_459,,
6/12/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Vent plunger, line psi spikes, sensitive, will surface and turn over to optimizer",user_84,asset_1225,48.02986698,-103.5154825
11/14/2018,Chemical System,Piping,In-Line Check Valve,,,Freezing,"Methanol injection system/ prior tubing transmitter piping, makes a trap of produced water and freezes splitting the in line check valve causing a gas leak ",user_21,asset_1914,43.252261,-115.0567324
1/16/2018,Gas Scrubber Separator,ESD,,,,,"lost half the pad & the compressor to valve fault on wells shutting in, checked regulator psi to esd's are good-not sure what happened here-program issue?????? RTP wells and compressor-drained liquids/walkthrough",user_131,asset_1350,40.7126799,-114.1193569
12/12/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Drain Desi and fuel gas scrubber of liqiuds ,user_109,asset_774,48.3271346,-103.6569767
1/29/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,"Found separators down. Inspected PSV's/Rupture disks for missing rain caps. Found all in place. Re-pressurized units and checked the desi for possible fluid issues. All the dump valves where closed and holding After dumping a small amount of fluid I found gas moving to/from the desi and ruled it out as a possible loss of pressure. I thumbed all the dumps and verified turbine functionality, after which I checked graphs and could not coincide a stuck dump with the losses of pressure. I shut off the glycol pumps and listened for possible gas leaks on each four packs and the only gas I found moving was that of the separators into the fuel gas system. After verifying this site is losing pressure do to lack of fuel gas to keep burners and pumps supplied in between all the wells cycling, with one sacrificial well being enough to keep the site fed, I instituted the choke burping program to ensure the wells can all take the burden of keeping the site fed and online. I informed OPT to watch and make any needed adjustments/ alert me if wells start going down. Requested TL to let me know when PSSR and MOC is completed to turn on fuel gas buy back meter to help with this issue.",user_6,asset_886,36.2541889,-91.2478009
1/15/2019,Separator,Back Pressure Valve,Sensing Line,Kimray,,Freezing,"I could not find sales line any where in the dropdowns to accurately capture this surface failure, please refer to my notes instead of the dropdowns 8. Siberia 13-2 - install cyclonic actuator on valve • Installed actuator on valve • Tested and verified actuator functions on valve • Sounds like a possible sales line freeze • Gave site a shut-in command • Coded well to ops • Notified ops ",user_38,asset_869,48.1131168,-103.83464
12/6/2017,Separator,Choke Valve/Loop,,,,Freezing,Lost unit pressure.,user_48,asset_1556,48.22216875,-103.6359583
5/30/2019,Pipeline/Piping,Valves,,,,End Of Design Life,2” KF blowdown valve leaking completed work request to replace,user_18,asset_1380,,
12/13/2016,Wellhead,Primary Choke,Body,Other,Other,,The travel sensor would not pick up the position of the arm. Changed out with another arm dvc.,user_162,asset_2013,48.3619066,-103.2129855
8/27/2018,Compressor,Compressor (Recip),Lubricator,,,,"CALLOUT Got to location and found that the compressor went down on low compressor oil level. Notified TL about issue, we decided to go ahead and release compressor Vented well to unload it and surface plunger due to it flowing while the compressor was down. TBG was at 296 CSG was at 504 Vented well for 20 mins unloaded well then allowed plunger to drop Put criteria into cyclonic RTP'd well ",user_56,asset_476,48.2728096,-102.8683227
1/31/2019,Separator,Dump Line,,,,Freezing," Kalter and I walked down location and found the fuel gas to the line heater frozen with the line heater down which took down the heat trace on the location and caused all the water dumps on the location to freeze . Used thaw tube on the truck and BP heater on all above ground pipping on the water dump lines to break freezes. Water dump was frozen from the unit all the way to the check valve at the water tanks. Finally got all dumps free from the production unit to the tanks clear. Got fuel gas to the line heater thawed out and started the heat trace system. Contacted Team Leader and eng. (Avery) was instructed to flow well through one unit, watched dumps on unit to make sure they would keep up and everything looked good. Then started troubleshooting the compressor on location found the water dump frozen from the compressor to the main water dump thawed and cleared line . Tried starting compressor and discovered the batteries were dead, these looked to be new batteries for the compressor / contacted Avery about possible battery issue after finding out that they were only 2 week old batteries. Got snow removed from compressor building so that we could jump the batteries , after charging we restarted compressor and loaded set rpms to 1300/ informed Avery of the set points. Rpt'd well and compressor.",user_10,asset_1600,40.5262342,-113.8824849
2/8/2019,Heat Medium,Waste Heat Recovery,Flow Controller,,,,"Glycol system not working on site, heat trace at the compressor is not circulating and on a couple of the separators neither ",user_21,asset_676,40.5262342,-113.8824849
7/18/2019,Wellhead,Valves,,,,Corrosion (Internal),The pipe section for the upper tubing flow path had bad weldolet threads. It was replaced with different pipe fittings.,user_68,asset_611,48.1470144,-103.6180489
4/14/2019,Surface Location,Lease Road,,,,Weather, Heavy equipment working on the big hill road didn't have the road construction sign to warn people about the equipment working and the trucks dumping gravel on the road. Talked to the equipment operators and they install sign on the road.,user_21,asset_92,48.1509653,-103.6204411
9/23/2019,Instrumentation,End Device,Moore,,,End Of Useful Life,"Installed new temp transmitter, tested and verified",user_44,asset_1462,46.2356189,-100.6010498
3/5/2018,Tanks/Pits,Flare/Combuster,,,,,"Lit SCC C. While on location, noticed SCC's were not lit. Pilot light on all 4 SCC's were out. Shut down all SCC's to let them purge, lit pilots and put them back in service. Cannot Identify root cause as to why they were out, i did not have to thaw or repair any thing to get them on.",user_62,asset_998,40.5960545,-113.9323891
2/12/2019,Automation,Cable,Coax,3M,,Electrical Short,Wyolectric replaced the heat trace section here that had failed. It goes underground and heat trace is not supposed to be buried. This may have been the cause of the heat trace failure.,user_108,asset_101,,
12/8/2018,Separator,Temp Control System,Heater/Burner,,,,"Dumps and sales line where froze. Because fuel gas to line heater froze off. Unit was flooded and ball checked. Drain unit. Broke dumps. Lit bath. Broke sales line freeze. Broke dump freeze on heater treater. Glycol pumps are running. All burners lit and running. Broke freeze at scc pilot fuel gas. Left compressor down,its still froze. Moved heater put it on dumps on heater treater",user_120,asset_1754,48.3715001,-103.5207258
4/12/2018,Plunger System,Plunger,Plunger,IPS,,No Liquid,Mon 19-130 had missed 2 plunger cycles and was going to miss another so I helped plunger in. RTP and started cycles ,user_71,asset_1992,48.1470144,-103.6180489
9/2/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ajax,,Trash,"comps down on low suction pressure, RTP",user_37,asset_2138,43.56424,-91.351691
4/21/2017,Gas Scrubber,Other,,Other,Other,Other,thawed choke,user_62,asset_48,48.1470144,-103.6180489
7/7/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Dispatched to well to check and rtp, found , plunger non arrival , casing psi 895 psi , tubing 401, loaded, will vent plunger and rtp, ",user_84,asset_2276,47.969923,-103.5231354
3/29/2018,Instrumentation,Controller,,,,,"Broken gauges on esd’s preventing pressure reads. Ordered parts, will replace when parts arrive",user_35,asset_1812,48.19881589,-103.4822992
10/1/2018,Fuel Gas/Start Gas,Regulator,,,,,"Satellite well, with a line heater in between well head and location. Multiple freeze points at the line heater where the hi\lo valve is at. All of the needle valves between the well head and the unit are seized and I cannot get depressurized. Shut well head in over night. Tomorrow if not broken I will need to put a jumper on from Williams and get pressure to the unit to get the line heater warmed up and the glycol pumps running. I did not have the supplies needed this afternoon. Will be the first stop in the morning. When the line is clear all needle valves wll need to be replaced. We need to look at removing the hi\low form the line heater, its not needed and is an added freeze point. This was an issue before and its a hard freeze to break at the line heater. ",user_106,asset_814,48.2630953,-102.9002853
1/18/2018,Separator,Temp Control System,Heater/Burner,,,,Bath A burner was out. Unable to establish root cause. Relit and returned to service. ,user_50,asset_364,48.33569362,-103.5983037
1/8/2017,Heater Treater,Mechanical Dump Valve,,,,,"Water dump line was frozen, piping thread started leaking probably due to the expansion of the frozen pipe.Thawed the frozen pipe, depressurized, removed, repaired and returned to service",user_60,asset_1276,48.31925327,-103.5578717
1/1/2018,Fuel Gas/Start Gas,Regulator,,,,,"Fluid getting into dbc and freezing system. Blew out best I could, will drain daily to see if issue resolves. Turned down bath 10 degrees as well.",user_35,asset_2142,48.18252893,-103.5378205
12/3/2016,Compressor,Compressor,,,Other,Freezing,Dump line continuously freezing,user_107,asset_1812,48.1991028,-103.4824184
12/11/2017,Compressor,Compressor,Suction Controller,Ajax,,Freezing,"Root cause undetermined due to lack of automation. No compressor pressures read into automation systems. Separator unit pressures did not indicate the low suction condition called by controller. Suspected freeze to be route cause. Dispatch to location. Find a low suction code on compressor panel. Pull graphs to determine cause. Condition cannot be pin pointed in graphs. Lack of automated pressures from suction to discharge limit the amount of troubleshooting that can be conducted. Unit pressures on vessels inputting compressor do not show signs of a low suction pressure condition. Possible freeze in suction at controller. Suction pressure was 80 psi upon arrival. Shut suction, open bypass and blowdown compressor. Some hydrates release while blowing down. May confirm freeze. Start compressor and warm. Bring up rpms and load compressor with on skid recycle open to warm stages. Off skid recycle functioning. Load compressor and hand wells to optimizer so I could travel to another site. Before leaving line up 70 to sales bypassing compressor. Optimizer adjusted criteria and kicked well to sales line pressure of 240 psi. Fluid arrived successfully. Flow for clean up. Dispatch back to location to drop bypass plunger. Drop used PCS Six Shooter Bypass. 1.89 top, middle, bottom. Plunger makes first arrival. Optimizer to continue to monitor cycles. Check scrubbers, desi, and other pots. Fluid level at compressor below dumps, minimal fluid in desi, no fluid in kimray pots and separator scrubbers. Ambient air temperature 30 degrees. Bath at 95 degrees. ",user_75,asset_638,,
7/31/2019,Compressor,Compressor (Recip),Valves,,,,"Arrived on location and did walk down of compressor. Got permission to remove tags, compressor had been shut down for test. Removed all tags and aligned valves to allow wells to flow into compressor. Arch rock arrived on location and checked all the things on the compressor that they needed to. Started compressor with out issue and loaded. All wells flowing into the compressor. Optimizer to watch wells and adjust cycles as needed with lower flowing pressures. ",user_15,asset_1735,46.2356189,-100.6010498
6/12/2017,Plunger System,Plunger,Plunger,Well Master,,No Liquid,due to the high line pressure over the weekend the plunger and well logged off. i vented plunger and restarted cycles.,user_11,asset_1275,,
1/25/2019,Heater Treater,Back Pressure Valve,Sensing Line,Kimray,,Freezing,"arrow dispatch.plowed location with plow truck and set two bp heaters on separators the day before.location has been down for several day.looks like we had originally lost location due to frozen fuel gas.this has happened multiple times. we need to move the big joe's closer to the fuel gas separator,or heat trace the fuel gas up to the big joe. takes a large pressure cut inside the the high pressure unit, the fuel gas line is slopped so any fluids in that line fall back don to the big joe and eventually freeze off.there was a free in the fowline that we blew down to the pit.high low was frozen thawed it out. thawed out fuel gas from high pressure to fuel gas sep.started glycol pumps and burner on fuel gas sep.dumpline from hp to lp was froze thawed that out. back pressure on lp was froze and so was water dump on lp right outside the cabinet. william dehys are both froze.contacted williams and ended up bypassing both dehys and are flowing through meter run building.sales line was froze from check valve to williams choke. thawed that out. williams blew there dehy down to tub and over ran tub. they aso blew there lateral from cap.which made a mess on location.spoke with dehy tech and reported this spill to team lead.after we got everything free we started selling. well loaded up and ihad to vent to the pit for over an hour.got well unloaded and put back to sales.equipment looks good but will need checked on to make sure lines and scrubbers stay dry and clear. thawed out pilot fuel gas to flare.thawed drain on ko pot at flare and relit flare",user_120,asset_580,46.2356189,-100.6010498
3/13/2018,Compressor,Engine (Gas),,,,,"Compressor was shut of for production test, Engineering team requested that the compressor be re-started. Arrived on location and found compressor off, inlet shut and tagged and batteries shut off. walked through all piping and made sure all valves were in proper order to start and run compressor. Started and warmed compressor, loaded compressor and am watching wells to see if any need unloaded to tanks.",user_62,asset_1413,48.1470144,-103.6180489
6/12/2018,Compressor,Compressor,Suction Controller,Sullair,,Trash,Compressor down on low suction pressure due to well shutting in on consecutive non arrivals I went to location worked on well then cleared alarm and restarted compressor.,user_51,asset_1774,48.1470144,-103.6180489
7/8/2018,Gas Scrubber Separator,ESD,,,,,"CALLOUT MC 3-pad down on low unit pressure. saved twice. Went back down wasn’t able to save, late call didn’t make it to location. ",user_37,asset_2148,43.252261,-115.0567324
4/29/2019,Instrumentation,End Device,RTD,,,Calibration Issue,Injection pump down.,user_94,asset_523,48.1051218,-104.8967462
1/31/2018,Compressor,Compressor (Recip),Bearings,,,,"this well also goes to the D-1 compressor wich is down to a bad bearing, I opend the bypass valve to sell gas while Arch Rock is working on it",user_84,asset_1509,48.1470144,-103.6180489
11/2/2018,Chemical System,Pump,Valves,Texam,HBC1,Debris,meth pump is bad need sreplaced,user_37,asset_1500,48.1497991,-103.6211501
9/17/2017,Compressor - Gas Lift,Engine,Vibration Switch,Caterpillar,,Freezing,"We have freezing going on in cooler. When I initially blow down compressor, have a quick hit of pressure followed by some fluids. Closed the louvers some more. ",user_141,asset_1350,48.3619066,-103.2129855
2/15/2018,Heat Medium,Pump,Diaphragm Gears,Sunpumper,HBT1,Wear,This was a GRACO pump nothing to pick from in list. Please fix ,user_119,asset_285,48.1604365,-103.6185235
4/1/2019,Pipeline/Piping,Valves,,,,Corrosion (Internal),"replace 1"" ball valve",user_157,asset_206,46.2356189,-100.6010498
10/17/2019,Instrumentation,Meter,Orifice Plate,Bristol,Wonder Card RS232,Passed Function Test,Found Issues with Wonder Card: Reset WFS Bristol Meter and Tested thru SAMS Systems,user_139,asset_2006,,
12/8/2017,Dehy,WFS Issue,,,,,Dehi is froze up.,user_0,asset_1163,48.2522019,-102.7574075
4/12/2018,Plunger System,Plunger,Plunger,IPS,,No Liquid,"Champ 452 C-70 had missed 2 plunger cycles vented plunger in, in 30 min. RTP and started cycles.",user_71,asset_1525,48.1470144,-103.6180489
8/26/2019,Chemical System,Pump,Strainer,Texsteam,HBC1,Debris,Couldn't get fuel gas past regualtor on side of the pump. So I STJ and contacted TL and he advised to clean the screen on side of the regualtor. After cleaning methanol pump functioned correctly ,user_145,asset_397,48.1078401,-103.6218456
12/28/2017,Separator,Liquid Dumps,Controller,Norriseal,,Improper Adjustment,call out well shut in-lost unit psi-found astuck condo dump improper adjustment-adjusted/rtp/boc,user_131,asset_577,40.7126799,-114.1193569
12/13/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,"the main drop pot for the B 4-pack was froze, turned on heat trace going to well head which will heat this area and should fix the problem",user_176,asset_1428,48.1470144,-103.6180489
4/3/2019,Heat Medium,Pump,Instrumentation,Texam,HBC1,Air Locked,Found Water Damaged to Batteries and Solar Controller; Snow Melting caused water to enter battery box. Tag out the Solar Glycol System.,user_139,asset_1742,,
1/26/2019,Separator,Choke Valve/Loop,,,,Freezing,"checked tanks no high tanks found, unit was froze in horseshoe thaw tubed cleared intefrlocks and RTP. all tank valves were shut for unknown reason open end condo tank all crossovers open,",user_37,asset_2274,43.56424,-91.351691
4/13/2018,Separator,Temp Control System,Heater/Burner,,,,Burner blew out on fuel gas separator. Pilot line and main are both clear and dry. Relit burner. Adjusted eclipse(fuel/air mixture),user_172,asset_1513,,
11/27/2018,Tanks/Pits,Flare/Combuster,,,,,"A scc out, probably due to high wind, relit",user_31,asset_1686,43.252261,-115.0567324
12/14/2017,Gas Scrubber Separator,ESD,,,,,"well went down on valve fault-ESD shut & wouldn't open remotely, need to troubleshoot-found the scrubber full of liquids, had to drain, and drained fuel filters, tried to drain desi-found the ht trace not lined up drain was froze, got the globe valve lined up and ht trace circulating to desi now, adjusted regs to ESD",user_131,asset_220,40.7126799,-114.1193569
9/6/2017,Compressor - Gas Lift,Engine,Emissions Control,Cummins,,Controller Failure,"02 sensor went out on the catalitic on the exaust, was bad and archrock replaced and returned the gas lift compressor back online this brought wells 10 and 20 back on",user_176,asset_551,48.3619066,-103.2129855
11/21/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Checked all scrubber pots and desi can. Find minimal fluid in desi can. Cause of fluid in desi can appears to be temperature drop out and not liquid carry over. Gas temps in spec. ,user_75,asset_2191,,
11/12/2017,Tanks/Pits,Flare/Combuster,,,,,Both A&B scc out. Went out because of a valve misalignment on esd. Got interlocks to clear and relit both scc ,user_172,asset_486,,
3/8/2018,Separator,Choke Valve/Loop,,,,Freezing,thawed hi low and relight burner. returned well back to service,user_11,asset_1819,40.7126799,-114.1193569
9/17/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,CALLOUT Gas lift compressor has been down since 14SEP18 Called out to restart compressor Found gas lift compressor down on low suction Root cause looks like a WFS issue. Restarted the compressor and got it going. RTP'd ,user_56,asset_1112,48.2651756,-102.8785229
11/18/2018,Automation,RTU,Display,Emerson,Model 700,Electrical Short,Unit transmitter showing sensor fail,user_31,asset_1247,43.252261,-115.0567324
3/19/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,"Vented plunger in and inspected. Found plunger to be : 1.897 top, 1.894 middle and 1.895 bottom. Plunger is within specc and was re-dropped. OPT made adjustments for the high line PSI spike that loaded the well up. OPS coding to OPT for further monitoring, OPS reset plunger cycles.",user_6,asset_461,36.2541889,-91.2478009
2/11/2019,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,"Sep. had heater on it so getting gas on and burners lit was no problem. both dump lines froze attempted to thaw no success, will De-pressure sep. tag FMC valve in front of unit and sales valve hopefully should be able to get gas on when steamer can get to location. Root cause, lost fuel gas to burners causing dump lines to freeze off.",user_63,asset_1600,,
4/9/2018,Tanks/Pits,Tank Level,Probe,,,Calibration Issue,Issue: pad called out shut in on hi tank alarm Root Cause: false alarm LSH switch is going in and out and wont let me clear the alarm and stay cleared Fix: wrote a work order to have automation look at the switch ,user_136,asset_271,48.1470144,-103.6180489
5/23/2019,Compressor - Gas Lift,Compressor,Valves,Compressco,,Trash,"arrived onsite and found gas lift compressor down on high discharge. panel is also flashing multiple alarms for PM. contacted JW and he said that they were just reminders for the jw tech.the discharge was froze across the d4 injection valve out at the wellhead. someone changed criteria in this valve and it was pinching valve down to 16% open. i removed the criteria. please leave d4 completely OPEN.this compressor runs a lot more efficiently when we leave d4 open and control injection rates with rpm from compressor. compressor is running in manual at 1250 rpm. currently injecting around 700.found glycol pumps and line heater burner shut off with no tags as to why. currently 28 degrees outside so i lit the line heater and started stroking pumps glycol level is good. checked interface on heater treaters everything seemed to be working good. we are no longer dumping to pit, the line to pit has been removed",user_120,asset_2046,40.5262342,-113.8824849
9/12/2018,Separator,Back Pressure Valve,Seat/Ball/Piston,Kimray,,Trash,"2"" Invalco Hi Lo packing leak",user_5,asset_1906,48.1470144,-103.6180489
3/7/2019,Pipeline/Piping,Pipe/Components,,,,Erosion Corrosion (Internal),well and separator shut in for washed out water dump. will need repaired prior to rtp. wear and debris appear to be underlying cause of piping fail,user_17,asset_581,,
11/21/2018,Wellhead,Cyclonic Valve,Actuator,,,Freezing,Cyclonic actuator gears were stripped. Possibly due to frozen valve. Replaced.,user_108,asset_683,,
3/24/2019,Heater Treater,Mechanical Dump Valve,Seat/Ball/Piston,Kimray,,Corrosion,"graphed tanks on emerson and noticed tank levels had not moved overnight. contacted team lead with this matter and he sent me to troubleshoot sight. arrived on location and checked green complete unit. both dumps were functioning and maintaining liquid level.went over to heater treater, found treater completely empty.leak tested condo dump on LP,condo is holding.leak tested water dump and it definitely failed. this leaking dump caused the LP to loose interface/fluid. shut water dump to start building a liquid level in LP and contacted TL.TL brought a new valve out for me to replace. got approval on single block assessment .isolated and bleed down water line. took apart 2in mechanical dump. found sand and some material i cant explain what it is.took pictures of valve and inside lines.replaced leaking valve with new valve on 2/24/19.leak and function tested valve.no leaks found. was unable to properly set kimray due to the lack of fluids that are in the LP.this valve with need set during RTP. contacted TL on another issue found. he asked me to shut in and blow down equipment. wellhead valves are all shut and tagged. shut choke on manifold,capped esd. blew down GC and flowline using blowdown on sand can.well is currently waiting on vendor,please contact TL before RTP>",user_120,asset_796,40.5262342,-113.8824849
3/29/2018,Fuel Gas/Start Gas,Coalescer/Filter,Mist Pad,,,,Fuel gas scrubber had liquid in it. Blew liquid for 5 seconds and then blew dry,user_107,asset_396,,
8/6/2018,Compressor,Compressor (Intergral),Process Gas Supply,,,,"CL 32-45 went to check VRU, battery was dead tried to jump start but comp wouldn’t start, left down.",user_37,asset_130,48.3619066,-103.2129855
9/21/2019,Separator,Dump Line,,,,Corrosion,Replaced bad check and returned to service,user_21,asset_1109,46.2356189,-100.6010498
4/30/2018,Tanks/Pits,Tank Level,Sonar,,,Calibration Issue,High condensate tank alarm 761249w 8ft 9in x 8ft 1in 761250w 8ft 6in x 8ft 5in 761249c 3ft 8in x 0ft 2in 761248c 2ft 2in x 0ft 1in FALSE ALARM Left as is.,user_51,asset_1809,47.9418861,-103.6976002
1/27/2019,Automation,Radio,,Cambium,,End Of Useful Life,Cambium PMP-100 failed. ,user_12,asset_2051,40.5262342,-113.8824849
5/14/2017,SWD System,Particle Filter,Element,,,,"Replaced filters due to low suction on pump, and to assure they run through the night.",user_141,asset_1918,48.1003142,-103.585106
5/29/2019,Separator,Dump Line,,,,Corrosion,"Well was shut in and tagged out stating that the oil dump trim needed replaced. I changed out trim and seat, installed new packing. Left well shut in per team leads request due to TAR. Removed old tags and installed new tags.",user_120,asset_826,,
8/28/2019,Separator,Liquid Dumps,Seat/Ball/Piston,Kimray,,Erosion,Found dump leaking. Replaced with new seat and stem,user_153,asset_1163,48.1433992,-103.4873496
3/23/2019,Heat Medium,Pump,Housing,Texsteam,375,Power Supply, +SOLAR GLYCHOL PUMPS NOT WORKING,user_34,asset_1252,43.56424,-91.351691
3/20/2017,Instrumentation,Transmitter,3n1 MVT,Other,Other,Recalibrated,,user_113,asset_794,48.22020671,-103.5961736
2/13/2018,Compressor,Compressor (Screw),Panel,,,,"compressor threw the belts, had to replace",user_84,asset_1466,48.1470144,-103.6180489
12/21/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,"Compressor sucked unit pressure down below operating pressure for ESD I got it linked up with ""B"" unit so I could get fuel gas to get ESD to open and RTP well.",user_0,asset_51,48.2522455,-102.7573824
11/15/2018,Compressor - Gas Lift,Engine,Water Pump,Waukesha,,Weather,"Arrived on location and found compressor down on low suction pressure. Did walk around of compressor and found turbo had oil on it. Unsure if this was some thing thaw was left from recent maintenance or if it was fresh. Started compressor and loaded it. Compressor went down in around 2 minutes on low suction again. Checked HMI and found that the off time set point for the 3 gas lift wells had been changed from .5 minutes to 78 minutes This caused the compressor to not have suction pressure to keep running. Adjusted the off time set points on all 3 wells (60, 70 and 80) back down to .5 minutes. All 3 wells have pace maker plungers and require minimal off time. Started and loaded compressor again, ran for about 15 minutes and went back down. Checked codes and found it went down on high engine jacked water temperature. Set point is 220. Called JW and told them what was going on, he asked me to start the unit and make sure of the following . 1- Coolant level was not low, 2- Suction pressure was set for 150 and 3-engine RPMs are set for 1550. I started and loaded the compressor making sure all 3 things he asked me to do were good, all were good. Compressor runs for about 10-15 minutes then goes down on high engine jacket water temperature. Called JW again and asked them to come to location and look over the unit. ",user_15,asset_1284,43.252261,-115.0567324
10/27/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Corrosion,Choke showed signs of wear,user_112,asset_1561,47.90820617,-103.6735421
7/11/2019,Surface Location,Berm,Dirt,,,Wildlife/Livestock,Hole in front of unit in walk path filled in. ,user_153,asset_853,48.0765041,-103.5213433
10/16/2018,Gas Scrubber Separator,Water Meter,Body,,,Freezing,"scrubber full of liquid, drained",user_31,asset_921,43.252261,-115.0567324
11/15/2016,Gas Scrubber,Mechanical Dump Valve,Seat/Ball/Piston,Other,Other,Erosion,Leaks through,user_105,asset_199,48.14248375,-103.4809162
2/24/2018,Tanks/Pits,Tank Level,Sensing Cable,,,Weather,Issue: found tank # 2 showing a live read of 16' Root Cause: Human Error/ Dispatch Fix: gauged tank got the cut and turned in for a bottom pull,user_136,asset_476,48.2594705,-102.9010554
1/13/2019,Heat Medium,Furnace,Process Indicator,,,,"glycol temp at 48 degrees on 4 pack and 38 degrees on T pack, opened esd valve and relit pilot and main burner on T pack",user_31,asset_886,43.56424,-91.351691
6/9/2019,Instrumentation,Transmitter,Unit Pressure,Rosemount,3051,Water,Transmitter lid was left cross-threaded and barely engaged. Water corroded/damaged transmitter electronics.,user_12,asset_252,40.5262342,-113.8824849
3/15/2018,Separator,Liquid Dumps,Controller,Norriseal,,Liquid,"Sales line had freeze, adjusted dumps",user_86,asset_989,,
12/12/2017,Tanks/Pits,Flare/Combuster,,,,,Lit scc,user_86,asset_1182,,
2/20/2019,Separator,Temp Control System,Heater/Burner,,,,#40 shut in on valve misalignment and bath was down on C I went to location and got bath going again I found the water dump line was frozen for the tpac well I left well in idle with the ESD shut until dump line broke it was froze underground but the burner is going so it should be good before too long.,user_159,asset_1103,43.56424,-91.351691
12/12/2016,Gas Scrubber,Dump Line,,,,,Desplacers frozen letting well run a cycle to get some liquid in unit,user_152,asset_245,,
9/17/2019,Sales Valve (PV),Sales Valve,Body,Valvcon,,End Of Useful Life,The salesline cyclonic valve was leaking to atmosphere and it was replaced with a new valve.,user_68,asset_1259,48.1470144,-103.6180489
5/13/2019,Wellhead,Plunger,Plunger,IPS,,No Liquid,Plunger did not come in to inspect shut in for pressure build to try to get it done tomorrow,user_146,asset_564,48.1821475,-103.6140549
7/14/2018,Separator,Choke Valve/Loop,,,,Corrosion,"Was dispatched to location to trouble shoot plunger non arrivals. Pulled graphs and saw tubing was tracking with unit pressure. Went to check choke and found it was hand open a few turns not allowing well to build pressure to get plunger arrivals. Shut choke and negative tested it, it tested bad. Not leaking a lot but probably enough to cause well to load. Wrote WM to have choke replaced. Root cause is human error, some one opened the choke by hand for some reason. Pumps and burners are not running so there is no reason to have a well in free flow. ",user_62,asset_1404,43.252261,-115.0567324
8/12/2019,Plunger System,Plunger,Plunger,Well Master,,Corrosion,Changed plunger and inspected lubricator.,user_153,asset_1599,48.2022644,-103.598788
3/25/2018,Gas Scrubber Separator,ESD,,,,,Issue: well called out shut in alarm Root Cause: shut in for the low low bath level. Fix: once i adjusted the level i was able to bring the well back on and return to service ,user_136,asset_396,48.1470144,-103.6180489
10/14/2018,Separator,Temp Control System,Pilot,,,,"pilot plugged with rust, cleaned out and lit",user_31,asset_1534,43.252261,-115.0567324
8/19/2019,Automation,Tank Level,Sensing Cable,,,Calibration Issue,"well was shut in and interlocked on high tank. Gauged all tanks and found nothing high, reset shut in and brought well back on line. Free flowing for a while to take pressure off and will put back in cycles and code to optimization. Tank live reads do not work, this location has high tanked several times and this pad continually trips the interlock on high false tanks",user_106,asset_863,40.5262342,-113.8824849
1/9/2018,Compressor,Cooler,,,,,"Compressor went down on high discharge, broke cooler freeze and RTP'd well ",user_53,asset_1744,40.7126799,-114.1193569
12/11/2017,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Desi has lots of liquid. Took several minutes to drain,user_156,asset_635,48.16963077,-103.6580608
2/20/2019,Separator,Manual Drain Valves,Body,,,Freezing,Blow line froze,user_94,asset_1353,40.5262342,-113.8824849
5/24/2019,Pipeline/Piping,Pipe/Components,,,,hydrate,"under ground hydrate cause a rupture in pipe for the 3"" sales line and on 1"" water dump from desy. both lines got re-routed",user_28,asset_197,36.2527392,-91.2689312
1/14/2019,Separator,Dump Line,,,,Freezing,"Check to make sure all dumps open and drained scrubber. Dump lines frozen, thawed on them and got both condo and water open to tanks. Drained scrubbers and fuel pots. RTP'd well",user_55,asset_1655,,
9/10/2019,Pumping Unit,Wellhead,Integrity Failure,,,,No fluid was found in the environmental containment pot on the stuffing box. Packing appears to be holding. ,user_66,asset_1823,,
12/28/2016,Gas Scrubber,Shell,,,,,Wellhead heat trace pump failed causing possible freezes in the flowline. Task request has been submitted. ,user_41,asset_60,48.20667631,-103.5352415
10/12/2017,Tanks/Pits,Valving/Swedges,Seat/Ball/Piston,,,Corrosion,Changed out 3 4' baylon valves and removed load lines on condo tanks,user_173,asset_638,40.5262342,-113.8824849
8/17/2017,Wellhead,Manual Valve,Stem/Seat,,,End Of Useful Life,"2"" KF ball valves on the upper and middle tubing flow path are leaking through stem area to the atmosphere",user_163,asset_58,48.20188609,-103.791791
12/21/2017,Compressor,Cooler,,,,,"Compressor went down on high discharge pressure, found it to be froze in cooler. Checked blue board insulation, it is good, no gaps. 2nd and 3rd stage is covered and louvers are closed. I cannot find the root cause as to why this keeps freezing. Contacted engineering with the issue, they are working on a solution. They recommended to keep trying to run the compressor as we can.",user_62,asset_1676,48.1470144,-103.6180489
11/26/2018,Heat Medium,Furnace,Process Indicator,,,,"glycol temp was at 70 degrees, not going to get much heat transfer, increased temp",user_31,asset_1995,3.9380804,137.7967699
4/4/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Drained desi while on location getting fluids shots and inspecting buy back meter piping. No fluids present, desi was dry. Location runs off of WFS buy back gas, temp at meter 54 degrees, desi dryer temp 42 degrees ambient temp 38. ",user_62,asset_1661,48.1470144,-103.6180489
6/4/2018,Tanks/Pits,Liquid Level Control,,,,,"Pad shut in on false high tank, went to location visually checked all tanks found tanks in good shape. Reset alarm and rtp’d pad. ",user_58,asset_2046,48.37141687,-103.5204387
12/8/2017,Gas Scrubber Separator,ESD,,,,,"pad went down on low unit pressure in between cycles, jumped back on and restarted cycles",user_71,asset_661,48.1470144,-103.6180489
4/25/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash,Issue: well still on a pinched choke from bringing it back on Root Cause: was trying to not over run the dumps Fix: pressure down and flow temps are up finished opening the choke ,user_136,asset_847,48.2595694,-102.9009394
3/30/2019,Separator,Temp Control System,Pilot Valve,,,,"actuator on burner supply valve will not actuate, unknown cause. may be due to wear and use or fluid getting in system. automation dispatched to troubleshoot and repair",user_17,asset_359,,
4/12/2018,Separator,Choke Valve/Loop,,,,Freezing,Well lost unit pressure. Freeze in choke. Broke freeze and RTP'd well,user_141,asset_2240,48.1470144,-103.6180489
10/27/2017,Separator,ESD Valve,Gas Supply Line,,,Fouling,"Found low fuel gas pressure. Adjusted big joe, and ESD is working properly",user_141,asset_1570,48.1470144,-103.6180489
8/30/2019,Separator,ESD Valve,Gas Supply Line,,,Trash,"block and bleed dirty from door being left off, cleaned and blew out supply",user_64,asset_935,40.5262342,-113.8824849
4/25/2018,Pipeline/Piping,Valves,,,,Corrosion (Internal),Ball seized up,user_173,asset_665,48.1470144,-103.6180489
3/29/2018,Tanks/Pits,Valving/Swedges,Body,,,Corrosion,Opened all condo tanks on location to operate battery as facility to maximize condo capacity onsite and align with predictive dispatch tools. ,user_62,asset_1826,48.1470144,-103.6180489
2/8/2017,Chemical System,Piping,In-line check valve,Other,Other,Other,Leaking around gasket,user_166,asset_743,47.88128081,-103.5971929
11/17/2017,Tanks/Pits,Tank Level,Sensing Cable,,,Calibration Issue,"Issue: pad keep shutting in on a hi water # 2 tank alarm. Root Cause: the tank level has been taken out of service to keep the pad from triggering an alarm off that tank but it still going into alarm and shutting the pad in with a level of 9' 10"" Fix: I am starting to think it may be more of a programming issue rather than a device issue",user_136,asset_2247,48.1470144,-103.6180489
3/21/2017,Chemical System,Pump,,Other,Other,Other,,user_119,asset_1220,48.3619066,-103.2129855
12/16/2017,Heater Treater,Burner,BMS,,,Pilot Went Out,"call out pilot out on line heater, went and relit",user_131,asset_2000,40.7126799,-114.1193569
1/25/2018,Fuel Gas/Start Gas,Regulator,,,,,", the supply to reg was froze, this pad sits in the middle of the wind tunnel freezes faster than you can thaw it out , thawed out & rtp/boc",user_131,asset_1536,40.7126799,-114.1193569
4/25/2018,Tanks/Pits,Liquid Level Control,,,,,Issue: found water tanks at 15' on the HMI Root Cause: Human Error/Dispatch must have missed it Fix: called IBEX and they sent a truck to start pulling it ,user_136,asset_601,48.2595694,-102.9009394
3/26/2018,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,"Knock out pots, to flare, fuel gas to flare, line heater, and line heater scrubber had liquids. Wells flowing over 110deg carries liquids through the gas stream which drop out in these pots and scrubbers. ",user_58,asset_1823,48.41599506,-103.5767569
3/16/2018,Separator,Temp Control System,Fuel Gas Supply,,,,"Upon arrival to location, did a location walk through. Saw the manual ball valve to the Kimray 3 way divert valve gas supply was closed with no tag. Opened valve. Root cause is human error. This is a new system and people do not see to understand how it works and valve configuration. Contacted team leader with what was found, I will be doing a training with Sector 3 team on proper set up, valve position and adjustment of the system. ",user_62,asset_1782,48.1470144,-103.6180489
7/1/2019,Separator Inlet Valve (XV),Valves,,,,End Of Design Life,The Hi/Lo was leaking out both weep holes. It was replaced with a complete assembly.,user_68,asset_58,48.1470144,-103.6180489
12/19/2017,Separator,Fuel Supply System,"Moisture, Regulators",,,,Bath heater solenoid would not shut . Went to location and thawed on solenoid and got valve to close restarted bath .,user_100,asset_2053,48.1470144,-103.6180489
9/8/2017,Pipeline/Piping,Valves,,,,End Of Design Life,"Packing leak found on 2"" KF valve on flow line by separator",user_150,asset_756,,
1/17/2017,Wellhead,Primary Choke,,,,,"DVC wasn't controlling, thawed it out, drained all the liquid out and got it working ",user_74,asset_1193,47.94938139,-103.3853109
6/2/2018,Compressor,Compressor,Process Gas Supply,Quincy,,Trash,compressor down again. not getting sufficient supply from LP units,user_172,asset_876,48.1470144,-103.6180489
6/11/2019,Separator,ESD Valve,Gas Supply Line,,,Fouling,"block and bleed was plugged, replaced",user_31,asset_316,43.56424,-91.351691
11/4/2016,,,,Other,,Other,Snap pilot kit diaphragm leaking.,user_130,asset_2111,47.99034312,-103.6048371
9/27/2019,Tanks/Pits,Valving/Swedges,Body,,,Corrosion,Valve needs replaced excessive corrosion. Cannot replace bull blug.,user_98,asset_162,46.2356189,-100.6010498
5/16/2017,Automation,Plunger Arrival Switch,Other,Other,Other,Other,none,user_74,asset_1412,48.1470144,-103.6180489
3/12/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Brought up ,user_86,asset_788,,
10/25/2019,Gas Scrubber Separator,Dump Line,,,,Trash,Dump scrubbers Desi 13 seconds scrubbers in unit 3 seconds,user_128,asset_1927,48.1718013,-103.5950243
1/20/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Vented well due to being loaded. Plunger arrived, RTP'd well, started cycles, and return to optimizer. Work done by Julio",user_141,asset_1264,48.1470144,-103.6180489
2/24/2019,Heat Medium,Pump,Process Indicator,Sunpumper,HBC1,Power Supply,"solar glycol pump to 30,90,150 wells had tripped out. Overload, lowered HZ from 4.0 to 3.5, reset and started",user_31,asset_521,48.257296,-102.8614304
4/29/2018,Wellhead,ESD Valve,Actuator,,,Liquid Plugging,Asco solenoid vavle failed due to plugging,user_134,asset_1759,48.1470144,-103.6180489
3/5/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Drained desi while on location working on well 50, 80 and 150. Took 30 seconds for fluid to drain.",user_62,asset_425,40.5960545,-113.9323891
10/7/2018,Fuel Gas/Start Gas,Regulator,,,,,Issue: found well down (INT) valve fault Root Cause: found the burner was out bath was 49deg and the big joe was freezing off Fix: relight the bath and once warmed up was able to get the well back on,user_170,asset_1442,43.56424,-91.351691
1/16/2019,Separator,Dump Line,,,,Freezing,"Thawed on dump lines outside of separator, managed to break condo dump line freeze but found that freeze pushed into Inlet of 761495 condo tank. Did not have long enough thaw tube to thaw Inlet of tank. Spoke with team lead to verify it was OK to swap into 761494 condo tank and was given approval. Swapped tanks and checked all condo dumps and verified they were clear and would push all the way through to the tank. Also found discharge valve on glycol pump going to tanks shut and therefore pump was not going. Opened discharge valve and verified glycol pump started, checked at tanks to verify glycol loop was getting warm. ",user_44,asset_825,,
3/5/2018,Fuel Gas/Start Gas,Regulator,,,,,Unit fuel gas froze ,user_111,asset_1160,48.06773109,-103.3833206
10/27/2019,Compressor - Gas Lift,Compressor,Suction Controller,Compressco,,Freezing,"suction controller froze, getting alot of liquids back from WFS, buy back, got compressor up, then interstage 1 then 2 froze, then compressor oil psi was to low, called randy with arch rock, finally got compressor running on its own, had alot of trouble with this compressor, found leak on water tank valve, got it repaired, heater is still running on this compressor, ",user_77,asset_387,40.5262342,-113.8824849
12/20/2017,Flare System,Flare Header,BMS,,,,Issue: found SCC down on the HMI Root Cause: pilot out Fix: relight remotely,user_136,asset_1585,48.0614644,-104.8417043
2/22/2018,Separator,Temp Control System,Heater/Burner,,,,Line heater at satellite wellhead had the burner out due to high wind and blowing snowing. Relit and returned to service. ,user_50,asset_38,48.33981664,-103.6364684
10/2/2019,Flare System,Flare Header,Regulator,,,,"Pad went down on low unit pressure,this well will need a downstream valve installed to keep the pad up when running the glycol baths and pumps running. Work order was already turned in but i wrote another work order for the downstream valve. Pressured up units and functioned tested chokes and rtp'd. found that the choke on the 40 well was not responding, removed and cleaned I/P and put well back into service and function tested. Restarted all scc's and baths on location did not start pumps because of fuel gas issue.",user_10,asset_478,40.5262342,-113.8824849
2/12/2019,Separator,Liquid Level Control,,,,,separator was having liquid carry over to the scrubber pot and it was flooding the fuel gas for the instruments. by installing cold finger it will help reduce the amount of liquid on the fuel gas for the instruments,user_28,asset_1741,48.1602729,-103.6179603
10/14/2019,Separator,Choke Valve/Loop,,,,Corrosion,The automated choke was leaking by and loading the well. All internal parts were replaced and the choke was calibrated.,user_68,asset_1573,41.474544,-90.6778637
1/6/2017,Gas Scrubber,,,,,,"All water dumps on location frozen, bath hot and pumps running. All water going to oil tanks, tanks getting high, thawing",user_87,asset_1272,48.01100375,-103.4279473
10/1/2019,Automation,Battery,Battery,Interstate,Blue Top,End Of Useful Life,Removed 72 (6 Volt) batteries from 6 banks of 12 batteries form racks in PLC building. Installed 48 (12 volt) batteries in 6 banks of 8 batteries into racks in PLC building. Verified voltages at each rack. ,user_169,asset_1861,46.2356189,-100.6010498
3/17/2018,Compressor,Compressor (Recip),Scrubber Level,,,,Drained scrubbers,user_46,asset_1999,48.0614644,-104.8417043
6/4/2018,Tanks/Pits,Liquid Level Control,,,,,"Pad shut in on false high tank, went to location visually checked all tanks found tanks in good shape. Reset alarm and rtp’d pad. ",user_58,asset_1915,48.37141687,-103.5204387
4/21/2018,Instrumentation,Controller,,,,,"The plunger cycles are not consistent on this well. This is a Kelvin controlled well that has too much off time in the criteria. This well runs best with 45 minutes of off time on it. Kelvin has this well with ~80 minutes of off time, costing us gas volume every day.",user_50,asset_807,48.1470144,-103.6180489
2/15/2017,Gas Scrubber,Shell,Nozzle,Other,Other,Other,Adjusted burner to get proper fuel air mixture,user_62,asset_456,48.2816201,-102.855151
4/13/2019,Separator,Dump Line,,,,Erosion,"The pneumatic motor valve on the lP separator condo dump allocation meter loop is bad and had to be replacesed with new, the valve was leaking through the rusted back of the motor.",user_174,asset_1140,39.2506642,-92.4357879
11/9/2017,Separator,Choke Valve/Loop,,,,Corrosion,"Choke hand wheel was turned out 1 1/2 turns , returned to normal position",user_109,asset_1730,48.2117231,-103.7735163
7/22/2019,Pipeline/Piping,Piping,In-Line Check Valve,,,Vibration,"Got sent to location for a possible gas leak, IBEX Gauger called in stating she heard gas blowing near a methanol tank. When I got to location she was blocking road to make sure nobody could enter. I then parked a location entrance, and then walked in to investigate. There was a 3/8 methanol busted off by Cows rubbing on it, the Lateral riser over past Williams meter shack. Williams methanol injection broke and venting gas, methanol was shut off, so no fluid leaks but gas was venting. Shut valves, and plugged, and Williams notified.",user_2,asset_1681,46.2356189,-100.6010498
4/5/2018,Separator,Choke Valve/Loop,,,,Trash,Well was deferring due to choke not holding. I suspected trash holding the stem open. Operator closed the ESD and actuated the choke twice. Operator opened the ESD and verified the choke was holding. The choke was holding. Started the well back on plunger cycles. Will probably have a long off time due to the long flow out causing the well to load. The fix for this is using downstream valve for well control. The trash will drop out in the vessel before going through the sales valve.,user_50,asset_834,48.1470144,-103.6180489
3/28/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,fluid,Site visit resulted in draining the scrubber.The front end filters were all dry to the chokes and the dvc's. Cold fingers seem to be having positive results in keeping the fluid out of the supply gas system or a buy back meter would be beneficial on this site due to a small number of wells with upstream control valves.,user_50,asset_825,48.1507681,-103.6208284
3/26/2019,Surface Location,Lease Road,,,,Weather,3/26/19 Plowed access roads & turnarounds. Ops can attempt to RTP well.,user_42,asset_1142,46.2356189,-100.6010498
9/17/2018,Wellhead,Tubing,,,,,ENG REQUEST Engineers wanted well to be worked on as well as to check equipment on location Performed the check they wanted and then vented well for 46 mins Well did unload so i shut it and im going to allow it to build pressure then determine if it needs another vent or just put back to sales ,user_56,asset_1271,48.2651756,-102.8785229
2/11/2018,Flare System,Flare Header,Regulator,,,,Issue: SCC # 1 down Root Cause: looks like the fuel gas line froze off. was able to break and drained the fluid Fix: relight and returned to service ,user_136,asset_57,48.2595091,-102.9010563
12/8/2016,Compressor,Compressor,Suction Controller,Other,,Freezing,Fuel supply freezing at Kimray valve suction controller. Thawed and RTP'd.,user_141,asset_265,48.3619066,-103.2129855
8/19/2019,Separator,Fuel Supply System,Regulator,Fisher controls,67CR-206,freeze,"OPS: Replaced main burner fuel gas supply regulator and fisher control/dump fuel gas regulators on A and B units as well as block and bleed on A unit. The regulators are over pressuring the end devices despite adjustment, likely due to multiple freezing incidents during 18/19 winter season, damaging regulator internals and damaging the block and bleed in the A unit. OPS left online flowing to the B unit.",user_54,asset_1323,40.5262342,-113.8824849
5/15/2019,Instrumentation,Choke Valve/Loop,,,,Corrosion,Found DVC malfunctioning holding choke open causing well to load. Repaired DVC and attempted to vent plunger but did not come in. Left ESD shut for pressure build.,user_18,asset_690,,
4/10/2017,Wellhead,Other,Other,Other,Other,Other,,user_50,asset_772,48.16023812,-103.6172241
6/4/2017,Compressor - Gas Lift,Compressor,Lubricator,Ariel,,Trash,Gas lift compressor down on High Compressor Oil Temp. All doors and roof opened on building. Was able to get louvers opened a little more. Outside temp has dropped about 6 degrees in the last hour. Hopefully be enough to keep it from shutting down again. ,user_141,asset_551,48.1003415,-103.5854403
7/1/2019,Surface Location,Valving/Swedges,Body,,,Freezing,Went to Luman 17 ponds and remove used cam locks fittings from piping laying in the yard there and re installed them on site,user_21,asset_1827,39.2506642,-92.4357879
2/7/2019,Tanks/Pits,Flare/Combuster,,,,fuel gas freeze," 3 scc's out, relit 2 of them the other 1 has frozen fuel gas, can't get with 100' of scc's to thaw",user_31,asset_1423,48.1470144,-103.6180489
12/20/2016,Automation,,,,,Other,,user_134,asset_299,48.1583546,-103.6167495
4/3/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,kicked well on and pause flowing got plunger to come in cycles resumed.,user_11,asset_2153,40.7126799,-114.1193569
4/3/2018,Separator,Temp Control System,Thermostat,,,,"bath temp turned down due to recent temps, turned up temp and adjusted glycol pump strokes, well rtp'd",user_115,asset_2203,,
11/4/2017,Compressor,Compressor (Recip),Scrubber Level,,,,"found the 1st stg suction scrubber full, new dump controller not set right by vendor wasn't dumping, adjusted to dump/blew all the scrubbers down , drained the control valves and desi/rtp compressor restart wells",user_131,asset_2073,40.7126799,-114.1193569
2/20/2017,Chemical System,Tank,,Other,Other,Other,Plunger hung up ,user_50,asset_766,48.16878927,-103.4446365
2/11/2018,Flare System,Flare Header,Regulator,,,,Issue: Called Out SCC (F) alarm Root Cause: with the temp swings has caused an excess of fluid to drop out in the fuel gas and is freezing in the regulators. Making them over pressure and then the pilot flame becomes unstable and is burning past the pilot tip instead of in the rose bud tip then the thermocouple temp alarm starts bouncing in and out triggering an alarm every time Fix: thawed out the regulator and drained the fluid out of it,user_136,asset_676,48.2595091,-102.9010563
3/29/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,Well is waiting on load ratio for over 400 min. Has had consecutive non arrivals. Lifted plunger and paused on to see if we could get an arrival. Will go vent plunger in if needed,user_172,asset_857,,
8/29/2017,Instrumentation,Meter,Orifice Plate,Bristol,4203DR,Recalibrated,Meter was froze had to send a download to the RTU and power cycle the meter.,user_13,asset_1825,48.3619066,-103.2129855
6/11/2018,Pipeline/Piping,Pipe/Components,,,,Corrosion Under Insulation (External),Insulation on pipe tape is cracked and is becoming and will be useless as time carries on. Needs to be retapped ,user_58,asset_580,48.3726719,-103.51747
6/5/2018,Plunger System,Plunger,Plunger,Well Master,,Corrosion,"Plunger wasn’t falling, got free and dropped",user_86,asset_1055,,
12/14/2017,Gas Scrubber Separator,ESD,,,,,"well went down on valve fault-ESD shut & wouldn't open remotely, need to troubleshoot-found the scrubber full of liquids, had to drain, and drained fuel filters, tried to drain desi-found the ht trace not lined up drain was froze, got the globe valve lined up and ht trace circulating to desi now, adjusted regs to ESD",user_131,asset_1046,40.7126799,-114.1193569
3/7/2018,Separator,Liquid Dumps,Supply Line,Fisher,,Freezing,Thawed out both dumps inside the cabinet and fuel supply system on the unit and cleaned pilot for the burner. Root cause was the fire going out and both dumps freezing which flooded the fuel gas lines and shut the well in.,user_100,asset_1278,48.1470144,-103.6180489
2/13/2019,Heat Medium,Pump,Housing,Sunpumper,113,Wear,Replace glycol pump and repair insulation,user_21,asset_558,46.2356189,-100.6010498
5/30/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,I went to location and surfaced plunger then put back on plunger cycles.,user_51,asset_2209,40.7126799,-114.1193569
9/12/2017,Plunger System,Plunger,Plunger,PCS,,Not Optimized,well was missing arrivals and deferring production,user_179,asset_2047,48.3619066,-103.2129855
8/6/2019,SWD System,Particle Filter,Element,,,,"Walk through, took readings, change filters due to high filter differential pressure. ",user_55,asset_523,,
5/20/2019,Tanks/Pits,Tank,Shell,,,Weather,called out on high tank#761383 at 17-1x4-5 switched to#82 while onsite i heard gas hissing coming from the bottom of water tank#761383 walked around to other side of tanks from leak and there is a puddle 30ftx5ftx6in it had recently rained so i dont know how much is the leak and how much is rain. reported to dean tagged out tank will submit WM and SV,user_37,asset_64,40.5262342,-113.8824849
8/5/2018,Gas Scrubber Separator,ESD,,,,,"Frew 8-70 down on low unit pressure between cycles, RTP and started cycles remotely.",user_37,asset_1642,48.3619066,-103.2129855
4/5/2017,Gas Scrubber,Other,Other,Other,Other,Other,Froze in Flow Line and Choke ,user_138,asset_901,48.07900987,-103.5155094
1/4/2019,Heat Medium,Pump,Bearings,Texam,375,Weather,*GLYCHOL PUMPS NOT YET TURNED ON FOR WINTER. STARTED GLYCHOL PUMP,user_34,asset_530,43.56424,-91.351691
3/17/2018,Heater Treater,Burner,BMS,,,Loss Of Fuel Gas,Issue: low pressure bath Root Cause: ran out of fuel gas when the location shut in on hi condo tank Fix: once i got the location pressured back up I was able to relight,user_136,asset_1212,48.1470144,-103.6180489
1/19/2019,Compressor,Compressor,Cylinder,Ariel,,Vibration,Compressor down on high compressor vibration I couldn't find an issue I had to thaw out the suction controller I left my tarp on the suction controller. I found that the line to the well head was froze I cleared freeze the glycol was a bit cold and the injection temp was around 47 degrees which is pretty cold for a gas lift injection.,user_159,asset_2046,40.5262342,-113.8824849
1/18/2017,,,,,,,False high tank. ,user_163,asset_284,47.90417963,-103.4875053
10/7/2018,Separator,Temp Control System,Thermostat,,,,"low glycol level, too low to run pumps",user_31,asset_985,43.252261,-115.0567324
7/1/2017,Separator,Choke Valve/Loop,,,,Trash,"Invalco 2""inlet valve was replaced because the trim seat/stem could not be removed for replacement ",user_163,asset_1690,48.20145459,-103.5626792
2/24/2018,Dehy,Contactor,Trays,,,,Williams dehy frozen. Separator is up to temp and glycol pumps running. Contacted Chris with williams. No answer left message,user_153,asset_26,48.17970994,-103.7377134
9/19/2018,Chemical System,Pump,Seals,Texam,HBC1,Wear,"packing worn out and leaking methanol into the containment tub, replace and RTP'd",user_25,asset_1707,,
9/7/2019,Tanks/Pits,Flare/Combuster,,,,,"relight scc's by hand, no igniters on these scc's. out due to wind/rain",user_64,asset_15,40.5262342,-113.8824849
11/17/2017,Fuel Gas/Start Gas,Coalescer/Filter,Mist Pad,,,,Wells are on cycles and ran out of fuel gas had to jump bak on and rtp,user_58,asset_102,48.32405522,-103.617736
4/17/2018,Separator,Choke Valve/Loop,,,,Freezing,burner was out and there was a freeze in coils/choke relight burner ,user_11,asset_1657,40.7126799,-114.1193569
11/28/2017,Separator,Liquid Level Control,,,,,"Tci scrubber got a slug of liquid when the comp was taken down for a PM , liquid build up in pipe do to temp swings, high kill switch is 1ft from bottom of the scrubber with 5ft of room above it till it dumps to the tci , engineering is working on replacing with a different set up ",user_122,asset_1675,48.38726957,-103.8415215
3/21/2018,Fuel Gas/Start Gas,Regulator,,,,,Well is cycling but not showing any volumes Suspect DVC is not opening choke Found kimray fuel pot full of liquids Weather could be the cause of this. but during the meantime i will lower bath temp to see if that will work to having dryer fuel gas Also found big kimray fuel pot full as well Drained both as well as the desi RTP'd well ,user_53,asset_1328,40.7126799,-114.1193569
3/13/2018,Heater Treater,Burner,BMS,,,Pilot Went Out,Issue: found Bath (B) down on the HMI Root Cause: there wasn't any (INT) but there is work going being done on location and they may have shut the pilot gas off and knocked down the burner Fix: I was able to relight the bath remotely,user_136,asset_224,48.1470144,-103.6180489
3/4/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,Well had shut in on non arrivals due to DVC fuel gas line was flooded I cleared it and brought well back online,user_51,asset_1203,48.0614644,-104.8417043
3/25/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Brought up plunger ,user_86,asset_1091,,
11/28/2017,Compressor,Compressor,Scrubber Level,Ariel,,Freezing,"Compressor down on High Suction Scrubber level. Freeze in dump line, thawed freeze and drained scrubbers. Turned glycol pump on to assist with freezing issue. Warmed up compressor and put back online",user_141,asset_453,48.1470144,-103.6180489
10/8/2018,Separator,Temp Control System,Air Valve,,,,"02 mixture was too much, causing the burner to woof itself out.",user_54,asset_1614,48.0831247,-104.8694691
5/21/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,Drained desi while on location working on well 140. No fluids present.,user_62,asset_296,40.7126799,-114.1193569
3/22/2018,Wellhead,Wellhead Piping,,,,hydrate,"Found freeze in casing. Closed tubing and opened casing, sent it to sales, freeze broke. In the process, knocked gas lift down on high discharge. Let 10 well casing flow until I confirmed freeze cleared. Put valves back in normal operating position. Adjusted inlet valves to where I thought they would work best. Restarted compressor, continued to adjust valves. As of this time, going into both wells. Will monitor throughout the day. Found 1 SCC out, relit.",user_141,asset_2055,48.1470144,-103.6180489
4/11/2018,Automation,Radio,Fuse,3M,,Unknown,"Meter locked up, sent task request to measurement",user_35,asset_1794,48.20370019,-103.453171
6/8/2017,Wellhead,Tubing,,,,,"tubing freeze, will leave equalize overnight",user_39,asset_948,48.0357148,-104.9369376
12/14/2017,Instrumentation,Controller,,,,,"Kelvin did not operator pad properly, had all wells on an off cycle at the same time. ",user_53,asset_1996,40.7126799,-114.1193569
2/12/2018,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,"Issue: Callout shut in alarm Root Cause: couple of issues. wells have to much off time allowing the pumps to use up all the fuel gas and there is no saving it because the pressure shut down set points never got put back after the compressor got removed Fix: jumped pad back on, readjusted a couple of the wells set points to callout earlier so can catch the pad before there is no recovery. Long Term fix is to get the buy back meter in operation ",user_136,asset_1332,48.2595091,-102.9010563
9/18/2019,Pipeline/Piping,Valves,,,,End Of Design Life,Pressured up flow line and separator no leaks. Started flowing well. When plunger arrived noticed fluid leaking from sales line cyclonic. Shut well in. Tagged out. Removed plunger 2 1/8 ordered plunger. Will replace when cyclonic is repaired ,user_90,asset_1389,48.09320377,-103.6505409
4/16/2018,Automation,Plunger Arrival Switch,,Tripmate,,,Tripmate failed. Probably end of useful life.,user_134,asset_1617,48.1470144,-103.6180489
5/21/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,notified by day ops gl comp dwn-dwn on high discharge-broke a freeze on 10 well-warm up/drain liquids/rtp comp/wells10 & 20-also checked meth/ vapor locked/adjusted,user_131,asset_551,40.7126799,-114.1193569
12/12/2017,Compressor,Compressor,Lubricator,Ariel,,Freezing,,user_48,asset_1675,48.32723201,-103.656564
1/18/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Found the Kimray drip pot on choke to be full of liquid. Found the fuel gas for the location was not routed correctly through desi dryer to more thoroughly dry the gas. Corrected valve position and drained liquids from drip pot. While on location, checked the WFS dehy and saw the meter for Buy back has been installed. I will check the MOC to make sure we are good to commission the buy back meter to start getting dryer gas to the end devices.",user_62,asset_1735,48.1470144,-103.6180489
1/14/2018,Fuel Gas/Start Gas,Regulator,,,,,Issue: found flare down on the HMI Root Cause: found the unprotected and exposed regulator froze at the flare. Fix: thawed out the regulator drained the fluid out of the line and relight flare ,user_136,asset_2046,48.1470144,-103.6180489
1/9/2019,Tanks/Pits,Piping,Equalizer,,,Freezing," 9. Luman 9-2 - check on tank automation failure • No automation installed in tanks • I found the expansion union for the crossover at the top of the tank leaking on the condo tank side, I notified Dean kinsey of findings • I found the water dump line shut and not the condo dump • I closed the correct dump line and waited for Jake and Ibex to get here • Jake got to location and I handled off leak to Jake • Ibex and Jake were able to pull the tank down and offload into the water tank to stop leak ",user_38,asset_1817,48.16032603,-103.6184276
2/24/2018,Tanks/Pits,Flare/Combuster,,,,,SCC out due to unit losing pressure. Rtp SCC,user_153,asset_1990,48.18122205,-103.6144792
10/27/2018,SWD System,Particle Filter,Element,,,,Replace filters and restart pump due to dirty produced water and dirty tanks,user_55,asset_101,,
11/18/2017,Compressor,Compressor,Process Gas Supply,Ariel,,Freezing,Froze in check valve ,user_156,asset_1675,48.27155911,-102.8691835
4/20/2019,Dehy,WFS Issue,,,,,Freeze downstream of meter. Dehy tech used methanol trailer and broke freeze in about 30 seconds.,user_55,asset_841,,
12/13/2018,Separator,Dump Line,,,,Freezing,"Dump line was froze at the end of the separator. Thawed on it, freeze broke. RTP'd well",user_55,asset_408,,
10/12/2017,Compressor,Compressor (Intergral),Panel,,,,compressor was showing a code 48 for equipment shutdown. checked oil levels and coolant levels and verified comp was safe to run restarted and had no more problems with it.,user_71,asset_1884,40.5262342,-113.8824849
3/1/2017,Gas Scrubber,Mechanical Dump Valve,Controller,Other,Other,Other,Chokes not functioning at all,user_88,asset_1388,48.08465378,-103.6178047
4/19/2017,Wellhead,Primary Choke,Stem/Seat,Lufkin,Other,Other,choke leaking causing well to constantly flow and eventually log well off,user_11,asset_1348,,
7/27/2019,Instrument Air,Compressor,Instrument Gas Supply,Gemini,,Trash,"pad is esd with no interlock again. arrived onsite and found both air compressors down due to overheating. contacted team lead and got bob fox number. contacted bob and he helped me troubleshoot air compressors over the phone. found both fans turned off in compressor and generator rooms, started fans to help cool rooms. checked oil levels on both air compressors. both of the were ran completely out of oil. filled them both, cleared alarms and restarted both units. dryer is having issues, its not switching bottles properly. bob said its been over 6months since hes performed a PM on this equipment. my recommendation is that our leadership schedules a PM with bob fox ASAP. this equipment will continue to fail if not maintained.the instrument air is carrying fluids because dryer is not fully working. please leave door open to air compressor room to help keep cool.drained dezy and scrubbers on four packs.drained regulators to esd's and DVC's. drained filters inside cabinets to dump controllers.restarted the 60,80,100,120 and the 40 on plunger cycles. put the 130 and 10 in auto to flow out high pressure so we can eventually restart gas lift. if air compressors fail again, please leave pad down and contact PTL. tanks are low and restarted scc's. contacted fluid management to let them know pad has been rtp",user_120,asset_491,39.0112008,-92.3881993
8/31/2017,Pipeline/Piping,Pipe/Components,,,,End Of Design Life,Repaired and retapped pipe insulation. ,user_41,asset_1086,48.19432792,-103.5549172
5/13/2018,Separator,Fuel Supply System,Regulator,,,corrosion,Big Joe regulator not holding back pressure. ,user_41,asset_1806,48.23293618,-103.5361587
11/14/2017,Heater Treater,Burner,BMS,,,Loss Of Fuel Gas,Drain fuel gas scrubber of liqiuds,user_109,asset_1323,48.3595548,-103.7770318
11/29/2018,Flare System,Flare Header,Instrumentation,,,,Issue: Arrow Dispatched for SCC Root Cause: shows SCC down time. Fix: SCC is running but the condo rate has dropped off so far the thermocouple doesn't register a hi temp tipping the alarm Long Term Fix: may need to relook at the SCC sizing ,user_170,asset_796,48.3619066,-103.2129855
3/6/2018,Gas Scrubber Separator,Dump Line,,,,Erosion,Mon 11-150 checked equipment and drained scrubbers. ,user_71,asset_2046,40.5960545,-113.9323891
1/31/2018,Instrumentation,Controller,,,,,"Kelvin failed. Kelvin let all wells be on their off cycle at the same time, resulting in the compressor running on the off skid recycle, ending in compressor going down on low discharge. need kelvin to optimize this pad to where we don't have all wells off at the same time. drained compressor and scrubbers, restarted compressor warmed compressor and RTP'd well ",user_53,asset_157,40.7126799,-114.1193569
1/14/2017,Compressor,Compressor,Process Gas Supply,,,Freezing,Williams line pressure a little high. Hit high second stage pressure. Restarted rtpd ,user_175,asset_934,47.88210802,-103.5965656
11/9/2018,Fuel Gas/Start Gas,Regulator,,,,,"main gas on 160 was set over 10psi , causing main to blow out, adjusted main to 8psi and main wouldn't blow out when i tried ripping open the main ball vale to the burner.",user_144,asset_0,48.1470144,-103.6180489
2/28/2019,Separator,Choke Valve/Loop,,,,Freezing,Unable to access location due to snow drifts. Blade is working on road coded to maintenance.,user_18,asset_814,,
12/3/2017,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,"Kicked well on due to non arrivals. Paused opened and watched. Plunger came in, restarted cycles.",user_141,asset_2225,40.5262342,-113.8824849
7/14/2019,Separator Inlet Valve (XV),Controller,,,,,HiLo controller was not allowing HiLo to open. Depressured and then turned pressure back on and HiLo opened. Having optimizer flow out for the due to high pressure. ,user_94,asset_1611,39.2506642,-92.4357879
3/23/2018,Flare System,Flare Header,Regulator,,,,Doing my site vist and swapping tanks. Checked pit and dehy tubs. Checked equipment and went through dumps. Fuel gas scrubber on pilots at scc had around a 1/4 gallon. kO pot on flare line had 2” built up. Drained all scrubbers onsite,user_172,asset_261,,
2/27/2017,Gas Scrubber,Other,,Other,Other,Other,"hydrate in SS to DVC/choke, was in 1/4/ piping not HT or insulated 1' header is ",user_115,asset_453,48.224585,-103.8291059
4/5/2017,Gas Scrubber,Other,Other,Other,Other,Other,None,user_112,asset_984,48.07873758,-103.6604067
4/4/2017,Heater Treater,Firetube,Firetube,Other,Other,Other,Loss of production ,user_58,asset_197,47.99306476,-103.4222366
2/16/2018,Separator,ESD Valve,Actuator,,,Trash,Bad block and bleed on the hi-lo,user_130,asset_266,47.88294546,-103.5195374
3/19/2018,Flare System,Flare Header,Regulator,,,,"Fuel gas line froze, due to liquids in fuel gas and temperatures drop cause line to freeze. Thawed out and returned to service ",user_58,asset_298,48.41618671,-103.5722643
12/9/2016,Automation,Cable,Data Cable,Automation-X,Other,Loose Connection,Thawed choke controller on well 10 ,user_62,asset_1280,,
2/12/2018,Plunger System,Plunger,Plunger,PCS,,Not Optimized,changed out worn dual pad with new dual pad,user_11,asset_709,48.1470144,-103.6180489
12/21/2017,Separator,Dump Line,,,,Freezing,Jumped unit back up and thawed water dump line and big Joe unit lost pressure at 1am . Got glycol bath and scc going RTP well,user_100,asset_736,48.1470144,-103.6180489
4/19/2019,Separator,Liquid Level Control,,,,,Dump controller leaking due to maybe corrosive water or wear and use over time. ,user_17,asset_293,48.23909244,-103.6179428
3/5/2017,Compressor,Compressor,Valves,Other,Other,Other,Compressor was up and down for about 1 hour while I adjusted discharge valved to wells.,user_141,asset_551,48.224585,-103.8291059
4/7/2018,Flare System,Flare Header,Instrumentation,,,,Issue: while on location i found the Abeutec # 4 SCC was down Root Cause: went down on flame failure. These SCC's are super close together and the radiant heat they put off is extreame. I think some of the issues are the heat is messing with the SCC when its trying to start up thinking its detecting a flame. second the shutting on and off from the pressure is just working the equipment way to much. With the Abeutec's not reliable at all them shutting on and off is causing them to fail even more. Then when they don't relight they send the ones that are running into a glowing stage that is going to shorten there life span. Fix: remove the set points and just let them run all the time especially on extremely hi profile wells like this one ,user_136,asset_1383,48.1470144,-103.6180489
4/28/2018,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Plunger worn,user_126,asset_1275,,
6/9/2017,Compressor,Compressor,Process Gas Supply,Ariel,,Trash,"Comp down on high discharge, warming up now, will rtp shortly",user_84,asset_609,48.00707834,-103.4963729
7/10/2018,Plunger System,Plunger,Plunger,IPS,,Not Optimized,PLGR lost arrivals due to incorrect cycle criteria. Vented and RTPd,user_107,asset_1404,,
9/22/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Trash,"Compressor down on Low Discharge. We discussed this earlier when it was set at 15%. Seemed awful low. It was raised to 40%. That's where I found it. Reset to 20% and will see what happens. Discharge pressure was 641 after 15 minutes, low shutoff is 550. Closed valve to 18%. Discharge pressure up to 681. Seems a little more tolerable. Left at 18%. Everything looks good",user_55,asset_1264,,
9/25/2018,Compressor - Gas Lift,Compressor,Regulator,Sertco,,Freezing,"Whole pad went down as a result of gas lift wells going down. Without the gas lift wells flowing the Lateral compressor will suck the units down to the point they shut in on low pressure. There are not enough wells flowing into this compressor and with that these wells all have long shut in times. The lateral completely depends on consistent flow from the 2 frewen 8 gas lift wells, lose one we lose it all. The compressor will only recycle for so long before pulling everything down when nothing is flowing. Gas lift compressor blew out some ice when I blew it down, adjusted loovers so they are shutting down sooner",user_106,asset_1961,48.2575609,-102.9119612
12/20/2017,Instrumentation,Controller,,,,,kelvin failed to keep unit pressured up. burp setting needs to be fixed ,user_53,asset_1924,40.7126799,-114.1193569
2/22/2017,Instrumentation,Other,Other,Other,Other,Other,Gas leaking ,user_166,asset_61,47.99941309,-103.6412349
6/16/2017,Compressor,Compressor,Suction Controller,Compressco,,Vibration,compressor down on low suction RTP,user_71,asset_2059,40.5960545,-113.9323891
2/5/2018,Compressor - Gas Lift,Compressor,Valves,Gemini,,Freezing,compressor went down on high discharge pressure.the 140 had a freeze on the casing / Meth was pumping but tank is low will but in a meth order for the 140 well. Broke freeze and RTP compressor and both wells,user_100,asset_1359,48.1470144,-103.6180489
9/27/2019,Flare System,Flare Header,Process Indicator,,,,Re piped the new pilot line on the flare line and returned to service,user_21,asset_2046,46.2356189,-100.6010498
2/25/2017,Gas Scrubber,Other,Other,Other,Other,Other,Lost heat trace to fuel supply for compressor. Working to get compressor up now heat trace is fixed,user_163,asset_1352,48.21100565,-103.7732289
12/6/2017,Separator,Temp Control System,Fuel Gas Supply,,,,Graco 1590 hole in diaphragm ,user_50,asset_1406,48.33578926,-103.5982547
9/21/2018,Flare System,Flare Header,Regulator,,,,"Pad had shut in due to WFS issues the other night. Wells didn't reset after being shut in for Sales Pressure High. Jumped pad back on, opened ESDs and restarted cycles on all wells. Relit all 3 SCCs. Had to adjust ignitor on SCC B.",user_55,asset_46,,
4/17/2019,Separator,Temp Control System,Pilot Valve,,,,"attempted to pull graph before going to location but could not find graph for this well.arrived onsite and found well had been shut in for winter ops. previous operator did a good job at tagging and blowing down equipment.got permission to remove tags,and filled out the pre start up checklist.opened up williams inlet and removed tag.opend master valves on tubing,found zero leaks. pressured up flowline using 100 psi from wellhead.opened choke and bypass on hi lo.slowly pressured up unit. hi lo opened at around 60 psi. checked for leaks on equipment couldn't find any.i paused open sales line cyclonic so i could flow off some of the built up pressure. tubing had around 900psi and 900 on casing.shut choke on separator and it was holding pressure. proceeded to open masters 100%.attempted to light bath on separator found pilot line was plugged with junk,cleared out pilot line and relit burner.tested burner by opening and closing main multiple times to verify main was not ""woofing"" out pilot. waited for temps to reach 80 degrees on glycol bath. checked bath level all good.started both glycol pumps and checked for leaks.one pump was struggling but i finally got it to work properly. i then opened choke and started selling gas. checked to see if williams meter was reading flow it was. checked jsams to see if it was reading flow it was.opened choke until one mil flowrate was achived. selling temp is around 59 degrees.increased bath temp around 5 degrees using t-12. thermo is reading 80 degrees shot bath temp with temp gun and it is more around 93.i adjusted big joe from 50psi to 80. verified big joe was holding at desired pressure. babysat choke until pressured dropped below 400psi on tubing,casing dropped 32 psi.well dropped down to line pressure and was struggling to unload fluids.i shut choke and opened blowdown cyclonic and started venting well to AGT.vented well for approximately 31 minutes,well began to unload and plunger came in. tubing and casing differential were withing 100psi of eachother. reset cyclonic to shut.and had optimizer restart plunger cycles.opened choke fully.did not get enough fluid on first cycle to verify fluid levels in separator were set correctly.waited until next cycle dumps seem to be set right. pressure tested both dump lines both trims are holding.pressure tested sales cyclonic while in an off cycle valve is holding. gauged both tanks and entered them into enbase. found missing plug on water load line. installed one inch plug on bleed. water load line also only has an inner valve does not have an outer. both four in and two in valves are shut and have seals. relit scc while onite.meth was shut off so i left as is. well has made arrivals on its last three cycles. well is rtp",user_120,asset_1933,40.5262342,-113.8824849
1/2/2018,Compressor - Gas Lift,Compressor,Process Gas Supply,Ariel,,Freezing,"gl-call out GL compressor down--troubleshoot/rtp-down on hi discharge psi /thawing out/warm up,can't find a happy medium with this one-atempt to rtp/installed a tarp on 3rd stg of cooler to see if this helps, to keep cooler open on 1st & 2nd",user_131,asset_1264,40.7126799,-114.1193569
1/11/2019,Surface Location,Well Pad,,,,Weather,Dump lines at tanks frozen due to not enough glycol circulation. Isolated only tanks in use to increase heat supply. Worked with steamer crew to get dumps free. Put pad back to production. May need to add 1 or 2 more solar pumps to be able to direct glycol to all surface equipment ,user_17,asset_592,48.18251153,-103.5380378
10/12/2019,Plunger System,Plunger,Plunger,PCS,,Not Optimized,Attempted to vent plunger to surface with no luck. Left ESD shut for pressure build.,user_18,asset_455,,
5/22/2018,Gas Scrubber Separator,Mechanical Dump Valve,Float,Kimray,,Out Of Adjustment,Issue: condo tanks getting lots of water in it Root Cause: found the dump out of adjustment yesterday and i adjusted it. stopped buy to see how my adjustment worked and if it needs more Fix: still no level adjusted a little more will check again tomorrow. hard to set with the well only flowing a couple times a day ,user_136,asset_2066,40.7126799,-114.1193569
11/2/2019,Automation,Charging System,,,,,"Arrived on location and checked pumps, they were running. Following the instructions I was given, changed settings in prostart controller so the pumps would run during the day when the sun was strong and not shut down on high voltage. Changed settings and reset controller and verified the pumps started back up and were working. ",user_15,asset_703,40.5262342,-113.8824849
12/6/2016,Compressor,Compressor,,,,,"Compressor went down on hi second stage discharge pressure, restarted ",user_148,asset_886,48.26312729,-102.8995745
3/13/2017,Wellhead,Other,,Other,Other,Other,"well logged ff, requiring vent to RTP",user_115,asset_916,48.224585,-103.8291059
9/19/2019,Heat Medium,Pump,Seals,Texam,HBC1,Wear,Changed out pumps,user_5,asset_984,41.474544,-90.6778637
4/25/2018,Fuel Gas/Start Gas,Regulator,,,,,Lost psi,user_86,asset_1461,,
10/18/2019,Separator,Temp Control System,Pilot,,,,Location was shut in for maintenance work. Work has been completed enough that the location could be brought back on line. Lit burners on all separators. ,user_15,asset_793,40.5262342,-113.8824849
2/22/2018,Sales Valve (PV),Pneumatic Control System (3Pgra),,,,,"Sales valve DG4 stuck open causing well to log off, function tested onsite and all worked, may have had Hydrate within system during the time it wouldn't close and caused well to log of",user_115,asset_291,,
10/28/2019,Gas Scrubber Separator,Dump Line,,,,Freezing,"Drained flare and fuel scrubber pots, drained the line heater scrubber pot, thumbed the dumps.",user_76,asset_787,46.2356189,-100.6010498
4/11/2019,Automation,Battery,Battery,Power Sonic,Model 112000,Weather,"Battery box tipped over by equipment from snow removal. Battery and box broken, work management entered to replace. ",user_44,asset_1102,,
6/14/2017,Compressor,Compressor,Process Gas Supply,Ariel,,Vibration,Root cause is not vibration it's low suction could not find it in tiles. Compressor went down due to low suction from pad shutting in on high water tanks 18+ feet ,user_103,asset_2239,48.22165058,-103.7500797
3/28/2018,Separator,Choke Valve/Loop,,,,Trash,Cleaned pilot tip and adjusted fuel mixture to burner,user_100,asset_1278,48.1470144,-103.6180489
2/28/2019,Surface Location,Lease Road,,,,Weather,Could not access location road drifted in. Coded to DW/WOM,user_94,asset_1852,43.56424,-91.351691
1/10/2019,Separator,Choke Valve/Loop,,,,Freezing,"Freeze in choke loop, thawed and broke freeze, verified gas flow through choke loop. ",user_44,asset_599,,
3/8/2018,Tanks/Pits,Flare/Combuster,,,,,Pilots in 4 SCCs were out. Re lighted and returned to service,user_60,asset_5,48.1470144,-103.6180489
4/27/2018,Instrumentation,Meter,Orifice Plate,Nuflo,4203DR,Installation Design," 5. High Point 27-2 - Wire up meter • Showed Ready where to drill the hole in the meter shack • Waited for Ready to complete Job including fire watch job • Installed CLX connector on okonite cable at meter shack • Realized we did not have a 1""-3/4"" RE ? Drove back to warehouse to get the part ? DNOW does not carry this part ? I looked all over warehouse and auto shop for part, could not find it ? I ended up grabbing 1""-3/4"" pipe bushing ? Talked to bob about getting the correct part in inventory • Arrived back to location • Finished installed wiring for meter • Verified wiring is correct and meter is communicating to RTU ",user_92,asset_1451,36.2541889,-91.2478009
4/1/2018,Compressor,Compressor (Recip),Valves,,,,"Got to location, whole pad was down all ESD's were shut Had to get pad back up, finally got ESD's opened lit burners Compressor was down on low discharge pressure, compressor sat there recycling for too long while all the wells were on off cycles Kelvin failure. RTP'd compressor and well ",user_53,asset_1996,48.2727581,-102.8682818
8/3/2018,Flare System,Flare Header,Instrumentation,,,,"CL 29-160 SCC callout, both SCC were out, relit SCC. ",user_37,asset_1035,48.3619066,-103.2129855
1/18/2017,Compressor,Engine,Fuel Gas Supply,Other,Other,Freezing,Down due to fuel gas freeze ,user_179,asset_597,48.01324487,-103.4975288
1/17/2017,Compressor,Engine,Water Pump,,,Oil Level,Compressor went down on low jacket water level. Called bob with jw Williams to fill. He filled I mentioned there might be a leak in storage tank he said he was aware of the issue and get it fixed when weather is more cooperative comp returned to service,user_11,asset_871,,
1/15/2019,Wellhead,Manual Valve,Wing,,,Freezing,Issue: when starting the RTP process i couldn't get the proper amount of turns on the tubing valve Root Cause: found the valves were froze. either they had not gotten shut all the way or they were leaking buy while they were shut Fix: moved the BP air heater on the well head and was able to get the valves thawed out opening and closing the proper amount of turns,user_170,asset_1760,43.56424,-91.351691
3/7/2019,Separator,Liquid Level Control,,,,,all water tanks at 15',user_64,asset_1819,39.2506642,-92.4357879
1/2/2018,Gas Scrubber Separator,ESD,,,,,call out well shutting in low psi-saved remotely & RTP-,user_131,asset_51,40.7126799,-114.1193569
1/13/2018,Instrumentation,End Device,Durag,,,End Of Useful Life,Issue: found SCC down on HMI Root Cause: had to rest the durag but wont stay rest. Fix: light SCC in manual. Durag needs replaced with a more reliable thermocouple ,user_136,asset_493,48.1470144,-103.6180489
8/31/2018,Pumping Unit,POC,Settings,Spirit,Genesis,Communication,Replaced Spirit controller with a Lufkin per team leader request. Bad data from Spirit controller not allowing rod pump to function like it should.,user_108,asset_1644,,
9/19/2017,Compressor,Intrumentation,,,,,Compressor C1 controller not actuating correctly. Adjusted controller sensitivity and pressure ,user_103,asset_1280,48.16030638,-103.6172875
3/30/2018,Chemical System,Pump,Instrumentation,Texsteam,HBT1,Wear,Fuel gas regulator for the methanol pump is bad and leaking gas through into the cabinet.,user_163,asset_1903,48.1470144,-103.6180489
8/8/2018,Dehy,WFS Issue,,,,,WFS meter (no share bar installed) not reading correctly and WFS working on solution. Likely last few days of open flow on casing is all false flow rate data. ,user_6,asset_1969,48.0831041,-104.869522
9/4/2017,Chemical System,Pump,Packing,Texam,HBC1,Wear,Western pump ,user_156,asset_2144,48.23314556,-103.6522955
9/7/2017,Wellhead,Cyclonic Valve,Actuator,,,Freezing,Torque limiter had been set to maximum. ,user_134,asset_667,48.1585395,-103.617363
5/5/2018,Plunger System,Plunger,Plunger,PCS,,Corrosion,pad plunger was worn out replaced with new pad,user_100,asset_1155,48.1470144,-103.6180489
1/11/2017,Gas Scrubber,,,,,,Choke leaking by will repair in next day or two,user_148,asset_1332,48.30615139,-103.6415772
10/26/2018,Wellhead,Cyclonic Valve,Actuator,,,Freezing,Old style actuator did not have torque limit,user_12,asset_306,48.1470144,-103.6180489
10/26/2019,Separator,Temp Control System,Heater/Burner,,,,"Sep C, main kept whoofing out the pilot. Adjusted regulators and got it going. Will monitor.",user_55,asset_1264,,
10/9/2017,Fuel Gas/Start Gas,Regulator,,,,,"Need sacrifice well to keep fuel gas going, waiting on buyback meter",user_35,asset_486,48.21105501,-103.4638566
4/4/2018,Tanks/Pits,Valving/Swedges,Body,,,Corrosion,Opened all condo tanks to operate battery as facility to maximize condo capacity onsite and align with predictive dispatch tools. ,user_62,asset_1849,48.1470144,-103.6180489
3/9/2019,Surface Location,Lease Road,,,,Weather,"road drifted in, no access",user_64,asset_402,,
2/9/2017,Chemical System,Pump,Packing,Texam,113,Debris,"Methanol pump not pumping, needs rebuilt ",user_107,asset_1928,48.30189351,-103.4042394
2/7/2019,Separator,Fuel Supply System, Big Joe Regulator,Fisher controls,,fluid,"Burner and choke failed due to fluid in the system, system flooded out due to temps and demand for fuel gas. Solution to fix is cold fingers.",user_25,asset_605,,
7/10/2019,Plunger System,Plunger,Plunger,Well Master,,Not Optimized,Wear: Plunger at end of useful life,user_54,asset_564,38.4425988,-95.5406131
12/24/2016,Automation,POC,Relay,,,Wear,DVC is bad. Not a freeze. Ran thaw tube and still won't actuate. Please repair or replace,user_175,asset_1978,47.95103744,-103.5791864
8/16/2018,Tanks/Pits,Electric Control System,Vent,,,,Primed pump using #8 pump. RTP'd land shark,user_55,asset_186,,
3/13/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Thawed out scc line and supply gas check dumps and burners . Fuel gas to the front end of the MOD was frozen pulled floor off the cat walk and thawed supply line under the walk way Got pressure to the esd and chokes. Drained all line on the front end of the Mod and check choke function on all wells . Will adjust cycles to maximize production on this pad all wells on this pad have been RTP.,user_100,asset_1120,48.1470144,-103.6180489
3/3/2018,Gas Scrubber Separator,Choke Valve/Loop,,,,Freezing,Champ 452 K finished opening choke. Checked equipment everything looks OK. ,user_71,asset_1212,40.5960545,-113.9323891
3/12/2018,Tanks/Pits,Tank Level,Probe,,,Weather,"Condo tank 37031C, high tanked. Waiting on pull bottom",user_141,asset_658,48.1470144,-103.6180489
11/7/2017,Separator,Choke Valve/Loop,,,,Trash,Auto choke not holding,user_111,asset_660,48.03881973,-103.4295886
8/2/2017,Compressor,Compressor,Process Gas Supply,Ariel,,Liquid Carryover,"Compressor down on low suction, all wells going to this comp, are plungers or cycled. Sometimes they all get in off cycle at the same time, the # 2 well is due for a vent, this comp runs good most of the time, no issues unless plungers loose arrivals, I run this comp. at 1780 rpm, slowed down to 1680 rpm for now,had it back up by 7:00 am this morning,",user_84,asset_2020,48.03627444,-103.5027181
1/31/2019,Tanks/Pits,Tank Level,Probe,,,Calibration Issue, +CHOKE SHUT IN AND TAGGED HIGH WATER TANK *WATER TANK HAS BEEN HAULED,user_34,asset_1271,43.56424,-91.351691
5/2/2018,Wellhead,Wellhead Piping,,,,hydrate,"wm has been turned in for glycol pump repair, shut well in for psi build to try brake freeze",user_122,asset_2056,48.1470144,-103.6180489
2/2/2017,Instrumentation,Transmitter,Flow,Other,Other,Other,,user_175,asset_2271,47.88269014,-103.5903787
2/27/2019,Chemical System,Piping,Discharge Line,,,Connections,"leak on check valve, connect was only hand tight, tightened and leak quit",user_31,asset_2087,48.257296,-102.863888
7/22/2018,Separator,Fuel Supply System, Big Joe Regulator,Fisher controls,,overpressure,60 psi gauge on scrubber was pegged. Removed gauge and verified zero. Adjusted jig joe until it was reading correctly ,user_31,asset_1384,48.28747484,-103.6497662
3/10/2018,Separator,ESD Valve,Gas Supply Line,,,Liquid Plugging,PAD dropped had to RTP,user_46,asset_1302,48.0614644,-104.8417043
7/25/2018,Wellhead,Manual Valve,Master Valve,,,Erosion,Found tubing master valve was leaking out stem were handle attaches to open and close valve. Installed one piece of packing and got leak sealed. Root cause is well has been shut in for over a year and has built up to 3500 PSI and caused packing to start leaking. ,user_15,asset_2243,48.1603317,-103.618705
12/19/2016,,,,,,,"Unit down til dumps thaw out, relit burner, temping everything up now",user_35,asset_1438,48.06084062,-103.470727
3/10/2019,Compressor,Compressor,Cylinder,Gardner Denver,,Freezing,"Vented well, unloaded liquids and rtp Loaded due to compressor to being down",user_63,asset_1421,,
12/15/2017,Fuel Gas/Start Gas,Regulator,,,,,"regulators going to SCC's froze because still having the issue with wet gas, the plan forward is to put in cold fingers on all t-packs which will solve the provlem",user_176,asset_2055,48.1470144,-103.6180489
6/19/2019,Tanks/Pits,Flare/Combuster,,,,, While on location I found all the scc's out and the esd's for the scc showing travel on Hmi but valve were all fully closed. Contacted Mike Edwards to help troubleshoot automation issue over the phone and discovered that is was a power issue in the PLC and that this would need a new Fisco before we could get the scc's running. Wrote work order for automation to fix.,user_10,asset_46,40.5262342,-113.8824849
10/19/2017,Separator,Choke Valve/Loop,,,,Freezing,suspected inlet freeze /broke freeze at inlet just passed the well blowdown valve and pressured up unit and rtp well called Brett for cycles,user_100,asset_93,40.5262342,-113.8824849
1/29/2019,Flare System,Flare Header,Regulator,,,,"Issues: found the flare down Root Cause: the fuel gas to the flare is wet from the wells flowing warm and having liquid carry over. So when people come to sight and see the heat trace is cool because the wells flow so warm they turn up the T-12's to make the heat trace warmer and in turn cause the carry over to get worse. To go along with that they made U in the line that catches fluid with no way to drain it and there is 20' of exposed pipe with no heat trace or insulation to protect it. Fix: i was able to drain the line as best as i could thawed out the pilot gas regulator. as for the carry over we should never regulate pressure at the flare that far away from any heat source, There should never be a U installed on purpose that doesn't have a drain, insulation, heat trace. As far as the flowing temps are i tried to get the glycol pumps installed at the line heater so the baths could run cooler but the decision was made not to do the up grade. This flare and LP has been turned into engineering for removal",user_170,asset_247,48.264926,-102.9013821
1/31/2019,Separator,Dump Line,,,,Freezing,"the dump lines froze due to the bath not having enough glycol to circulate, talked to Colton and he is ordering glycol for location. the glycol level is about 1/4 inch up on the 2 inch inlet pipe and not allowing any volume to go thru the pumps.",user_22,asset_118,46.2356189,-100.6010498
3/2/2018,Dehy,WFS Issue,,,,,"CL 29-50 pad gauger found a rupture disk leaking in one of the dehis. I isolated and blew down dehi ,Williams will need to be contacted.",user_71,asset_1800,40.5960545,-113.9323891
1/26/2018,Automation,Plunger Arrival Switch,,Tripmate,,, 4. Champlin 242 A-1 - MSO issue • Found Tripmate MSO installed • Removed tripmate • Installed cyclops MSO • Tested and verified good • Notified optimizer ,user_92,asset_100,36.2541889,-91.2478009
10/17/2017,Compressor,Compressor,Lubricator,Compressco,,Vibration,low compressor oil tech is dispatched to address,user_176,asset_524,40.5262342,-113.8824849
2/22/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Fuel gas to choke controller was froze. This pad had the winterization project done and is having issues with freezing in the poly lines and the metal pots. I thawed this out and the well was able to flow. I feel like I had less issues with the stainless lines and clear filters. ,user_50,asset_1396,48.32415991,-103.617741
1/10/2018,Plunger System,Plunger,Plunger,Ferguson,,Not Optimized,Issue: whole pad called out shut in alarm Root Cause: all the wells being in the off cycles at the same time and the pad ran out of gas Fix: not having all the wells shutting off a the same time. I left one well running to keep the units pressured up. Long Term Fix: get the buy back meter in service ,user_136,asset_767,48.1470144,-103.6180489
2/3/2017,Wellhead,Primary Choke,Stem/Seat,Other,Other,Other,,user_173,asset_1117,48.16020526,-103.6172393
12/12/2017,Gas Scrubber Separator,Dump Line,,,,Freezing,Drained desi dryer.,user_62,asset_1168,48.1470144,-103.6180489
11/21/2017,Compressor,Intrumentation,,,,,"Issue: compressor down alarm. found went down on low suction again Root Cause: Human Error, found the recycle had been adjusted so it wasn't opening. Fix: restarted the compressor adjusted the recycle valve and then tested 10times to verify it was working ",user_136,asset_2264,48.2594821,-102.9011497
4/14/2019,Instrumentation,Transmitter,Unit Pressure,Rosemount,3051,Wiring,"Actual cause of failure unknown. Display reads ""Sensor failed"".",user_12,asset_1165,40.5262342,-113.8824849
4/20/2018,Separator,Liquid Level Control,,,,,Found water dump controller door in the open position. Root cause is human error. Some one did not close it last time they opened the dump controller door. Closed door.,user_62,asset_2066,48.1470144,-103.6180489
1/25/2017,Compressor,Compressor,Lubricator,Ariel,Other,Liquid Carryover,There is an oil leak somewhere on engine or compressor can't tell exactly where it's coming from but making a mess on skid/notified to,user_131,asset_2073,47.88298305,-103.5120531
1/8/2019,Heat Medium,Pump,Crankshaft,Texam,HBC1,Wear,"Motor on solar pump seized up inside motor housing and also faulted out the speed control box. Replaced both the motor and speed controller. Manufacturer, model and root cause incorrect. ",user_33,asset_1174,48.21120683,-103.7735031
6/19/2017,Instrumentation,Transmitter,3N1 MVT,Rosemount,4088,Recalibrated,Complete calibration ,user_113,asset_1518,48.32424369,-103.61754
1/12/2019,Heater Treater,Burner,BMS,,,Pilot Went Out,"Issue: while performing my walk around i found the line heater down on the satellite well Root Cause: found many issues, first when i got there the burner was just blowing gas. Then i found fluid in the scrubbers casing the regulators to act sticky, then the line heater was only set to 88deg Fix: I drained the scrubber before i started and then after it ran i blew the rest of the fluid build up in it out again. I pulled the pilot line off blew out the fluid in it then i was able to get the burner relight. Once the burner was running i was able to get the regulators thawed out, when the bath hit 88deg the burner was running rough so i raised the T-12's to get the bath to 150deg and adjusted the main burner for a more efficient burn and fast heat up. ",user_170,asset_314,40.5262342,-113.8824849
7/29/2019,Fuel Gas/Start Gas,Dump Line,,,,Corrosion,Arrived on location and found that regulator to dump contollers was bad. Repaced with a 67 cfr 0-35 regulator. Set pressures and tested dumps.,user_153,asset_869,48.262246,-103.6132885
10/15/2018,Separator,ESD Valve,Gate/Seat,,,Freezing,"hi low froze, thawed out, needs insulation",user_31,asset_48,43.252261,-115.0567324
7/14/2019,Separator,Temp Control System,Pilot,,,,"Well was loading up from a partial freeze in wellhead and some cycle issues. Broke freeze and RTP well. Pilot was out on separator, relit",user_31,asset_284,43.56424,-91.351691
2/4/2018,Separator,Fuel Supply System,"Moisture, Regulators",,,,Pilot plugged up on the fuel gas separator. Took pilot apart and cleaned it out. Put back together relit burner,user_172,asset_705,,
8/24/2017,Fuel Gas/Start Gas,Coalescer/Filter,"Process Indicator,Shell",,,,ball check kept checking fuel pot while it was dry ,user_53,asset_1056,40.7126799,-114.1193569
2/21/2019,Separator,Dump Line,,,,Freezing,"Attempted to RTP well. Found that the scrubber was ball check. Drained scrubber, and got the ball to drop. Got the burner relit on Sep A. Started checking dumps, found that dumps are froze. Checked a few others and all are froze. Will write a work order to have steamer come and thaw dumps.",user_55,asset_330,,
2/13/2018,Flare System,Flare Header,Regulator,,,,"call out SCC- all of them were down, went there in relit-back in service not sure why all were down-everything looks good?",user_131,asset_1302,40.7126799,-114.1193569
3/5/2018,Fuel Gas/Start Gas,Coalescer/Filter,Elements,,,,"Drained desi while on location working on well 50, 80 and 150. Took 30 seconds for fluid to drain.",user_62,asset_998,40.5960545,-113.9323891
2/25/2018,Heater Treater,Dump Line,,,,Freezing,Water dump on LP unit froze. Luckily we caught it quick enough that we weren’t sending water to oil tanks. Water line froze off right inside cabinet. Thawed out line and got vessel water level dropped down to normal.,user_172,asset_1513,,
3/17/2017,Wellhead,Other,,Other,Other,Other,"filed down knock out rod to remove chips/burrs, replaced 6"" pacer sleeve",user_115,asset_2201,48.3619066,-103.2129855
11/7/2017,Plunger System,Plunger,Plunger,PCS,,Not Optimized,had to vent plunger up ,user_53,asset_839,48.2726595,-102.8721127
10/18/2018,Tanks/Pits,Liquid Level Control,,,,,"Was forced to shut in well due to a high water tank. Level is 18'4""x17'4"". Bleed down unit. Shut and tagged wellhead.",user_120,asset_166,48.41298624,-103.5863817
1/25/2019,Tanks/Pits,Tank Level,Probe,,,Calibration Issue, 4. Five mile 24-130 - False high tank • Worked with Justin on this task • Found Tank ID04 reading 18 feet in PI • Found tank level spiked up around 8:50 last night • Found water tank transmitter broken due to tank tube fell into tank and snapped transmitter tape • I was able to reach into tank and retrieve tank tube • We re-installed tube and secured it so it won't fall back into the tank • Replaced broken tank transmitter tape • Tested and verified transmitter now reading accurate levels • Tested and verified HLA switch functioning correctly • Found bath heater burner down • Cleaned out plugged pilot tip and relit burner Well is ready for optimization to reset high tank,user_38,asset_1741,40.5262342,-113.8824849
12/10/2018,Compressor,Compressor,Process Gas Supply,Ariel,,Liquid Carryover,"Issue: run status shows comp is running but units are at line pressure Root Cause: Human Error, found some one put in a lot of time to thaw out the line and open the valve that bypasses the compressor. so with that valve open the compressor was recycling all of its own gas and really not compressing any thing. Fix: closed the valve and the compressor started pulling the pad down ",user_170,asset_1720,43.56424,-91.351691
10/6/2018,Tanks/Pits,Flare/Combuster,,,,,SCC “A” pilot was relit after it was extinguished by rainfall. ,user_68,asset_2168,48.12573411,-103.6162038
10/3/2018,Gas Scrubber Separator,ESD,,,,,Issue: Flexing for well Deferral Root Cause: found the hi/low shut and looks to have pressure locked. Fix: got the hi/low open and the well came back on watched for a bit to make sure everything was okay and the well was flowing great left as is ,user_170,asset_2189,43.252261,-115.0567324
8/29/2017,Gas Scrubber Separator,ESD,,,,,Went to rtp well. Could not get skinner valve to actuate on JSAMS. Checked out the fisher control box found a bad block and bleed. Going to order part and get replaced. ,user_103,asset_1815,48.19411741,-103.7558756
2/22/2019,Separator,Choke Valve/Loop,,,,Freezing, +EandJ HEATER HAD BEEN FUELED BUT NOT RESTARTED *RESTARTED HEATER +ONLY ONE BURNER WORKS * ASKED TL TO CONTACT E AND J * THEY ARE ON THE WAY TO TROUBLESHOOT,user_34,asset_1810,48.224585,-103.8291059
5/3/2018,Tanks/Pits,Flare/Combuster,,,,,SCC B out due to rain. Could not relight remotely due to igniters needing adjusted. Adjusted igniter and lit SCC.,user_50,asset_345,48.1470144,-103.6180489
2/15/2017,Tanks,Valving/Swedges,Body,Other,Other,Other,Thawed out blow down valve,user_62,asset_1910,48.2816201,-102.855151
1/31/2018,Compressor,Compressor (Recip),Process Gas Supply,,,,"comp called out went down while I was at Dr23, it went down on high discharge, must have a lateral freeze again, I started it but the psi is climbing-nope went down again-high discharge watching the meter it looks like a lateral freeze again-shut the suction & blew everything down-",user_131,asset_1346,40.7126799,-114.1193569
2/1/2019,Heater Treater,Burner,Fire Tube,,,Freezing,GLYCHOL WAS VERY LOW NOT ALLOWING T12 TO FUNCTION CORRECTLY **TURNED T12 DOWN VERY LOW WHILE AWAITING GLYCHOL +GLYCHOL DELIVERED YESTERDAY AFTERNOON **T12 THERMOSTAT TURNED BACK UP AND SET FOR 90 DEGREE BATH 60 DEGREE VESSEL,user_34,asset_1271,48.1508,-103.6191904
1/6/2018,Chemical System,Pump,Plunger,Texam,HBC1,Wear,1 glycol pump was stalled out. Bleed off and restarted. 2 nd pump from the west. ,user_156,asset_1168,48.20700081,-103.6214182
5/5/2018,Wellhead,Tubing,,,,hydrate,"Jawbone 31-1 went to location to open choke and tubing was at 160psi. opened casing to equalize and tubing is froze. don’t know if well has a plunger, so didn’t try to break freeze. meth tank empty, left equalized.",user_71,asset_1321,48.1470144,-103.6180489
1/10/2018,Dehy,Contactor,Shell,,,,"WFS has a freeze in the dehy, the freeze knocked down the compressor, once freeze was broke i restarted compressor and RTP'd well",user_53,asset_1357,48.1602322,-103.6171901
1/1/2018,Compressor,Compressor,Suction Controller,Ariel,,Vibration,"Compressor went down on lo interstage, found root cause to be hpg-30 was out of adjustment, was able to get suction controller valve back into spects for pressure control, tighten up jam nut to adjustment screw, verified repair ",user_122,asset_1196,48.36286092,-103.7893546
10/24/2017,Tanks/Pits,Flare/Combuster,,,,,#2 down Light,user_111,asset_56,48.05177849,-103.444926
12/19/2017,Tanks/Pits,Flare/Combuster,,,,,Re-lit SCC A after thawing fuel. Root cause is temperature on separators was 100 degrees causing lots of fluid carry over to SCC supply gas. Adjusted unit temps down to 70 degrees.,user_62,asset_629,48.1470144,-103.6180489
10/28/2018,Heat Medium,Pump,Process Indicator,Texam,HBC1,Power Supply,"too much pressure to pump blew diaphragm, 80 psi, WM for pump, shut pump off, ",user_31,asset_1059,43.252261,-115.0567324
12/20/2017,Gas Scrubber Separator,Choke Valve/Loop,,,,Trash,This is a cyclonic sales line valve ,user_119,asset_1481,48.1470144,-103.6180489
2/28/2019,Separator,Choke Valve/Loop,,,,Freezing,Well was shut in earlier in the winter for surface freezes. Found sales line was froze as I was getting things warmed up and tried to flow well. Shut in sales line for around 30 minutes and left it open to atmosphere and was able to get sales line freeze to break. ,user_15,asset_2019,39.2506642,-92.4357879
5/16/2019,SWD System,Particle Filter,Shell,,,,"Tried to use my long prybar to open lid. Wouldn't budge. Attempted to grease lid, wouldn't take any grease. Sprayed lubricant on swivel. Still wouldn't move. Had to use a maintenance crew tool to move filter pot lid to gain access to filters.",user_55,asset_538,,
2/21/2019,Separator,Choke Valve/Loop,,,,Trash,Can not access location because road to location is drifted in and needs plowed ,user_10,asset_1925,48.1470144,-103.6180489
12/14/2017,Separator,Choke Valve/Loop,,,,Freezing,Choke was froze broke freeze,user_86,asset_1970,,
4/11/2018,Wellhead,Tubing,,,,,Needed vent ,user_86,asset_510,,
1/10/2019,Flare System,Flare Header,Regulator,,,,Issue: found SCC # 4 down on the HMI Root Cause: found the fuel gas froze going to the SCC's where it goes threw the burn Fix: broke freeze blew line dry. needs to be blown clean once a year or so to clear out the residual fluid build up or from one of the units flooding out. cleared out relight and returned to service ,user_170,asset_1029,40.5262342,-113.8824849
9/22/2019,Automation,Cable,Data Cable,Automation-X,,Loose Connection,"gauged tanks, will have a condo load 9-23-19, compressor is running loaded, but with only 500 psi discharge psi, guess thats a good sign, wells are flowing, meth is going, drain dezzi, and scrubbers, 34 degrees here this morning, need to get elect glycol pumps running, W/M in for automation to power up in breaker building, i am not qulified to open breaker box. i will follow up with another Work request, besides winterization, bath is warmed up just need heat tape and elect, glycol pumps turned on, ",user_77,asset_943,40.5262342,-113.8824849
4/30/2018,Wellhead,Wellhead Piping,,,,hydrate,broke flow line freeze. returned well to production. contacted optimizer,user_11,asset_658,40.7126799,-114.1193569
9/14/2018,Separator Inlet Valve (XV),Pneumatic Control System,Electrical,,,,"si on valve misalignment , controlled valve open , no issue found",user_144,asset_1106,48.1470144,-103.6180489
4/19/2018,Compressor,Compressor,Process Gas Supply,Ariel,,Trash,"Issue: compressor down alarm Root Cause: Off skid recycle. the compressor went down on low discharge pressure and that comes from using the off skid recycle. The on skid recycle works between the 1st and 2nd stage so when the on skid recycle starts to open and the RPM's are in auto the compressor starts to idle itself down to conserve gas. so if the compressor is in full recycle the set points change to allow the pressures to match the comp being in recycle and the RPM's are backed way down to keep from using any unnecessary gas and keep it from overheating the recycle and as wells turn back on the recycle closed the RPM's come back up and the set points go back. But when we use our off skid recycle the compressor doesn't know there is not a well flowing so the RPM's never back down so we use up a ton of gas for no reason other than to recycle the compressor set points are made/set to account for that kind of recycle. The other very big problem from using the off skid recycle is that the discharge on the compressor is what feeds us the higher pressure to operate the ESD's so this location is running 3burners, 3 SCC's. 6glycol pumps and methanol pumps so with the pad using all this gas and now the compressor using the discharge gas as well the gas is used up quickly and then the compressor goes down on low discharge pressure and buy that time is now low enough the pad starts shutting in on valve fault. once this all happens then the true work begins because the compressor is down and used up all the discharge pressure now we have to find a well with enough pressure to get the whole pad pressured up and enough pressure to open an ESD so that you can start the compressor to get gas back to run the pad Fix: got a well to give enough gas to get the compressor restarted and save the rest of the pad ",user_136,asset_1393,48.1470144,-103.6180489
3/2/2017,Gas Scrubber,Other,Other,Other,Other,Other,Choke Froze - no production ,user_138,asset_2025,48.07879931,-103.4788138
6/29/2017,Instrumentation,Transmitter,Flow,ABB,1151,End Of Usefu
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